ML20114B809

From kanterella
Jump to navigation Jump to search
Environmental Assessment & Finding of No Significant Impact Re 910924 Application for Amend to License,Increasing Rated Core Power Level from 3,293 Mwt to 3,430 Mwt
ML20114B809
Person / Time
Site: Fermi DTE Energy icon.png
Issue date: 08/24/1992
From: Marsh L
Office of Nuclear Reactor Regulation
To:
Shared Package
ML20114B811 List:
References
NUDOCS 9208310261
Download: ML20114B809 (6)


Text

..

7590-01 UNITED STATES NUCLEAR REGULATORY COMMISSION DETROIT EDIS0N COMPANY FERMI-2 DOCKET NO. 50-341 Lt(y1RONMENTAL ASSESSMENT AND FINDING OF NO SIGNIFICANT IMPACl The U. S. Nuclear Regulatory Commission (the Commission) is considering issuance of an amendment to facility Operating License No. Npf-43 issued to the Detroit Edison Company (DECO or the licensee) for operation of the Fermi-2 facility, located in Monroe County, Michigan.

ENVIRONMENTAL ASSESSMENT Identification of Pronosed Action:

This Environmental Assessment is written in connection with the proposed core power level increase for the Fermi-2 facility in response to the licensee's application for a license amendment dated September 24, 1991 as modified January 31, and April 30, 1992. The proposed action would increase the rated core power level for Fermi-2 from the current level of 3293 megawatts thermal (MWt) to 3430 MWt.

The Nuclear Steam Supply System (NSSS) power level would be increased accordingly.

This represents an authorized 2

power level increase of-approximately 4.2 percent.

This will require resetting of the safety relief valve setpoints to accommodate the slight operating pressure increase (less than 40 psi). Operating temperature will also increase slightly (1sss than S*F). ;The result of these changes will be an approximate S percent increase in NSSS power level.

Plant instrumentation i

v208310261 920024 DR ADOCK 05000 1

_ _. _.. _ _ _ _. _ _. - _ _ _ _ _ _ _ _ _ _ _. _ _ _ _ ~ _

-2 will be recalibrated to reflect the uprated power and core reload design will be modified to maintain the current 18-month reload cycle.

This will include the use of higher enrichment fuel with extended burnup over that currently used.

The licensee is planning to use fuel enrichments up to 4.8 weight percent U-235 and burnup to 49,100 megawatt days per metric ton uranium (MWD /MTU).

The licensee will implement these changes during the third refueling outage currently scheduled to begin September 12, 1992.

Additionally, at the recommendation of their NSSS vendor. the licensee is restoring a Reactor Core Isolation Cooling (RCIC) bypass line which had been previously removed.

No changes will be made to the basic fuel design =and fuel operating limits such as maximum average planar linear heat generation rate (MAPLHGR) or minimum critical power ratto (MCPR) will-still be met at I

uprated power.

These changes will be achieved by increasing core flow along existing flow control lines of the power / flow map thereby slightly increasing reactor vessel dome pressure.

However, there will not be an increase in the maximum recirculation flow limit over the pre-uprate value.

The Need for the Proposed Action:

The action would increase the thermal output by 138 megawatts thermal (MWt) which corresponds to approximately 44 megawatts electric (MWe).

This would provide additional power to the grid which supplies the licensee's service area. The changes in higher fuel enrichment and extended burnup are necessary in order to maintain the current 18-month operating cycle.

l l

2

.0 I

l Environmental Impacts of the Proposed Action:

l The effect of power uprate on radiological effluent or offsite doses, as evaluated in the Environmental Report, Operating Licensing Stages (ER/0L) and the NRC Final Environmental Statement (fES), is not significant. The original analyses were based on 104.2% (3430 MWt) of the licensed power (3293 MWt).

The analyses for peeer uprate were performed at 102% of uprated power, resulting in a calculated increase of approximately 2% in effluent s and doses, still well within 10 CFR Part'50, Appendix I, limits.

A slight increase in occupational radiation exposures may occur due to the slight increase in radiation levels in some areas of the plant, primarily due to increased activation products.

The licensee used conservative assumptions; the design radiation source increase is proportional to the increase in power.

Even with this assumption, neither individual ncr i

cumulative occupational radiation exposure will be significantly increased.

The expected increase would not be more than four to five percent of the current occupational exposure.

The non-radiological environmental impacts of the proposed power uprate were reviewed based on the information submitted in the ER/0L, the FES, and the requirements of the Environmental Protection Plan (EPP), Section 3.0 (Appendix B to the Operating License).

Based on this review, it was concluded that the proposed uprate will not have significant impacts on the non-radiological effluent or releases and the plant will be operated in a manner as established by the FES.

Existing Federal, State, and local regulatory permits presently in effect will not need to be modified as a result of power uprate.

- -... _..... -.. -., -. -. - -.... - -.... - - ~..

. There will not be any significant change in the types or amounts of any effluents that may be released offsite as a result of power uprate which have not already been evaluated in the FES or any significant increase in individual or cumulative occupational radiation exposure.

The Commission has completed its evaluation of the use of higher enriched fuel and extended burnup which would be necessary to support the proposed action.

The enviranmental consideration associated with reactor operation with higher enrichment and extended irradiation have been previously evaluated by the NRC staff for enrichment, up to 5.0 weight percent U-235 and burnup of up to 60.000 MWD /MTV (53 FR 60340 dated February 29, 1988).

The staff has concluded that such changes would not adversely affect plant safety.

The proposed changes have no adverse effect on the probability of any accident.

The higher enrichment, with fuel burnup to 60,000 MWD /MTU, may slightly change the mix of fission products that might be released in the event of a serious accident, but such changes would not significantly affect the consequences of serious accidents.

No changes are being mace in the types or amounts of any radiological effluent that may be release offsite.

There is no significant increase in the allowable individual or cumulative occupational radiation exposure.

With regard to potential non-radiological impacts of reactor operations with higher enrichment and extended irradiation, the proposed changes to the l

Technical Specifications (TS) involve systems located within the restricted area are defined in 10 CFR Part 20. They do not affect non-radiological plant effluents and have no environmental impact.

1

.s.

The environmental impacts of transnortation resulting from the use of i

higher enrichment fuel and extended irradiation were published and discussed in the staff assessment entitled, "NRC Assessment of the Environmental Effects i

of Transportation Resulting from Extended Fuel Enrichment and Irradiation,"

dated July 7,1988, and published in the f3dgal llegittu on August 11, 1988 (FR 53 303555) as correcitu August 24, 1988 (53 FR 32322), in connection with the Shearon Harris Nuclear Power Plant, Unit '1, Environmental Assessment and finding of No Significant Impact.

As indicated therein, the environmental cost contribution of the proposed increase in the fuel enrichment and irradiation limits are either unchanged or may, in fact, be reduced from those summarized in Table S-4 asset forth in 10 CFR 51.52(c).

These findings are applicable to the propos?d change for fermi-2.

Therefore,' the Commission concludes that there is no sighificant radiological or non-radiological environmental impacts associated with the proposed amendment.

Alternative to the Proposed Action:

Since the Commission concluded that there are no significant environmental effects that would result from the proposed action, any other alternatives would have equal or greater environmental impacts and need not be 4

evaluated.

The principal alternative would be to deny the requested amendments.

This would not reduce the environmental impacts of plant operations and would I

i result in reduced operational flexibility.

l l

, s t

a

' Alternative Use of Resources:

This action does not involve the use of any resources not previously considered in the Final Environmental Statement dated July 1972 related to operation of the Fermi-2 facility.

Aaencies and Persons Consulted:

The NRC staff reviewed the licensee's request and did not consult other agencies or persons.

FINDING Of NO SIGNIFICANT IMPACT Accordingly, the Commission has determined not to prepared an environmontal impact statement for the proposed license amendment.

Based upon the foregoing environmental assessment, we conclude that the proposed action will not have a significant effect on the quality of the human environment.

For further details with request to this action, see the application for amendment dated September 24, 1991 as modified January 31 and April 30, 1992, which is available for public inspection at the Commission's Public Document Room, 2120 L Street, N.W., Washington, D.C. and at the Monroe County Public Library, 3700 South Custer Road, Monroe, Michigan 48166.

l Dated at Rockville, Maryland, this 24th day of August 1992.

FOR THE NUCLEAR REGULATORY COMMISSION Ledyard B. Marsh, Director Project Directorate 111-1 Division of Reactor Projects Ill/IV/V Office of Nuclear Reactor Regulation 1

r

....- ~,,.....- -,

.,.--,,..rm..,~,.-

~.

-