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Category:REPORTS-TOPICAL (BY MANUFACTURERS-VENDORS ETC)
MONTHYEARML20113H4961992-04-30030 April 1992 Rev 0 to Licensing Topical Rept Nutech Feedwater Nozzle Bypass Leakage Monitoring Sys,App:Results for Browns Ferry Unit 2,June-Dec 1991 ML20059L4961990-08-31031 August 1990 BWR Owners Group NUREG-0578 Implementation: Analyses & Positions for Plant-Unique Submittals ML20235Z0491987-03-17017 March 1987 Nonproprietary Topical Rept, RDS-1000 Radwaste Dewatering Sys ML20113H5051986-09-0505 September 1986 Rev 0 to Licensing Topical Rept Nutech Feedwater Nozzle Bypass Leakage Monitoring Sys,App:Results for Browns Ferry Unit 1 ML20113H4991986-09-0505 September 1986 Rev 0 to Licensing Topical Rept Nutech Feedwater Nozzle Bypass Leakage Monitoring Sys App:Results for Browns Ferry Unit 3 ML18030B0411985-12-31031 December 1985 Radiological Impact of Ventilation Damper Closing Time During Design Basis Fuel Handling Accident. ML20128A0421985-05-31031 May 1985 Rev 2 to LOCA Accident Analysis for Browns Ferry Nuclear Plant Unit 2 ML20112F6931984-08-31031 August 1984 Core Region Matls Info (Units 1,2 & 3) ML20077C8841983-05-31031 May 1983 Rev 1 to LOCA Analysis for Browns Ferry,Unit 1 ML20069J1721982-08-31031 August 1982 Errata & Addenda Sheet 5 to NEDO-24088-1, LOCA Analysis for Browns Ferry Nuclear Plant,Unit 2 ML20069J1691982-07-31031 July 1982 Errata & Addenda Sheet 4 to NEDO-24088-1, LOCA Analysis for Browns Ferry Nuclear Plant,Unit 2 ML18025B8221982-07-23023 July 1982 BWR Transient Analysis Model Utilizing Retran Program, Second Part ML20028G3681982-05-31031 May 1982 Safety Review of Browns Ferry Nuclear Plant Unit 1 at Core Flow Conditions Above Rated Flow During Cycle 5. ML17276B8021981-12-31031 December 1981 BWR Transient Analysis Model Utilizing Retran Program. ML20039B7011981-12-0909 December 1981 Errata to LOCA Analysis, Sheet 1 ML18025B7101981-09-21021 September 1981 Method for Development of One-Dimensional Core Kinetics Data for RETRAN-02. ML20041E4721981-05-31031 May 1981 Plants,Units 1,2 & 3 Single Loop Operation. ML20126J6151981-04-30030 April 1981 Errata 2 to LOCA Analysis for Browns Ferry Unit 1 ML18030B2231980-09-30030 September 1980 DC Power Source Failure for Browns Ferry Nuclear Power Station,Units 1,2 & 3. ML20147D6701980-09-0808 September 1980 In-Vessel Neutron Spectral Analysis ML19270F6121979-01-31031 January 1979 Verification of TVA Steady-State BWR Physics Methods. ML19270F6141978-06-0101 June 1978 Three-Dimensional LWR Core Simulation Methods. ML19270F6131978-04-15015 April 1978 Methods for Lattice Physics Analysis of Lwr'S. 1992-04-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML20217F9671999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML20212E6341999-09-23023 September 1999 Suppl to SE Resolving Error in Original 990802 Se,Clarifying Fact That Licensee Has Not Committed to Retain Those Specific Compensatory Measures That Were Applied to one-time Extension ML20212D3831999-09-20020 September 1999 Safety Evaluation Supporting Proposed Rev to Withdrawal Schedule for First & Third Surveillance Capsules for BFN-3 RPV ML20212B8561999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Browns Ferry Nuclear Plant.With ML18039A8821999-08-31031 August 1999 Increased MSIV Leakage Tech Spec Change Submittal - Seismic Evaluation Rept. ML18039A8391999-08-0606 August 1999 BFN Unit 2 Cycle 10 ASME Section XI NIS-1 & NIS-2 Data Repts. ML20210N1221999-08-0202 August 1999 Safety Evaluation Accepting Licensee Request for Relief from ASME B&PV Code,Section XI Requirements.Request 3-ISI-7, Pertains to Second 10-year Interval ISI for Plant,Unit 3 ML20210R0931999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML20209J0771999-07-16016 July 1999 Safety Evaluation Concluding That Licensee Provided Adequate Information to Resolve ampacity-related Points of Concern Raised in GL 92-08 for BFN & That No Outstanding Issues Re GL 92-08 Ampacity Issues for Browns Ferry NPP Exist ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML20209H4381999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML20196F8811999-06-23023 June 1999 Safety Evaluation Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power Operated Gate Valves ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML20196B8051999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7761999-04-30030 April 1999 Revised Surveillance Specimen Program Evaluation for TVA Browns Ferry Unit 3. ML20206R0731999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Bfnp.With ML18039A7561999-04-23023 April 1999 Bfnp Risk-Informed Inservice Insp (RI-ISI) Program Submittal. ML18039A7671999-04-0808 April 1999 Rev 0 to TVA-COLR-BF2C11, Browns Ferry Nuclear Plant Unit 2 Cycle 11 Colr. ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML20205N8341999-04-0101 April 1999 Part 21 Rept Re Automatic Switch Co Nuclear Grade Series X206380 & X206832 Solenoid Valves Ordered Without Lubricants That Were Shipped with Std Lubrication to PECO & Tva.Affected Plants Were Notified ML20205F9341999-04-0101 April 1999 Safety Evaluation Authorizing Licensee 990108 Relief Request PV-38,from Requirements of ASME BPV Code Section XI IST Testing,Valve Program for Plant,Units 1,2 & 3 ML20205T5441999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Bfnp.With ML20205S0601999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with Status Change from Previous Update,990331 ML20205S0661999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with No Status Change from Previous Update,990331, Atlas Corp ML18039A7361999-03-11011 March 1999 Rev 4 to TVA-COLR-BF2C10, Bfnp,Unit 2,Cycle 10 Colr. ML20204C7891999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6931999-02-0303 February 1999 Rev 3 to TVA-COLR-BF2C10, Bfnp Unit 2 Cycle 10 Colr. ML18039A6941999-02-0303 February 1999 Rev 1 to TVA-COLR-BF3C9, Bfnp Unit 3 Cycle 9 Colr. ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6661998-12-31031 December 1998 Ro:On 981215,HRPCRM 2-RM-90-273C Was Declared Inoperable. Caused by Downscale Indication.Containment RM Will Be Utilized as Planned Alternate Method of Monitoring Until Hrpcrm 2-RM-90-273C Can Be Returned to Operable Status ML20199K8951998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Browns Ferry Nuclear Plant.With ML20199F2721998-12-31031 December 1998 ISI Summary Rept (NIS-1), for BFN Unit 3,Cycle 8 Operation ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML20199F2791998-12-0303 December 1998 Bfnp Unit 3 Cycle 8 ASME Section XI NIS-2 Data Rept ML20198D9621998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Bfn,Units 1,2 & 3. with ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr 1999-09-30
[Table view] |
Text
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d.h 4.
XTV-01-105 Revision 0 i September 1906 l' I l e fi u m n e r 165.1501.0105
, LICE!1 sit 1G TOPICAL llEPOflT 11UTECil PEEDWATEll 110ZZLE DYPASS LEAKAGE M0111TORIt1G SYSTEli APPEt1 DIX: RESULTS FOft IIROWilS FEltitY Ut1IT 3 Prepared for Tennesace Vr.lley Aut.hority Prepared by 11UTECil Engineers, Inc.
San Jose, California Prepared by: Apjeroved by hktf d fkNo*x .Y A - -
W M. 10 Kleinamith C.. II . Proch11ch, P.E.
Project Engineer Engineering Manager i
Issued by:
[. .
Date: bh / C/ 9 [> _
l Mones Tay1 r, J r. , P.E.
Project. Manager l
9200040115 920729 .
PDR ADOCK 05000259 l] (l{ @ C.:l.]-
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' i REVISION CONTROL SHEET Licensing 'Ibpical Ibrort TITLE.ju11DI l'eedsater ibzzle DyinSG DOCUMENT FILE rdUMBER 165.1501.0105 Icakage obnitoring Syst.wn Appealix: Insults for Urcw n Terry Unit 3
/J. G. Cofic/ Technical 1.cader wcc INITIA U N AME / TITLE M. E. Kleinsmith/ Project Engineer Nff'/'
NAuf / TITLE ' N ' I ' I INI T I A .$
N AME / TITLE HAME / TITLE INiilA M PREPARED ACCUHACY CHITERIA "IM*""I AFFECitD DOC P AGt ts) nty BY I DAf t CllECK BY / DATE CHECK BY / DATE D
, sac 1/r/s6 *'c
- N' Initial Issm klii 0 N('gf l B(, /
^;1; o gqy.g.u ~.,,tr/a ~ >I* 6 PAGF: I Of l
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n TADI,E OF _ cot 1TEtiTS Page t.0 I!!TitODUCTIO!1 A.I 2.0 DISCUSSIOli A.I 3.0 METilOD OF AtlALYSIS A.2 s l 4.0 ItESULTS A.4 5.0 PATIGUE USAGE PACTOil A.4 6.0 ItECOMMEllDATIOtlS A.5 7.0 ItCPERCllCES A.10 TADLE I A.6 TAllLE II A.6 TABLE III A.6 TADLE IV A.7 FIGURE 1 A.D FIGURE 2 A.9 s
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XTV-01-105 A.iii nut.e....c..h,
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1.0 I t1 Tit 0 DUCT 10ti_
The feedwater nozzles of Tennessee Valley Authority's Browns Ferry Unit 3 nuclear power plant were modifled by installing triple thermal sleeve spargers. This d
modification was made to minimize thermal sleeva bypass leakage, which leads to rapid thermal cycling due to turbulent mixing of cold feedwater and hot reactor -
water. Rapid thermal cycling nas been identified as the major cause of observed cracking of icedwater nozzles, as discussed in itUREU-0619 (Reference 1).
140TECl! provided Tennessee Valley Authority with a leak-g age monitoring system (LMS) to monitor the effectiveness of the new thermal sleeves in preventing leakage. Data taken from the LMS during plant operation (November 15, 1984 to March 19, 1985, see Reference 2) was sent to _
tJUTECll for analysis. That analysis 10 now complete and results are presented in this report.
2.0 DISCUSSION The leakage monitoring system consists of four thermo-couples attached to the outside of each of thc six feedwater nozzles (one at the top and three at the bottom). These thermocouples monitor the nozzle's XTV-01-105 A.1 nutg_cj]
i.h outside temperature downstream of the thermal sleeve seal. The temperature at this location correlates well with the amount of bypass leakaget the greater the leakage the lower the temperalure. .
e' 3.0 METHOD OF ANALYSIS l
The first step in analyzing each nozzle for leakage is to group the data by reactor power level (or percent feedwater flow) and then average the data from the bottom three thermocouples for each nozzle. Each thermocouple data point is then expressed as a factor of the difference between reactor and feedwater tempera-tures. This' process is referred to as normalization gggg (see Reference 3).
T ~I FW Tg = T/C III T -T RX FW Where Tg = Normalized temperature
= Bottom average temperature TT/C Tpg = Feedwater temperature T gx = Peactor; temperature The Icakage rate may now be calculated from XTV-01-105 A.2
~
.t .
. i
- T -T N
[ L" (To -T 1.5
} x 1.5 gpm (2) 1 Where L = Analytically determined 1 akage rate in gallons per minute el To = Analytically determined normalized temperature at 0 leakage T1.5
= Analytically determined normalized temperature at 1.5 gpm leakage To and T1 .5 were determined from finite element analysis of the Browns Perry feedwater nozzle configuration (Reference 5). Based upon Browns Perry data and analysis, 14UTEcli selected 0. 57 for T o and 0.12 for T1.5 d,'
in the Browns ,arry 3 leakage calculations.
Substituting T o and T1.5 back into equation (2) gives 0.57 - T 0.57 - T L * (0.57 - 0.12
Therefore, equation (3) is the equation for bypass i
! leakage around the triple-sleeve spargers at Browns i
Perry 3.
- w XTV-01-105 A.3 nut.e. c..h..
e
- .6 .
4.0 RESULTS
/*
i The analysis of the LMS data at Browns Ferry 3 revealed that no significant bypasa lenkage is present at any of the feedwater nozzles. This result var to be expected d since these spargers are newly installed. Tables I, II, and III summarize the resu'*.s of leakage calculations done at 100%, 90%, and 80% ftedwater flew rates _
(Reference 4). t1egative values should be interpreted as zero leakage.
5.0 FATIGUE USAGE FACTOR Since there l's no leakage around the thermal sleeves, ELM 893 there is minimal contribution to the fatigue usage tactor due to rapid thermal cycling. Figure 1 is a ple ;
of fatigue usage factor vs. constant leakage over a 40-year period for the Browns Ferry 3 station (based on the Thermal Duty Map presented in Table IV, from Reference 5). As can be seen from this figure, the contribution to the fatigue usage factcc is quite small for leakaga rates of about 1.0 3pm or less. However, $
the fatigue usage factor increases rapidly for leakages above this level. The usage factor for a leakage rate of 1.5 gpm is 0.543 after 40 years, which is less than the code allowable value of 1.0.
(
XTV-01-105 A.4 nutega 1 - -
d.h figure 2 presents a graph of IJiS temperaturen versus leakage (Reference 4). As the temperature falls below about 390*F, the correlation 'with leakage bcsaks down.
If the temperature does fall below 390*, the leakage is 8
quite high as is the u sage factor.
6.0 RECOMMEt1DATIOtJS, The data analyzed through March 19, 1985 indicates that, up to this date, the newly installed triple sleeve spargers are not leaking. However, continued tempera-ture monitoring of the outside surface of the feedwater nozzles is important to assure that with time, any leakage that may occur is detected.
Data should be taken on an hourly basis when the plant ,
is in start-up or shut-down, and bi-weekly when the plant is at or near full power. This data should be plotted versus time, to determine trends of thermal sleeve seal performance. 5t ep changes in the calculated leakage rate may be an indication of a malfunction in the LMS.
XTV-01-105 A.S nLit.GC1. -.
^ - - - - - - - - - - - - . _ _ . _ _ _ - - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
. I' Table I LEAKAGE CALCULATED AT POWER = 1001 (Reference 4)
NOZZLE LEAKAGE (GPM) 1
- -0.209 2 -0.107 3 -0.311 j
4 -0.470 5 -0.362 6 -0.107 Table II LEAKAGE CALCULATED AT POWER = 90% (Reference 4)
NOZZLE LEAKAGE (GPM) 1 -0.191 2 -0.056 M 3 -0.288 4 -0.456 5 -0.288 6 -0.049 Table III
' LEAKAGE CALCU,ATr.D L AT POWER = 80% (Reference 4)
NOZZLE LEAKAGE (GPM) 1
-0.247 2 -0.065 3
-0.299 4 -0.462 5 -0.306
-0.072, 6
XTV-01-105 A.6 nutgg,lj
r.
l .i _
l Table IV
/ BROWNS PERRY PLANT SPECIFIC TiiERMAL OUTY MAP (Reference 5)
Region, % Power flours / year Rx Temp, FW Temp.
' 372.00 I 100.00 5520.00 539.00 2 95.00 1195.00 539.00 360.00 3 80.00 373.00 539.00 350.00 4 70.00 302.00 539.00 337.00 5 50.00 94.00 539.00 315.00 6 50.00 3.00 539.00 285.00 40.00 42.00 539.00 305 00 7
8 40.00 14.00 539.00 240.00 9 32.00 14.00 539.00 185.00 10 23.00 12.00 539 00 175.00 11 23.00 8.00 539 00 120.00 12 15.00 16.0C 539.00 120.00 13 5.00 64.00 530.00 120.00 14 5.00 14.00 470.00 120.00 15 5.00 10.00 360.00 120.00
$N$$
16 5.00 40.00 240.00 120.00 17 5.00 40.00 512.00 210.00 18 5.00 29.00 298.00 210.00 19 5.00 13.00 536.00 308.00 _
20 0.00 43.00 340.00 300.00 21 1.00 .40 360.00 350.00 22 2.00 1.78 350.00 190.00 23 2.00 1.38 340.00 125.00 24 2.00 .25 330.00 'O.00 2.00 1.60 400.00 190.00 25
'6 3.00 .38 340.00 160.00 0.00 900.00 70.00 70.00 41 k
XTV-01-105 A.7 1
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3
. . Il.
figure 1
(
(Reference 5)
' 40 YEAR USAGE FACTORS AT COHSTANT LEAKAGE d a t h
U e '
< d f*fMR LL to . -
l3 l0 N .
) O
' ' i 0
1Fi 1.2 5 1.5 0 0.25 0.5 0.75 1 4
LEAKAGE (GPM) s XTV-01-105 A.8 nutg.g}]
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7.0 REFERENCES
\
I 1. NUREG-0619, "DWR Feedwater Nozzle and Control Rod Drive Return Line Nozzle Cracking," April 1900.
- 2. Unit 3 Leakage Monitoring System and Main Steam / Reactor Feedwater Pressure and Temperature Data, November 1984 through March 1985,, File No.
~
165.1501 0016.
- 3. " Licensing Topical Report - NUTECil Feedwater Nozzle Bypass Leakage Monitoring System," Rev. O, dated October 1982, File No. 165.1501.0018.
- 4. NUTECli Calculation Package, " Drowns Ferry Unit 3 Leakage Monitoring System Leak Rate Prediction,"
Rev. O, File No. 165.1501.0303.
- 5. " Structural Integrity Assessment of Browns Ferry Peedwater Nozzles," Rev. O, Document No. XTV 008, File No. 165.1500.0017.
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1 XTV-01-105 A.10 ritit.e.3c.t.i.
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