ML20101U290
| ML20101U290 | |
| Person / Time | |
|---|---|
| Site: | Comanche Peak |
| Issue date: | 06/30/1992 |
| From: | William Cahill, Gina Davis TEXAS UTILITIES CO. |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| TXX-92342, NUDOCS 9207220345 | |
| Download: ML20101U290 (5) | |
Text
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M Log # TXX-92342 EE File # 10010.2 h
j Ref, # 10CFR50,36
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7UELECTRIC July 15, 1992 William J. Cahill, Jr.
Group Vice Presided Director, Office of Resource Management U. S. Nuclear Regulatory Commission Washington, DC 20555
SUBJECT:
COMANCHE PEAK STEAH ELECTRIC STATION (CPSES) - UNIT 1 DOCKET NO. 50-445 MONTHLY OPERATING REPORT FOR JUNE 1992 Gentlemen:
Attached-is the Monthly Operating Report for June 1992 prepared and submitted pursuant _o Technical Specification 6.9.1.5 contained in Appendix A to the Comanche Peak Steam Electric Station Unit 1 Operating License No. NPF-87.
Sincerely.
/
a William J. Cahill, Jr.
JLR/grp Attachment c - Mr. J. L. Milhoan, Region IV Mr. T. Reis, Region IV Resident Inspectors CPSES (2)
Mr. T. A.
Bergman, NRR Document Control Desk F
&. U ' ' H s t
/l/
9207220345 920630 PDR ADOCK 05000445 400 N. Olive street LB. 81 Dallas, Texas 7321 j
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A'ttachrvent to TXX. 92342 Page 1 of 4 COMANCHE PEAK STEAM ELECTRIC STATION, UNIT 1 NRC MONTHLY OPERATING REPORT DOCKETNO:
50 445 UNIT:
CPSES 1 DATE:
July 15,1992 COMPLETED BY:
Glenn Davis TTLEPHONE:
817 897-5277 OPERATING STATUS 1.
Reporting Period: JUNE 1992 Gross hours in reporting period:
22D 2.
Currently authorized power level (MWt):
M11 Max. depend. capacity (MWe-Net): - 115.Q
- Design Electrical Rating (MWe-Net):
115.0 3.
Powerlevelr which restricted (if any)(MWe-Net):
None 4.
Reasons for restriction (if any):
THIS MONTH Y3TO DATE. CUMULATIVE 671.6 4273.2 12688.4 5.
Number of hours reactor was critical 0
20.8-2003.3 6.
Reactor reserve shutdown hours 650.9 4225 12434.2-7.
Hours generator on lino 0
8.
Unit reserve shutdown hours 0
0 1,997,702 13,114,860 33,446,854
- 9.
Gross thermal energy generated (MWH) 662,996
-4.371,325 12,708.323 10.
Gross electrical energy generated (MWH) 11.
Net electrical energy genarated (MWH) 629,t45 4,175.627 12,071,191 12.
Reactor Service factor 93.3 97.9 76.9 13.
Reactor availability tactor 93.3 98.3
-89.0 14.
Unit service factor' 90.4 96.7 75.3 15.
Unit availability factor 90.4 96.7 75.3 76.0
'83.1 63.6 16.
Unit capacity factor (Using MDC)
'76.0 83.1-63.6 17.
Unit capacity factor (Using Design MWe) 9.6 3.3 8.5 18.
Unit forced outage rate 19.
Shutdowns scheduled over next 6 months (Type, Date, and Duration of each):
Refueling outage 2 is scheduled to begin October 1,1992, with a duration of 70 days.
20, if shutdown at end of report period, estimated date of startup:
21.
Units in test status.(prior to commetcial operation):
ACHIEVED C7mmercial Operation 900813-i Estimated
Attachmert to TXX-92342 Page 2 of 4 AVERAGE DAILY UNIT POWER LEVEL DOCKETNO:
50 445 UNIT:
CPSES 1 DATE:
July 15,1992 COMPLETED BY:
Glenn Davis 817-897 5277 TELEPHONE:
MONTH: JUNE 1942 DtY AVERAGE DAILY POWER LEVEL DsY AVERAGE DAILY POWER LEVEL (MWe-Net)
(MWe-Net) 1 1090 t7 1087 2
1097 18 1101-3 362 19 1119 4
424 20 1050' 5
585 21 1089 6
995 22 1092 7
1007 23 1079 8
1096 24
-1083 9
1093 25 1092 10 1095 26
-1085 11 217 27 993 12 0
28 1087 13 0
29 1092 14 174 30-1092 15 768 31 16 1062
Attachment to TXX. 92342 Page 3 of 4
SUMMARY
OF OPERATING EXPERIENCE FOR THE MONTH DOCKETNO:
50-445 UNIT:
CPSES 1-DATE:
July 15,1992 COMPLETED BY; Glenn Davis TELEPHONE:
817 897-5277 MONTH: JUNE 1992 06/01 0000 Unit started.he month in Mode 1, with the reactor operating at approximately 100 percent of rated thermal power.
06/f>J 0215 A plant shutdown was initiated as required tsy plant Technical Specifications after one of two compressors associated with Train A of tle Control Room HVAC system tripped and could not be restarted, Train 8 of the Control Room HVAC system had yeviously been removed from service for corrective maintenance.
(
0250 A Notification of Unusual Event (NOUE) was declared following initiation of tha plant shutdown.
1 0640 The plant shutdown was terminated wnh tho reactor at approxims.le!y 8 percent of rated thermal l
power after Train A of the Control Ro.3m HVAC was retumed to service.
i 0823 The NOUSE was terminated.
1300 Reactor power increase initiated; however, power was required to remain below 50 percent to allow stabilization of tM reactor core flux distribution.
06/05 0542 Commenced increase to 100 pr rcent of rated thermal power.
06/11 0528 The reactor was manually tripped when both niain feedwater pumps tripped due to problems in printed circuit cards in the solid state protection system (SSPS).
06/13 0550 Achieved criticality and began power increase after replacement of several SSPS circuit cards and a relay.
06/23 1948 A thunderstorm damaged transformer 1ST re6utung in the safeguards busses transferring to the attemate power supply and the blackout suquencer actuating.
06/30 2400 Unit ended the month in Mode 1, with the reactor operatirt at approximately 100 percent of rated thermalpower.
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Attachment to TXX. 92342 Page 4 oi4 UNIT SHUTDOWNS AMD POWER REDUCTIONS DOCKETNO-50-445 UNIT:
CPSES 1 DATE-July 15,1992 -
COMFLETED BY:
Glenn Davis g
TELEPHONE-817-897-5277 REPORT MONTH. LUNE 1992 Mc M OF T/PE SHUTTING DO'M4 FfDRCED DUPAT!ON THE REACTOROR LL MIE SSCHEDULED (HOURS 1 REASON REDUCING POWEB CORRECTIVE ACTIONSCOMMENTS 7
920600:
F D
4
- Plant stotdown initiated due to inoperability of both trains of Cor#rol Room HVAC. LER 92-012 submitted 920706 l
8
- 920611, F
69.1 A
2 Manual reactor trip initiated due to loss of feedwater flow. LER 92-014 submitted 920710.
i l
- 2) - MEN
-1)
REASON
)
A-EOU!?MENTFAILURE(EXPLAIN)
E. OPERATORTRAINING AND L' CENSE EXAMINATION 1: MANUAL l8: MAINT OR TEST F: ADMINISTRATIVE 2: MANUALSCRAM C REFUEUNG-O 'OPERATIONALERROR(EXPLAIN) 3: AUTOMAT'CSCRAM 4: OTHER (EXPLAIN)
D: REGU!ATORYRESTR!CTDON H: OTHER (EXPLAIN)
,