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Category:NPDES NONCOMPLIANCE NOTIFICATION
MONTHYEARML20248M1031998-05-26026 May 1998 NPDES Noncompliance Notification:On 980518,spill of Sodium Hypochlorite Occurred.Sys Was Shut Down & Monitoring Was Conducted to Verify That No Detectable Total Residual Chlorine Discharged from Outfall 101 to Tn River ML20245G8971989-04-26026 April 1989 NPDES Noncompliance Notification:On 880801,dead Fish Discovered in Intake Forebay & Sample of Intake Water Analyzed for Total Residual Chlorine.Caused by Release of Sodium Hypochlorite to Water.Levels within NPDES Limits ML20155J0321988-10-20020 October 1988 NPDES Noncompliance Notification:On 880801,util Reported Kill of Approx 278 Fish in Intake Forebay.Caused by Low Dissolved Oxygen Levels in Water Withdrawn from Chickamauga Reservoir.Conditions in Reservoir Improved.Count Terminated ML20151Q2501988-08-0303 August 1988 Noncompliance Notification:On 880711,approx 1,500 Dead Fish Discovered in Diffuser Pond.Species Killed Were Threadfin & Gizzard Shad.Caused by Thermal Stress.Fish Removed & Allowed to Decay in Place ML20100G6401985-03-27027 March 1985 NPDES Noncompliance Notification:On 850107,11,18 & 31,temp Rise Limit & Rate of Temp Change Limit Exceeded at Diffuser Discharge Gate.Caused by Malfunctions of Equipment,Including Cooling Tower Lift Pumps ML20099G4871985-03-0505 March 1985 NPDES Noncompliance Notification:On 840808 & 10,total Residual Chlorine Concentrations Exceeding Permit Limitation Detected in Grab Samples.Caused by Malfunction of Sodium Hypochlorite Pumps.Pumps Repaired ML20091F8751984-05-28028 May 1984 NPDES Discharge Monitoring Repts for Feb-Apr 1984 ML20076E1021983-05-23023 May 1983 NPDES Noncompliance Notification:On 830326 & 28,temp Rise Between Upstream Ambient Monitor & Downstream River Monitor Exceeded 5.4 F Limit.Caused by Low Riverflows.Cooling Tower & Increased Riverflows Used to Eliminate Delta Temp Changes ML20069H6971983-03-31031 March 1983 NPDES Noncompliance Notification:On 830314,samples of Effluent Yard Drainage Pond Exceeded Allowable Ph Values. Caused by Accidently Damaged Sodium Hydroxide Tank Valve Releasing Contents Into Drainage Sys.Personnel Counseled ML20071D9461983-03-0808 March 1983 NPDES Noncompliance Notification:On 830223,grab Sample Collected from Concrete Batch Plant Settling Pond Contained 53 Mg/L Total Suspended Solids.Caused by Rainfall Runoff Vol Exceeding Treatment Capacity of Pool.No Action Taken ML20079P3271983-02-16016 February 1983 NPDES Noncompliance Notification:Determined That Natl Pollutant Discharge Elimination Sys Permit Should Be Issued W/No Substantial Changes from Tentative Determinations Previously Announced ML20055C0801982-08-0505 August 1982 NPDES Noncompliance Notification:On 820721,three Samples of Yard Drainage Pond Effluent Contained Oil & Grease Concentrations Exceeding Daily Max Permit Limitation.Caused by Tanker Overflowing.Oil Absorbent Pillows Deployed ML20058J5651982-07-22022 July 1982 NPDES Noncompliance Notification:On 820707,diffuser Discharged Into Tn River.Caused by Analytical Error Re Inoperable Titrator.Titrator Repaired & Returned to Svc. Spare Parts for Titrator on Emergency Order ML20054E9071982-06-10010 June 1982 Notification of 820515 Noncompliance W/Effluent Limitations Re Diffuser Gate Discharge to Tn River.Cause Unknown. Increase in Release Vol from Chickamauga Dam Initiated to Increase Riverflow Past Plant to Increase Mixing Ratio ML20050B7981982-04-0101 April 1982 NPDES Noncompliance Notification:On 820304 Svc Bldg Sump Samples Contained Concentration of Oil & Grease in Excess of Tech Specs Limit.Caused by Sump Not Being Cleaned Daily to Remove Normal Buildup of Oil.Sump Will Be Cleaned Daily ML20038C9101981-12-0909 December 1981 NPDES Noncompliance Notification:On 811130,svc Bldg Sump Sample Exceeded Max Permit Limitation of Total Suspended Solids.Caused by Plant Workload Precluding Routine Sump Cleaning.Sump Cleaned on 811202 ML20004C4651981-06-0101 June 1981 NPDES Noncompliance Notification:On 810319,sample Const Sewage Treatment Plant Effluent Had Ph of Less than Min Limits.Cause Not Known.Sodium Bicarbonate Added to Plant on 810319 to Increase Ph ML19346A0081981-06-0101 June 1981 NPDES Noncompliance Notification:On 810507,svc Bldg Sump Discharge Found to Exceed Max Permissible Limit of 20 Mg Per Liter for Average Oil & Grease Concentration.Cleaning Solutions Believed Poured Down Svc Bldg Drains ML19347E9171981-05-11011 May 1981 NPDES Noncompliance Notification:On 810427 Const Sewage Treatment Plant Effluent Sample Collected Less than Min Permit Limitation.Possibly Caused by Potable Water Being Turned Off Over Weekend Resulting in Flow Decrease ML19347E6101981-05-11011 May 1981 NPDES Noncompliance Notification:On 810429,plant Effluent Sample Collected & Exceeded Max Permit Limitation.Possibly Caused by Sand Filter Sys Not Fully Recovered from Upset Described in 810417 Notification of Noncompliance 1998-05-26
[Table view] Category:TEXT-ENVIRONMENTAL REPORTS
MONTHYEARML20217J7831999-09-30030 September 1999 Discharge Monitoring Rept for Sequoyah Nuclear Plant for Third Quarter of 1999. with ML20209H1951999-06-30030 June 1999 Discharge Monitoring Rept for 990401-990630. with ML20205R1881999-03-31031 March 1999 NPDES Discharge Monitoring Rept,Jan-Mar 1999. with ML20205T0231998-12-31031 December 1998 Annual Radiological Environ Operating Rept for Sequoyah Nuclear Plant 1998. with ML20209J1431998-12-31031 December 1998 Radiological Impact Assessment Rept, for Jan-Dec 1998 ML20203C4051998-12-31031 December 1998 1998 Annual Reports for Sequoyah Nuclear Plant. with ML20205H8931998-12-31031 December 1998 1998 Tennessee Multi-Sector General Permit Storm Water Monitoring Rept for Sqn ML20209J1221998-12-31031 December 1998 Annual Radioactive Effluent Release Rept, for 1998 ML20199G3751998-12-31031 December 1998 Discharge Monitoring Rept for Sequoyah Nuclear Plant for Period of 981001-1231. with ML20155J3881998-09-30030 September 1998 Annual Non-Radiological Environ Operating Rept for Period Oct 1997-Sept 1998. with ML20154P5511998-09-30030 September 1998 NPDES Discharge Monitoring Rept for Period 980701-0930 ML20236Q9231998-06-30030 June 1998 Discharge Monitoring Rept for Sequoyah Nuclear Plant from 980401-980630 ML20248M1031998-05-26026 May 1998 NPDES Noncompliance Notification:On 980518,spill of Sodium Hypochlorite Occurred.Sys Was Shut Down & Monitoring Was Conducted to Verify That No Detectable Total Residual Chlorine Discharged from Outfall 101 to Tn River ML20217A6541997-12-31031 December 1997 Annual Radiological Environ Operating Rept,Sequoyah Nuclear Plant for 1997 ML20217F0891997-12-31031 December 1997 Annual Radioactive Effluent Release Rept for Period of Jan-Dec 1997 ML20217N4621997-12-31031 December 1997 1997 Annual Repts for Sequoyah Nuclear Plant ML20198N7211997-10-0101 October 1997 Annual Non-Radiological Environ Operating Rept for Period from 960915-1001 ML20138F2381996-12-31031 December 1996 Annual Radioactive Effluent Release Rept for Jan-Dec 1996 ML20138F2431996-12-31031 December 1996 Radiological Impact Assessment Rept ML20138B3591996-12-31031 December 1996 1996 Annual Radiological Environ Operating Rept for Sequoyah Nuclear Plant ML20132D3641996-09-14014 September 1996 Annual Non-Radiological Environ Operating Rept 950915- 960914 ML20108B3931995-12-31031 December 1995 Annual Radioactive Effluent Release Rept for Period of Jan- Dec 1995 ML20108A0981995-12-31031 December 1995 Annual Radiological Environ Operating Rept Sequoyah Nuclear Plant 1995 ML20108B3991995-12-31031 December 1995 Radiological Impact Assessment Sequoyah Nuclear Plant Jan- Dec 1995 ML20094G7761995-09-14014 September 1995 Annual Nonradiological Environ Operating Rept for 940915- 950914 ML20087H4951994-12-31031 December 1994 Annual Radioactive Effluent Release Rept for Jan-Dec 1994 ML20082P9881994-12-31031 December 1994 Annual Radiological Environ Operating Rept Sequoyah Nuclear Plant 1994 ML20080L6361994-12-31031 December 1994 Annual Rept for 1994, Consisting of Occupational Exposure Data,Rcs Specific Activity Analysis & Diesel Generator Reliability Data ML20080B7381994-09-14014 September 1994 Annual Non-Radiological Environ Operating Rept 930915- 940914 ML20065Q6221993-12-31031 December 1993 Radiological Impact Assessment Rept Sequoyah Nuclear Plant Jan-Dec 1993 ML20065Q6181993-12-31031 December 1993 Annual Radioactive Effluent Release Rept for Period Jan-Dec 1993 ML20064C3661993-12-31031 December 1993 Annual Repts to NRC Jan- Dec 1993, Containing Summary of Occupational Exposure Data, RCS Specific Activity Analysis & DG Reliability Data.W/ ML20029C7391993-12-31031 December 1993 Annual Radiological Environ Operating Rept Sequoyah Nuclear Plant. W/940419 Ltr ML20058L1111993-09-14014 September 1993 Annual Environ Operating Rept. W/ ML20126B2261992-12-15015 December 1992 Annual Environ Operating Rept for 910915-920914 ML20114C8051992-06-30030 June 1992 Semiannual Radioactive Effluent Release Rept for Jan-June 1992 ML20095K0121991-12-31031 December 1991 Annual Radiological Environ Operating Rept Sequoyah Nuclear Plant 1991 ML20090D2041991-12-31031 December 1991 Semiannual Effluent Release Rept for Jul-Dec 1991 ML20090D2101991-12-31031 December 1991 Radiological Impact Assessment Rept, Jan-Dec 1991 ML20082L3601991-06-30030 June 1991 Effluent & Waste Disposal Semiannual Rept Jan-June 1991 ML20073G4761990-12-31031 December 1990 Annual Radiological Environ Operating Rept,Sequoyah Nuclear Plant,1990 ML20029B2481990-12-31031 December 1990 Semiannual Radioactive Effluent Release & Radiological Impact Assessment Rept for Jul-Dec 1990. W/910225 Ltr ML20065R7241990-09-14014 September 1990 Annual Environ Operating Rept 890915-900914 ML20012A0751989-12-31031 December 1989 Radiological Impact Assessment Rept,Sequoyah Nuclear Plant, 1989. ML20012A0731989-12-31031 December 1989 Supplemental Effluent & Waste Disposal Semiannual Rept for Second Half 1989. ML19332G0881989-09-14014 September 1989 Annual Environ Operating Rept 880915-890914. W/891215 Ltr ML20246L8801989-08-31031 August 1989 Predictive Section 316(a) Demonstration for Alternative Winter Thermal Discharge Limit for Sequoyah Nuclear Plant, Chickamauga Reservoir,Tn ML20247J7611989-06-30030 June 1989 Chicamauga Reservoir 1988 Fisheries Monitoring Cove Rotenone Results ML20246H3761989-06-30030 June 1989 Effluent & Waste Disposal Semiannual Rept Supplemental Info Jan-June 1989 ML20245G8971989-04-26026 April 1989 NPDES Noncompliance Notification:On 880801,dead Fish Discovered in Intake Forebay & Sample of Intake Water Analyzed for Total Residual Chlorine.Caused by Release of Sodium Hypochlorite to Water.Levels within NPDES Limits 1999-09-30
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' TENNESSEE VALLEY AUTHORITY KNOXVILLE. TENNESSEE 37902 MAR 271985 Mr. John Marlar U.S. Environne al Protection Agency, Re on IV Water Man at Division
.345 Cou and Street, NE.
- Atlan , Georgia 30365
Dear Mr. Marlar:
^
Enclosed is a revised Notification of Noncompliance (NON) for Sequoyah Nuclear Plant (NPDES Permit No. TWOO26450, DSN 101) for January 1985. The January 31 noncompliance event, which was the date the cooling towers were e removed from service, was inadvertently omitted on the original NON. The figures submitted with the previous NON remain unchanged and are not being subaitted.
If you have questions, please call Nadonna Martin at FTS 856-6695 in ;
Knoxville, Tennessee.
I
!. Sincerely, GL tk Hartin E. Rivers, Director Environmental Quality i
Enclosure 4
cc (Enclosure):
Mr. Harold R. Denton. Director Office of Nuclear Reactor Regulation U.S. Nuclear Regulatory Commission Washington, D.C. 20555 Attention: Document Control Clerk.
Mr. D. Elmo Lunn. Director Tennessee Department of Public Health Division of Water Management
- 150 Ninth Avenue, North--TERRA Building i Nashv111e. Tennessee 37203-Mr. James P. O'Reilly, Director i Office of Inspection and Enforcement U.S., Nuclear Regulatory Cossaission l Region II - Suite 2900. '
! 101 Marietta Street NW.
Atlanta, Georgia ~30303 see page 2 f i
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/sh 8504080335 PDR- ADOCM O 8 b327327-S PDR ' f y\'
- Ari Equal Opportunity Employer
o MAR 271985
-Mr. John Marlar cc: Tennessee Division of Water Management Environmental Health Services 2501 Milne Street Chattanooga, Tennessee 37406 1
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('* NOTIFICATION OF NONCOMPLIANCE WITH EFFLUENT LIMITATIONS - NPDES PERMIT NO.
TN0026450 - SEQUOYAH NUCLEAR PLANT (SQN)
- Description of the discharge--Discharge No.101 - Diffuser discharge gate. During January the temperature rise limit (5.40F or 3.000) and rate of temperature change limit (+3.60F or +2.000) were exceeded.
Since-there were several occurrence's, these a're detailed in the next section.
I
- Cause and period of the noncompliance--Unprecedented cold temperatures during January 1985 created a large demand on the TVA power system. In January, SQN operated at full two-unit load for the first time during severe cold weather. Lack of rainfall in November through January caused I low flow conditions and reservoir storage below normal levels. Hydro plants were scheduled to peak during periods of high demand and hold back flow during the morning hours. Figure 1 shows the major plant features and the location of instream temperature monitors.
4 Five separate noncompliances with the temperature rise limit occurred on January 7, 11, 18, and 31. Problems associated with malfunctioning equipment (cooling tower lift pumps) were responsible for four of the
- noncompliances. . Computed compliance model results were not valid from January 20-31 when a diffuser gate was closed, causing bad input to the model. Backup instream temperature monitors showed no further temperature 4
rise noncompliances during January 20-31. However, there were times when the rate of temperature change limit was exceeded in the instream temperature monitor data during that period. These occurrences were due to cooling tower lift pump problems which caused large changes in the pond temperature before discharge. The plant was on full closed mode (two-tower operation) between January 20-31. The following paragraphs detail the events, starting on January 7, which led to the thermal noncompliances at SQN. Plant operating loads, cooling tower use, and air temperatures are shown in Figure 2. Figure 3 shows the temperature rise and river flow data. Figure 4 shows rate of temperature change data and discharge pond temperatures.
The first noncompliance occurred on January 7, at 0545 CST. The maximum temperature rise (delta T) was 5.6 degrees F. Temperature rises exceeded 1 the thermal limit for 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />. SQN was operating at full power. - River I
, flow, scheduled for hydro peaking operation, fell to 14,700 cubic feet per l second (cfs) at 0645 CST. River flows increased immediately after the i
limit was exceeded. One cooling tower was placed in service at 2030 CST, anticipating further high temperature rises during the next morning's low-flow period.
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.v The scheduling model used to determine the effects of river flo:' on the thermal' limits at SQN showed partial cooling tower operation was needed to ,
. meet the thermal limits. The plant has experienced problems with the cooling tower' lift pumps and plant operators were concerned about and reluctant to use partial cooling tower operation because of extremely cold weather.- Last year. partial usage lead to severe icing damage which cost 1 approximately one half million dollars to repair. For these reasons, full tower ~ operations were not commenced immediately r,esulting in the noncompliance. ,
The second noncompliance occurred on January 11 at 0030 CST. The maximum 1 temperature rise was 5.6 degrees F. Temperature rises were above the limit for 1.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />. River flow at SQN was as low as 14,300 cfs during this i period. A third noncompliance occurred at 0445 CST, reached a maximum of 5.7 degrees F and lasted 1.0 hour0 days <br />0 hours <br />0 weeks <br />0 months <br />. River flow had increased for a period
' of two hoars but then decreased .to 21,900 ofs causing the added temperature rise problems. SQN was operating one tower, open/ helper mode, anticipating low-flow induced temperature rise problems. The cooling tower placed in -
operation on January 10 at 2300 CST was started too late to prevent these l noncompliances.
The fourth noncompliance occurred on January 18 starting at 1615 CST. The I maximum temperature rise was 5.6 degrees F. Total duration above 5.4 degrees F was one hour. SQN operated at full two-unit operation with one cooling tower in service (helper mode). River flow dropped to 7,700 cfs and was not enough flow for operation of only one tower. The secord tower was placed in service at 1800 (helper mode).
I The 'fifth noncompliance occurred on January 31 starting at 1315 CST, during the transition from closed mode (beginning at 1020 CST) to helper mode (1225 CST) to open mode (1428). The maximum temperature rise was Total duration above 5.40F was 2.25 hours2.893519e-4 days <br />0.00694 hours <br />4.133598e-5 weeks <br />9.5125e-6 months <br />. The cooling towers
! 6.40F.
' were taken out of service in order to assess icing damage.
l On January 20, SQN went to full closed mode operation to prevent further t
icing which was first observed early that morning. While on closed mode, a 1 diffuser' gate was closed routing all flow through one diffuser leg. The computed compliance model had been previously changed to.use only two
, diffuser leg operation. The computed discharge flow is based on the difference between elevation in the diffuser pond and the river. The-i closed diffuser gate caused the model to receive false diffuser flowrate information and produced invalid results. This continued through January 31' at 1020 CST when the diffuser gate was opened during transition
- to open mode operation. Backup temperature monitors in the river from
' January 20-31 (figure 3), show temperature rises below the limit during the closed mode operation. Procedures at the plant will be changed to leave both diffuser gates open during all plant operations. Discharge flow measurements will also be calibrated under low flow and closed mode operation.
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During January 20-31, there were times when the river monitored data were outside the rate of temperature change limit. 'igure 4 shows this data
- along with the discharge pond temperatures. Measured values exceeding the limit coincide with large changes in discharge pond temperature. The plant had problems with the cooling tower lift pumps during most of closed mode operation. 'When a lift pump failed, the heated water it was pumping had to be discharged into the diffuser discharge pond. All exceedances of the J rate of temperature change limits were an hour or less. A list of these occurrences is shown in Table 1 which provides starting times, maximum values, and durations. Lift pump maintenance will be improved to provide better operation during cooling tower use.
I Steps taken to reduce, eliminate, and prevent recurrence of the noncomplying discharge--TVA is currently assessing cooling tower damage and procedures to be followed when cooling tower icing is expected. During periods of possible icing, full cooling (as opposed to partial) tower operation will be implemented when the scheduling model indicates that the thernal limits cannot be met in open mode. Plant procedures will be changed to keep diffuser gates oren during all plant operation. The 1 computer model for verification cf compliance with the thermal limits will 4 be calibrated for closed mode operation. Cooling tower lift pumps will be repaired, and maintained and tested on a periodic basis to be ready for future cooling tower operation.
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