ML20099H121

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Monthly Operating Repts for Oct 1984
ML20099H121
Person / Time
Site: Saint Lucie, Turkey Point, 05000000
Issue date: 10/31/1984
From: Grant N, Williams J
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF RESOURCE MANAGEMENT (ORM)
References
PNS-LI-84-413, NUDOCS 8411280030
Download: ML20099H121 (17)


Text

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' AVEll AC,E !)All Y (; Nil powt p; g, ygg

- 50 DOCKET NO.

h UNiy Turkey Point Unit 3 11-15-84 DATE CO. f rLETED gy N. W. Grant

\\

(305) 552-3675' TELEPil0NE October, 1984 MONTH DAY AVER AGE DAILY POWER LEVEL DAY AVER AGE DAILY POWER LEVEL tMWe Net)

.IMWe Neil 677 gj 676 2

681 18 677 683 3

19 676 4

690 20 675 652 5

21 674 684 6

673 22 686 7

23 674 686 g

674 24 531 674 25 Io 681 26 675 682 671 27 679 2s 671 675 33 671 29 14 671 30 672 6 74 15 675 3,

16 672 INSTRUCTIONS h[il i gafv'a'ii' g daily uriit p.>wer leselin Mwe.Nel for each day in the rep..riin; m.inth. C he arets

('3/771 8411280030 841031 PDR ADOCK 05000250

%' YY.Q R

PDR

  • ~.

a OPERATING DATA REPORT DOCKET No

_50-E50 DATE.11-15-84 COMPLETED BY N W Grant TELEPHONL (305) 552-3675 OPERATING STATUS N "' Unit #3 Operated At I. Unit Name:

Turkev Point Unit #3

2. Reporting Period:

Ortnhor,1984 Essentially Full Power.

2200

3. Licensed Thermal Power (MWI):

760

4. Nameplate Rating (Gross MWe):
5. Design Electrical Rating (Net MWe):

693

~700

6. Maximum Dependable Capacity (Gross MWe):

666

7. Maximum Dependable Capacity (Net MWe):
8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report,Give Reasone
9. Power Lnel To Which Restricted.If Any (Net MWe):
10. Reasons For Restrictions.lf Any:

This Month Yr to-Date Cumulative 745 7.390 104.385.6

11. Houts in Reporting Period
12. Number Of Hours Reactor Was Critical 745 6.358.3 72,664.5
13. Reactor Reerve Shutdown Hours 0

0**

844.4

14. Hours Generator On-Line 745 76,2483 72.170.8
15. Unit Reserve Shutdown Qours 0

0 121,8

16. Gross Thermal Energy Generated (MWH) 1,619,414 13.431.461 148.920.053
17. Gross Electrical Energy Generated (MWH) 525.210,_,

4,323,995 47,534,560 500,152 4,100,809 45,013,806

18. Net Electrical Energy Generated (MWH),

100.0 85,4 69.1

19. Unit Service Factor
20. Unit Availability Factor 100.0 85.4 69.3 100.8 84,1 66.5
21. Unit Capacity Factor (Using MDC Net) 96.9 80.8 62.2
22. Unit Capacity Factor (Using DER Net)
23. Unit Forced Outage Rate 0

11.2 5.9

24. Shutdowns Scheduled Oser Next 6 Months (Type.Date.and Duration of Eacht:

Refnplino. March 22. 1985. 11 weeks.

25. If Shut Down At End Of Report Period. Estimated Date of Startup:
26. Units In Test Status (Prior to Commercial Operation):

Forecas Arliined INITI AL CRITICALITY INITI AL ELECTRICITY COMMERCIAL OPER ATION n

i 50-250 TNO.

UNIT SHUTDOWNS AND POWER REDUCTIONS Tui ney ruinr. Unit #3 DATE 11-15-84 hu$)

REPORT MONTy October 1984 Sb/6

=

c Cause & Corrective jg 3

j Ei Licensee Eg g*d

^

l.

N..

Daic g

3g 4

2s&

Event g'2 E

Prevent Recurrence g:

5 jg Report sr mo H

g d

Unit #3 had no " shutdowns or power reductions".

t i

i 2

3 4

F: Forced Reason:

Method:

Exhibit G. Instructiuns S Scheduled A-Equipment Failure (Explain) 1 -Manual for Preparation of Data B. Maintenance of Test 2-Manual Scram.

Entry Sheets for I.ieensee C Refueling 3 Aufumalic Scram.

Event Repor ILER) File (NUREG-D-Regulatory Restriction

@-Other (Explain) 0161)

I:-Operator Training A Ucense Examination F Administrative 5

G-Operational Frror IF splain) 4-. /.e de A4tuc.v.**#

Ethibit I - Same Source tis /77)

II.Other ( Explain)

SUMMARY

OF OPERATING EXPERIENCE DOCKET NO.,

50-250 UNIT Turkey Point Unit #3 November 15, 1984 DATE COMPLETED BY N.W. Grant

~

TELEPHONE REPORT MONTH October,1984 Unit 3 operated at essentially full power.

Inspection and requirements of IE Bulletins and NUREG-0737 are continuing.

4 Florida Power & L ght Company commitments for NUREG-0737 implementation are continuing. Refer to correspondence between FPL and NRC for additional informatici..

I i

L

r --

AVLI; AGE I;4lt y t;xij pgwg,; L, vll DOCKET NO. 50-251 UNil Turkey Point Unit 4 DATE H-15-84 COMPLETED gy N. W. Grant TELENIONE (305) 552-3675 October.1984 MONTH DAY AVER AGE DAILY POWER LEVEL DAY AVER AGE DAILY POWER LEVEL IMWe. Net)

IMWe Neil

~-

I 37 2

88 327 3

19 4

20 5

21

~~

22 7

23 g

23 9

25 10 26

~~

11

~~

27 12 26

~~

13

-~

29 14 30

-~

IS

~~

31 16 1

INSTRUCTIONS On this forenai. list the ate:43e daily unit power leulin MWe.Nei for each day in the reporting m inth. Compute to the neJtest uhulf ITpwall.

I'l/771 O

OPERATING DAT A REPORT DOCKET NO _50-251 11-15-64 DATE.fl. H. Grant COMPLETED BY TELEPHONL (305) 552-3675 OPERATING STATUS Turkey Point Unit #4 Notes I.Ud h October 1984 See the Unit shutdowns

2. Reporting Period:

2200 and Power reductions report

3. Licensed Thennel Power (MWI):

760

4. Wylate Rating (Gross MWe):

693

5. Design Electrial Rating (Net MWe):

700

6. Maximum Dependable Capacity (Gross MWe):

666

7. Maximum Dependable Capacity (Net MWe):
8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report.Give Reasone
9. Power I.svel To Which Restricted,1f Any (Net MWe):
10. Reasons For Restrictions.lf Any:

This Month Yr to Date roomlatise 745 7.370 98,117 II. Homes In Reporting Period

12. Number Of Hours Reactor Was Critical 45.2 3,851.9 68,490.5 0

0

'165.6

13. Reactor Reserve Shutdown Hours
14. Hours Generator On Line 1R 1 1.649 1 66.116.2 0

0 31.2

15. Unit Reserve Shutdown l(ours 27,614 7,941,773 139.688.514
16. Gross Thermal Energy Generated (MWH)
17. Gross Electrial Energy Generated (MWH) 8.455 2,470,940 44,392,242 254 2.370.7p7

_42,024.846

18. Net Electrical Energy Generated (MWH),

2.0 49.8 67.4

19. Unit Service Factor
20. Unit Availability Factor

?.0 49.8 67.4

21. Unit Capsciry Factor (Using MDC Net)

.1 47.6 6_6.I 0

45.7 61.8

22. Unit Capacity Factor (Using DER Net) 95.5 24.4 5.8
23. Unit Forced Outage Rate
24. Shutdowns Scheduled Oser Next 6 Months (Type.Dete.and Duration of Each);

flovember 5. 1984 __(a.ctua l )

25. If Sliut Down At End Of Report Period. Estimated Date of Startup:
26. Units in Test Status (Prior io Commercial Operstion):

Forecast Ailiined INITIAL CRITICALITY INITI AL ELECTRICITY COMMERCI AL OPER ATION N%

50-251 DOCEET NO.

UNIT SHUTDOWNS AND POWER REDUCTIONS UNIT N AME Turkey Point Unit f4-DATE 11-16-84 ND gy N. W. G ra n t October. 1984 REPORT MONTH TELEPHONE (309) 69 1674

~h 2

g "i

j h*i Licensee

,E g Cause & Corrective

~

N...

Date r;.-

3g 4

.g i s Event l'?

Ed g-4 j ;5; -

Rep >rt s ev Prevent Recurrence s

g 6

21 840928 S

194.3 B

1

-CB VALVEX Unit #4 remove.d from power operation to repair leakage to the pressurizer relief tank.

22 841009 5

195.6 B

1 251-84-022 EB GENERA During heatup, reactor tripped due to blown fuse in normal static in-verter.

23 841017 S

19.8 A

1 HB VALVEX MSIV required modifications to allow valve to meet closure times and operability requirements.

24 841018 F

319.1 A

1 CG PUMPXX RCP seal replaced l

l 2

3 4

F-Forced Reason:

Method:

Exhibit G -Instructiores S Scheduled A-Equipment Failure (Explain) 1-Manual for Preparation of Data B-Maintenance or Test 2-Manual Scram.

Entry Sheets for Licensee C. Refueling 3-Automat e Scram.

Event Repor:1LER) File (NUREG.

D-Regulatory Rest:ictiim

$0ther (Esplain) 016l)

I. operator Training A 1xense Euamination 9,

F-Adnunistrative 5

G-Operatumal Feror iF splam t 4_ /.

4.

A sinwc.w.,#

Eshibit I Same Source es/77)

Ilother (Espfam t

SUMMARY

f'P CPERATING E.EERIENCE DOCKET NO.

50-251 UNIT Turkey Point' Unit #4

, s DATE November 15, 1984 ant COMPLETED BY TELEPHONE (305) 552-3675 REPORT HONTH October.1984 See the " Unit Shutdowns and Power Reductions" Report.

Inspections and requiremen'ts of IE Bulletin and NUREG-0737 are continuing.

Florida Power & Li'ght Company comitments to NUREG-0737 implementation are continuing. Refer to correspondent.e between FPL and NRC for additional information.

AVLR AGE DAlt ) usij pc,wg,, (, y, t DOCKETNO. 50-335 St. Lucie Unit 1 UN11 11-15-8'4 DATE N. W. Grant COMPLETED sy TELEPHONE (305) 552-3675 October, 1984 Af0 NTH DAY AVER AGE DAILY POWER LEVEL DAY AVER ACE DAILY POWER LEVEL (MWe Net) lMWe Nei) 763 I

1:,

853 2

850 is 851 851 3

'9 852 851 d

20 852 851 5

23 854 852 6

22 7

851 850 23 S

R 6'?

24 850 9

852 850 25 850 851 to 26 II 852 2

852 12 852 852 23 13 A41 29 850 14 835 850 30 is 851 849 31 36 852 INSTRUCTIONS On this formai. lat the aseiase daily unit pinwer lesel in MWe Sei for each day in the reporting m.inth. Compute to the fleafell %hadt ITyJwall.

N/77)

OPERATING DAT A REPORT 50-335 DOCKET NO.

11-15-84 DATE.N.W. Grant COMPLETED BY TELEPHONL (305) 552-3675 OPERATING STATUS St. Lucie Unit #1 Notes I. Unit Name:

October, 1984 (Jnit #1 operated at essentially

2. Reporting reriod.

ful1 power.

3. 8.leensed Thermal Power (MWI):
4. Nameplete Reting (Gross MWe):

830

5. Design Electrial Reting(Net MWe):

867

6. Maximum Dependable Cepecity (Gross MWe):

g

7. Maximum Dependable Cepecity (Net MWe):
8. If Changes Occur in Cepecity Retings (Items Number 3 Through 7) Since Last Report,Give Reasone
9. Power Level To which Restricted,lf Any (Net MWe):
10. Reasons For Restrictions.lf Any:

This Month Yr to.Dete Cumulatise 745 7320 6RG28

11. Hours in Reporting Period

/45 4122.S 48588.6

12. Number Of Hours Resetor Was Critical 205.3-U
13. Resetor deserve Shutdown Hours 745 3747.3 47323.5
14. Hours Generator On.Line 0

0 39.3

15. Unit Reserve Shutdown gours 1990103 9704949 IT5T/2887.
16. Gross Thermal Energy Generated (MWH) 00m mmu

%Umb

17. Gross Electrical Energy Genereted (MWH)

~~

631689 3035196 36369469 i

18. Net Electrical Energy Generated (MWH).

100.0 51.2 68.7

19. Unit Service Factor 100.0 51.2 68.7
20. Unit Availability Factor 10J.2 60.4 66.6
21. Unit Cepecity Factor (Using MDC Net) 102.2 50,0 65.0
22. Unit Capacity Factor (Using DER Net) 0 7.3 4.8
23. Unit Forced Outage Rate
24. Shutdowns Scheduled Oser Next 6 Months (Type.Dete.end Duration of Eschi:
25. If Shut Down At End Of Report Period. Estimated Date of Startup:
26. Units in Test Status (Prios to Commercial Operation):

Forecast Athii sed o

INITIAL CRITICALITY INITI AL ELECTRICITY COMMERCIAL OPER ATION

_y..

50-335 DOCKET NO.

UNIT SHUTDOWNS AND POWER REDUCTIONS M* Lucie Un1t #1..

UNIT NAME

    • -2

-M DATE

"*"* urant o er,1984 COIWLETED BY REPORT MONTH TELEPHONE tJUbl bbd-Jb/b l

E E

.5 ?

3 y _E_ 5 Licensee

,E,

  • E",

Cause & Corrective Nii.

Date h

3g

(

,g g y Event g7 f*3 Actitm to

$5 5

jig Rep >r a mu Prevent Recurrence F

g 6

Unit #1 has no " shutdowns or power reductions".

I 2

3 4

F: Forced Reason:

Method:

Exhibit G - Instructions S. Scheduled A Equipment Failure (Explain) 1-Manual fnr Preparation of Data B-Maintenance or Test 2-Manual Scram.

Entry Sheets for Licensee C-Refueling 3-Automatic Scram.

Event Report ILER) File (NUREG-D Regulatory Restrietion 9 Other(Explain) 016I)

E-Operator Training & Ucense Examination F Administrative 5

G-Operatismal Feror (Fxplain) 4-4e de AEDwc.v *,#

Exhibit I Same Source (9/77)

II Other iExplaini 4

SUMMARY

OF OPERATING EXPERIENCE DOCKET _NO.

50-335 UNIT St. Lucie Unit 1 DATE November 15, 1984 COMPLETED BY N.W. Grant

~

TELEPHONE I

\\

~

REPORT MONTH October, 1984 Unit #1 operated at essentially full' power.

Inspections and requiremer)ts of IE Bulletins and NUREG-0737 are continuing.

Florida Power & Light Company commitments for NUREG-0737 implementation l!efer to correspondnece between FPL and NRC for are continuing.

t additional infomation.

In accordance with requirements of NUREG-0737 Item II.K.3.3, there were no challenges to PORV or safety valves during the report month.

q'

AVLl' AC.L DAll Y llNil POwl R LI VI.t DOCKET NO.

50-335 gygir St. Lucie Unit 12 DATE COMPLETED BY N. W. Grant TELEPilONE (106I RR2-3675 October,1984 MONDI DAY AVER AGE DAILY POWER LEVEL DAY AVER AGE DAILY POWER LPVEL (MWe Net)

~

.(MWe. Net; 802 I

1, 2

803 gg 3

805 39 4

And 20 5

804 2:

804 6

22 7

801 23 g

802 24 9

801 25 10 802 26 11 An1 2,

12 716 28 13 29

~~

14 30 IS 33 16 l

INS 1 RUCTIONS On this format hst the aseenge daily unit power lesel in MWe Nei for each day in the reporting m.mth. Compute io the nearest wheile megawatt.

(9.f77 i l

~

l l

l I

OPERATING DATA REPORT l

502389 DOCKET NO-

=

l DATE. 11-15-84 COMPLETED BY N ' W ~.' G ra n t l

TELEPHONL (30sMs?-3675 OPERATING STATUS St. Lucie Unit #2 Notes I. Unit Name:

uctober, 1984 Unit #2 was removed from

2. Reporting Period:

service for scheduled refueling 2560

3. I leensed Thermal Power (MWI):

and naintenance.

i 850

4. Nameplate Rating (Gross MWe):

804

5. Design Electrical Rating (Net MWe):
6. Maximum Dependable Capscity (Gross MWe):

786

7. Maximum Dependable Capacity (Net MWe):
8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7)Since last Report.Give Reasone l
9. Power Level To Which Restricted.lf Any (Net MWe):
10. Reasons For Restrictions.lf Any:

This Month Yr to.Date Cumulative 745 7320 10825 II. Hours in Reporting Period 28/.2 6668.1 9895.1

12. Number Of Hours Reactor Was Critical

'U U

13. Reactor Reserve Shutdown Hours

./

c m.4

%%.6

14. Hours Generator On.Line
15. Unit Reserve Shutdown Qours 0

0 0

731545 16355515

.24013459

16. Gross Thermal Energy Generated (MWH)

U "D

  • OW#U
17. Gross Electrical Energv Generated (MWH) 22/u91 51569b0 7554535
18. Net Electrical Energy Generated (MWH),

38.5 88.3 88.7

19. Unit Service Factor 38.5 88.3 88.7
20. Unit Availability Factor
21. Unit Capacity Factor (Using MDC Ne ).

38.8 89.6 88.8 37.9 87.6 86.8

22. Unit Capacity Factor (Using DER Net) 0 4.0 6.3
23. Unit Forced Outage Rate
24. Shutdowns Scheduled Oser Next 6 Months (Type.Date.and Duration of Each):
25. If Shut Down At End Of Report Period. Estimated Date of Startup:
26. Units In Test Status (Prior to Commercial Operation):

Forecast Arliirsed INITIAL CRITICALITY INITI AL ELECTRICITY COMMERCIAL OPER ATION

50-389 NO UNIT SHUTDOWNS AND POWER REDUCTIONS x. Lucle Unit #2=..

DATE. 11-15-84 October' 1984 C000PLETED BY N.W. Grant REPORT MONTH TELEPHONE (305) 552-3675 c

.] g 3

y E3-Licensee E,

    • L Cause & Corrective

^ ' " ' "

No.

Date g

3g s

,;; y 5 Event g?

Ed Prevent Recurrence H

f:

E jgg Report a mV g

6 11 831012 S

457.3 C

1 RC FUELXX Unit #2 was shutdown for refueling and scheduled maintenance.

l 2

3 4

F: Forced Reason:

Method:

Exhibit G Instructions S Scheduled A. Equipment Failure (Explain) 1 Manual for Preparation of Data B-Maintenance or Test 2-Manual Scram.

Entry Sheets for Licensee C Refueling 3 Automatic Scram.

Event Report ILER) File (NUREG-D Regulatory Restriction

@-Other (Explain)

-01611 E-Operator Training & Ucense Examination F Administrative G Operational Fernr lF xplain) 4-. /.e ae Asewc.w.cJ Ethihit I Same Source 19/77)

Il-Other (Explain)

SU21 MARY OF OPERATING EXPERIENCE DOCKET NO.

50-389 UNIT St. Lucie Unit #2 DATE November 15, 1984 N.W. Grant COMPLETED BY

~

TELEPHONE REPORT I40 NTH November,1984 Unit #2 was shutdown for refueling and scheduled maintenance.

Inspections and requirements of IE Bulletins and NUREG-0737 are continuing.

Florida Power & Ljght Company commitments for NUREG-0737 implementation are continuing. Refer to correspondence between FPL and NRC for additional information.

In acco-dance with requirements of Technical specification 6.9.1.6 there were no challenges to PORV or safety valves during the report month.

l

1-FLORIDA POWER & LIGHT COMPANY November 15, 1984 PNS-LI-84-413 Director, Office of Resource Management U. S. Nuclear Regulatory Commission' Washington, D.C.

20555

Dear Sir:

Attached are the October 1984 Operating Status Reports and Operating Summary Reports for Turkey Point Units No. 3 and 4 and St. Lucie Units No. I and 2.

Very truly yours, J. W. Williams, Jr.

Group Vice President Nuclear Energy JWW/NWG/cas Attachment cc:

J. P. O'Reilly, Region II d

9 6

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