|
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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML20217D1261999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Monticello Nuclear Generating Plant.With ML20216E7031999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Monticello Nuclear Generating Plant.With ML20210Q6611999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Monticello Nuclear Generating Plant.With ML20209F7901999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Monticello Nuclear Generating Plant.With ML20195H0351999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Monticello Nuclear Generatintg Plant.With ML20206N1721999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Monticello Nuclear Generating Plant.With ML20205P5701999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Monticello Nuclear Generating Plant.With ML20205G7391999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Monticello Nuclear Generating Plant.With ML20199F6211998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Mngp.With ML20198B2531998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Monticello Nuclear Generating Plant.With ML20195D2381998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Monticello Nuclear Generating Plant.With ML20154L3471998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Monticello Nuclear Generating Plant.With ML20153B0861998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Monticello Nuclear Generating Plant.With ML20237B8461998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Monticello Nuclear Generating Plant ML20236R1941998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Monticello Nuclear Generating Plant ML20249A5861998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Monticello Nuclear Generating Plant ML20247K3971998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Monticello Nuclear Generating Plant ML20217F6431998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Monticello Nuclear Generating Plant ML20216H6481998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Monticello Nuclear Generating Plant ML20203B2821998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Monticello Nuclear Generating Station ML20198P2201997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Monticello Nuclear Generating Plant ML20203J7131997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Monticello Nuclear Generating Plant ML20199H8181997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Monticello Nuclear Generating Plant ML20217K2081997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Monticello Nuclear Generating Plant ML20216H7771997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Monticello Nuclear Generating Plant ML20217K2741997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Monticello Nuclear Generating Plant ML20149E2921997-06-30030 June 1997 Monthly Operating Rept for June 1997 for MNGP ML20141C2841997-04-30030 April 1997 Monthly Operating Rept for Apr 1997 for Monticello Nuclear Generating Plant ML20137W2621997-03-31031 March 1997 Monthly Operating Rept for Mar 1997 for Monticello Nuclear Generating Plant ML20136H1671997-02-28028 February 1997 Monthly Operating Rept for Feb 1997 for Monticello Nuclear Generating Plant ML20134M7071997-01-31031 January 1997 Monthly Operating Rept for Jan 1997 for Monticello Nuclear Generating Plant ML20133J1401996-12-31031 December 1996 Monthly Operating Rept for Dec 1996 for Monticello Nuclear Generating Plant ML20132A8771996-11-30030 November 1996 Monthly Operating Rept for Nov 1996 for Monticello Nuclear Generating Plant ML20134L2761996-10-31031 October 1996 Monthly Operating Rept for Oct 1996 for Monticello Nuclear Generating Plant ML20128Q7831996-09-30030 September 1996 Monthly Operating Rept for Sept 1996 for Monticello Nuclear Generating Plant ML20117M8161996-08-31031 August 1996 Monthly Operating Rept for Aug 1996 for Monticello Nuclear Generating Plant ML20116M2991996-07-31031 July 1996 Monthly Operating Rept for July 1996 for Monticello Nuclear Generating Plant ML20115H5651996-06-30030 June 1996 Monthly Operating Rept for June 1996 for Monticello Nuclear Generating Plant ML20112J1921996-05-31031 May 1996 Monthly Operating Rept for May 1996 for Monticello Nuclear Generating Plant ML20112A3121996-04-30030 April 1996 Monthly Operating Rept for Apr 1996 for Monticello Nuclear Generating Plant ML20107E9831996-03-31031 March 1996 Monthly Operating Rept for Mar 1996 for Monticello Nuclear Generating Plant ML20106H0591996-02-29029 February 1996 Monthly Operating Rept for Feb 1996 for Monticello Nuclear Generating Plant ML20100G5031996-01-31031 January 1996 Monthly Operating Rept for Jan 1996 for Monticello Nuclear Generating Plant ML20096C8061995-12-31031 December 1995 Monthly Operating Rept for Dec 1995 for Monticello Nuclear Plant ML20095G0231995-11-30030 November 1995 Monthly Operating Rept for Nov 1997 for Monticello Nuclear Generating Plant ML20094L1921995-10-31031 October 1995 Monthly Operating Rept for Oct 1995 for Monticello Nuclear Generating Plant ML20093E6241995-09-30030 September 1995 Monthly Operating Rept for Sept 1995 for Monticello Nuclear Generating Plant ML20092F4121995-08-31031 August 1995 Monthly Operating Rept for Aug 1995 for Monticello Nuclear Generating Plant ML20087H3011995-07-31031 July 1995 Monthly Operating Rept for Jul 1995 for Monticello Nuclear Generating Plant ML20086K1731995-06-30030 June 1995 Monthly Operating Rept for June 1995 for Monticello Nuclear Generating Station 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217H2061999-10-12012 October 1999 Safety Evaluation Supporting Amend 106 to License DPR-22 ML20217D1261999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Monticello Nuclear Generating Plant.With ML20216E7031999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Monticello Nuclear Generating Plant.With ML20210Q0521999-08-0404 August 1999 Safety Evaluation Approving Relief Request 10 to License DPR-22 Per 10CFR50.55a(g)(6)(i).Inservice Exam for Relief Request 10,Parts A,B,C,D & E Impractical & Reasonable Assurance of Structural Integrity Provided ML20210Q6611999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Monticello Nuclear Generating Plant.With 05000263/LER-1999-007, :on 990610,HPCI Test Return Valve Was Unable to Close Against Max Expected Differential Pressure.Caused by Failure to Accurately Predict Valve Performance.Procedure Revised.With1999-07-0909 July 1999
- on 990610,HPCI Test Return Valve Was Unable to Close Against Max Expected Differential Pressure.Caused by Failure to Accurately Predict Valve Performance.Procedure Revised.With
05000263/LER-1999-006-01, :on 990602,during Quarterly Surveillance Hcpi Was Declared Inoperable.Caused by Drain Pot Alarm.Revised HPCI Surveillance Test Procedure.With1999-07-0202 July 1999
- on 990602,during Quarterly Surveillance Hcpi Was Declared Inoperable.Caused by Drain Pot Alarm.Revised HPCI Surveillance Test Procedure.With
ML20209F7901999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Monticello Nuclear Generating Plant.With 05000263/LER-1999-005, :on 990508,personnel Inserted Manual Scram When Pressure Transient Closed Air Ejector Suction Isolation Valves & Tripped off-gas Sys.Caused by Recombiner Catalyst Migration.Catalyst Was Removed.With1999-06-0707 June 1999
- on 990508,personnel Inserted Manual Scram When Pressure Transient Closed Air Ejector Suction Isolation Valves & Tripped off-gas Sys.Caused by Recombiner Catalyst Migration.Catalyst Was Removed.With
ML20195H0351999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Monticello Nuclear Generatintg Plant.With 05000263/LER-1999-004-01, :on 990422,low Reactor Water Level Scram,Group 2 & 3 Isolations & Subsequent HPCI Became Inoperable.Caused by Feedwater Controller Power Supply Failure.Three Power Supplies Replaced & Connections Cleaned.With1999-05-24024 May 1999
- on 990422,low Reactor Water Level Scram,Group 2 & 3 Isolations & Subsequent HPCI Became Inoperable.Caused by Feedwater Controller Power Supply Failure.Three Power Supplies Replaced & Connections Cleaned.With
05000263/LER-1999-003-01, :on 990412,HPCI & Division 1 ECCS Equipment Were Declared Inoperable Due to Svc Water Pump Failure.Pump Shaft Was Mechanically Freed,Check Valve Was Repaired & Pump Was Successfully Tested.With1999-05-12012 May 1999
- on 990412,HPCI & Division 1 ECCS Equipment Were Declared Inoperable Due to Svc Water Pump Failure.Pump Shaft Was Mechanically Freed,Check Valve Was Repaired & Pump Was Successfully Tested.With
05000263/LER-1999-002-01, :on 990329,event Sequence That Results in Available ECCS Being Reduced to Less than That Assumed in Current Safety Analysis.Caused by Failure of Edg.Plant Operating Procedures Revised.With1999-05-11011 May 1999
- on 990329,event Sequence That Results in Available ECCS Being Reduced to Less than That Assumed in Current Safety Analysis.Caused by Failure of Edg.Plant Operating Procedures Revised.With
ML20206N1721999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Monticello Nuclear Generating Plant.With ML20205N0861999-04-12012 April 1999 Safety Evaluation Re Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20205P5701999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Monticello Nuclear Generating Plant.With ML20205C1651999-03-19019 March 1999 Safety Evaluation Supporting Amend 105 to License DPR-22 ML20204H4951999-03-18018 March 1999 SER Concluding That Licensee Established Acceptable Program to Verify Periodically design-basis Capability of safety-related MOVs at Monticello.Therefore Staff Concludes Licensee Adequately Addressed Action Required in GL 96-05 05000263/LER-1999-001-02, :on 990215,HPCI High Steam Flow Isolation During Quarterly Surveillance Test Was Noted.Caused by Inadequate Surveillance Procedure.Revised Surveillance Procedure.With1999-03-17017 March 1999
- on 990215,HPCI High Steam Flow Isolation During Quarterly Surveillance Test Was Noted.Caused by Inadequate Surveillance Procedure.Revised Surveillance Procedure.With
ML20205G7391999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Monticello Nuclear Generating Plant.With ML20202F7901999-01-25025 January 1999 1999 Four Year Simulator Certification Rept for MNGP Simulation Facility ML20199E4871999-01-0606 January 1999 SER Accepting Licensee 951116,960214 & 0524 Responses to NRC Bulletin 95-002, Unexpected Clogging of Residual Heat Removal Pump Strainer While Operating in Suppression Pool Cooling Mode ML20205H0561998-12-31031 December 1998 Northern States Power Co 1998 Annual Rept. with ML20199F6211998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Mngp.With ML20198P0691998-12-28028 December 1998 Safety Evaluation Concluding That NSP Proposed Alternative to Paragraph III-3411 of App III to 1986 Edition of Section XI of ASME Code Provides Acceptable Level of Quality & Safety.Alternative Authorized ML20198M8221998-12-24024 December 1998 Safety Evaluation Supporting Amend 104 to License DPR-22 ML20198M6901998-12-23023 December 1998 Safety Evaluation Supporting Amend 103 to License DPR-22 ML20198D0751998-12-10010 December 1998 Safety Evaluation Supporting NSP Proposed Change to EOPs to Use 2/3 Core Height as Potential Entry Condition Into Containment Flooding ML20198B2531998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Monticello Nuclear Generating Plant.With ML20195E3691998-11-12012 November 1998 Safety Evaluation Concluding That Licensee USI A-46 Implementation Has Met Purpose & Intent of Criteria in GIP-2 & Staff Sser 2 for Resolution of USI A-46 ML20195D2381998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Monticello Nuclear Generating Plant.With ML20198J4451998-10-22022 October 1998 Rev 2 to SIR-97-003, Review of Test Results of Two Surveillance Capsules & Recommendations for Matls Properties & Pressure-Temp Curves to Be Used for Monticello Rpv 05000263/LER-1998-005-01, :on 980921,HPCI Was Removed from Service to Repair Steam Leak in Drain Trap by Pass.Caused by Localized Erosion of Valve Body.Valve Was Declared Inoperable & Was Replaced with Manual Valve1998-10-21021 October 1998
- on 980921,HPCI Was Removed from Service to Repair Steam Leak in Drain Trap by Pass.Caused by Localized Erosion of Valve Body.Valve Was Declared Inoperable & Was Replaced with Manual Valve
05000263/LER-1998-004-02, :on 980909,manual Scram Was Inserted Following Pressure Transient Closed Air Ejector Suction Isolation Valves & Trips Offgas Recombiners,Occurred.Caused by Seat Leakage.Leaking Valve Seat Was Reworked1998-10-0909 October 1998
- on 980909,manual Scram Was Inserted Following Pressure Transient Closed Air Ejector Suction Isolation Valves & Trips Offgas Recombiners,Occurred.Caused by Seat Leakage.Leaking Valve Seat Was Reworked
ML20154L3471998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Monticello Nuclear Generating Plant.With ML20153F0511998-09-21021 September 1998 Rev 2 to MNGP Colr,Cycle 19 ML20153E9361998-09-0808 September 1998 Rev 1 to MNGP Colr,Cycle 19 ML20153B0861998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Monticello Nuclear Generating Plant.With ML20151T0981998-08-28028 August 1998 Safety Evaluation Supporting Amend 101 to License DPR-22 ML20237B8461998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Monticello Nuclear Generating Plant ML20236W5041998-07-21021 July 1998 ISI Exam Summary Rept - Refueling Outage 19 ML20236R1941998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Monticello Nuclear Generating Plant ML20249A5861998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Monticello Nuclear Generating Plant 05000263/LER-1998-003-01, :on 980417,transgranular Stress Corrosion Cracking Was Identified in Control Rod Drive Lines.Caused by chloride-induced Transgranular stress-corrosion Cracking. Affected Sections of Two Lines Replaced1998-05-14014 May 1998
- on 980417,transgranular Stress Corrosion Cracking Was Identified in Control Rod Drive Lines.Caused by chloride-induced Transgranular stress-corrosion Cracking. Affected Sections of Two Lines Replaced
05000263/LER-1998-002-02, :on 980415,main Steam Isolation Valve Position Setpoint Outside Allowed Range,Was Found.Caused by Previous Testing Technique & Use of Particular Switch Model.Eight New Position Switches W/Less Deadband Installed1998-05-14014 May 1998
- on 980415,main Steam Isolation Valve Position Setpoint Outside Allowed Range,Was Found.Caused by Previous Testing Technique & Use of Particular Switch Model.Eight New Position Switches W/Less Deadband Installed
ML20247K3971998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Monticello Nuclear Generating Plant 05000263/LER-1998-001-02, :on 980323,discovered Containment Isolation Valve Leakage Exceeded TS Limit.Caused by Foreign Matl Found on Valve Seat.Repaired Subject Valves & Developed Process to Ensure Cleanliness of Testing Equipment1998-04-22022 April 1998
- on 980323,discovered Containment Isolation Valve Leakage Exceeded TS Limit.Caused by Foreign Matl Found on Valve Seat.Repaired Subject Valves & Developed Process to Ensure Cleanliness of Testing Equipment
ML20217E9611998-04-20020 April 1998 Safety Evaluation Supporting Amend 100 to License DPR-22 ML20217D8731998-04-13013 April 1998 Rev 0 to MNGP Colr,Cycle 19 ML20217F6431998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Monticello Nuclear Generating Plant 1999-09-30
[Table view] |
Text
r a
Northem States Power Company 414 Nicollet Mall i
Minneapoks. Minnesota 55401 1927 Telephone (612) 3365500 June 9, 1992 Monticello Technical Specifications Section 6.7.A.3 US Nuclear Regulatory Commission Attn: Document Control Desk Vashington, DC 20S55 MONTICELLO NUCLEAR GENERATING PLANT Docket No. 50 263 License No. DPR-22 Monthly Operating Report May. 1992 Attached is the Monthly Operating Report for May, 1992 for the Monticello Nuclear Generating Plant.
/ c
&ik Thomas M Par e Manager Nuclear Support Service TMP/mk1 C:
Director, Office of Resource Management Regional Administrator-III, NRC NRR Project Manager, NRC NRC Resident Inspector State of Minnesota - Kris Sanda-Attachment I
l 9206150373 920531 k
i PDR ADOCK 05000263 t !
-R PDR
'00vAu f
OPERATING DATA-REPORT U
i
,e DOCKET NO.
50-263 DATE 6-1-92 COMPLETED BY H. H. Paustian TELEPHONE 612/295-5151:
- l OPERATING STATUS
.] Notes
]
- 1. Unit-Name :
-Monticello
)
)
- 2. Reporting period:
_J4ay J'
]
- 3. Licensed Thermal Power (MWt):
_1670
)
-]=
4._ Nameplate Rating (Gross MWe):
569
)
)
- 5. Design Electrical Rating (Net MWe):
545.4
)
]'
,6. Maximum Dependable Capacity (Gross MWe): __564
)
)
- 7. Maximum Dependable Capacity (Net MWe):
536
)
)
-8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
- 9. Power Level To=WhichLRestricted, If Any (Net MWe):
N/A
- 10. Reasons For Restrictions, If Any: __N/A' T
THIS MONTH YR.-TO-DATE CUMULATIVE--
111.~ Hours In Reporting Period 744 3647-183384-i 11 2. Number Of Hours Reactor:Was Critical.
744.0' 3429.3 146847.7 4
- 13. Reactor Reserve-Shutdown Hours 0 ~. 0 0.0:
940.7
- 14. Hours' Generator'On-Line 744.0 3391.31 144139.2
- 15. Unit Reserve Shutdown Hours 0.0 0.0-0.0
- 15. Gross Thermal Energy Generated (MWH) 1228822-5610970 -
221144547
-17.-Gross Electrical Energy Generated (MWH) 409095 11883944 74773789
- 18. Net Electrical Energy _-Generated-(MWH) 393562
_1811982 71514200
- 19. Unit Service Factor 100.0%
93.0%
7;8.6%
- 20. Unit 1 Availability Factor
-100.0%-
.93.0%
78.6%
- 21. Unit Capacity Factor'(Using MDC Net) 98.7%-
92.7%'
-72.8%
i
- 22. Unit Capacity. Factor-(Using DER Net)
=97.0%
-91.'1%-
71.5%
- 23. Unit Forced-Outage Rate
-0.0%z 2.0%1 3.9%
L
- 24. Shutdowns-Scheduled Over Next.12 Months-(Type, Date,-and-Duration of Each)-
- Refueling Outage
=1/6/93-- 56 days-
- 25. If Shut Down At End Of Report Period, Estimated-Date Of Startup:N/A~
~
26.1 Units In__ Test Status (Prior to Commercial Operation):LN/A; Forecast Achieved?
INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL: OPERATION ll u
O
. ~. -.
.---~w.
AVERAGE' DAILY UNIT POWER LEVEL DOCKET NO.
50-263-UNIT Monticello,_
DATE 6-1-92 COMPI.TED BY
-H.
H. Paustian TELEPHONE 612/295-5151 MONTH OF May DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)
(MWe-Net) 1 535.
17 361.
2
- 528, 18 539.
3 535.
19 536.
4 534.
20
- 532, 5
540.
21 537.
6
- 526, 22 537.
7 535._
23
-535.
8 533.
24
-539.
9
- 533, 25 537.
10 532.
26 539.
11
- 533, 27 534'.
12 532.
28
- 540, 13 534.
29 537.
14 535.30-537.
15 530.
31
- 531,16-533.
INSTRUCTIONS.
On this format,-list the average daily unit-power-level in-MWe-Net for each
-day in-the reporting month.
Compute:to'the' nearest-whole megawatt.
.. -.. _. _ _. ~. _,
i a
4.. ' -
NARRATIVE
SUMMARY
OFLGPERATING EXPERIENCE
-DOCKET NO.
50-263
..DATE 6
1 COMPLETED'BY H.-H.=Paustian-TELEPHONE 612/295-5151 4
MONTH MAY 5-1-92 to Power operation, i
5-17-92 1
5-17-92 Power reduction to 30% to repair-Turbine Moisture-Separator
. dump valve.
5-17-92 to
-Power operation.
5-:31-92 t
s Note: Power-operation. defined.as-essentially 100% of rated power /except for weekend load drops' for-specified surveillance testing,
~
\\;
F
..uu
~.
.- - ~, =. -
UNIT SHITIDCT4G A!D F0 vier REDUCTIO 15 DOCKER 10.
50-263 UNrr IAME ~hxiticello DATS ~~06-01-92 CGiPLETED BY 1. H. Paustian REPOR'r FOtml May TELEPHONE'[612/295-5151 Ib.
Date T@e Duration Reason Method LER Sp> temComp.
Cause & Corrective 11)
(hours)
(2) of tb.
u de Code Action to Shutdown (1)
(5)
Prevent Recurrence (3) 5 05-17-92 S
0 B
4' N/A TF ICV Power reduction to 30% to repair Turbine Moisture-Separator drp valve.
1 2
3 4
F: Forced Reason:
ftthod:
Draft IEEE Standard S: Scheduled. " A-Equiment Failure (Exclain) 1-Manual -
805-1984(P805-D5)
B-Maintenance or Test 2-Manual Scram
'C-Refueling 3-Autcxnatic Scram 5'
D-lator Restriction
. '4-Other (Explain)
.IEEE Stardard 803A-1983 E-rator Training & License Examination F
niptrative G-Operational Error (Explain)
H-Other (Explain)
-s
--.-,_c.
. ~. - -.
J
-