ML20096C565

From kanterella
Jump to navigation Jump to search
Forwards Response to Item of Noncompliance Noted in Insp Repts 50-317/84-01 & 50-318/84-01.Corrective Actions:New Radiation Chemistry Procedure Will Be Implemented & Facility Change Request Initiated to Modify Key Function
ML20096C565
Person / Time
Site: Calvert Cliffs  
Issue date: 06/29/1984
From: Lundvall A
BALTIMORE GAS & ELECTRIC CO.
To: Starostecki R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
References
NUDOCS 8409050345
Download: ML20096C565 (3)


Text

$

1<,

O

$,N

%f BALTIMORE GAS AND ELECTRIC CHARLES CENTER P.O. BOX 1475 BALTIMORE, MARYLAND 21203 ARTHun E. LUNDVALL,JR.

3 me 29,1984 Vict PREslOENT SuPPLv U. S. Nuclear Regulatory Commission Docket Nos.

50-317 Region I 50-318 631 Park Avenue License Nos.

OPR-53 King of Prussia, PA 19406 DPR-69 ATTENTION: Mr. R. W. Starostecki, Director Division of Project & Resident Programs Gentlemen:

This refers to Inspection Report 50-317/84-01,50-318/84-01; which transmitted one item of apparent noncompliance with NRC requirements. Enclosure (1) to this letter is a written statement in reply to that item r.oted in your letter of June 1,1984.

Should you have further questions regarding this reply, we will be pleased to discuss them with you.

Very truly yours,

/

/

J W4 y

AEL/ LOW / tim Enclosure cc:

D. A. Brune, Esquire G. F. Trowbridge, Esquire D. H. Jaffe, NRC T. Foley, NRC 0

l hg '.

8409050345 840629 PDR ADOCK 05000317-

(JI G

PDR

4 r -

e

= -

)

I b

i ENCLOSURE (1)

REPLY TO APPENDIX A OF NRC INSPECTION REFORT 50-317/84 01: 50-318/84-01 We have reviewed'the circumstances that led to the apparent violation of Technical Specification 3.6.4.1 requiring that the Post Accident Sampling Liquid Return Valve to Reactor Coolant Drain Tank (SV-6529) and Hydrogen Sample Return Valves (SV-6507G &

SV-6540G) be administratively maintained in the required position during MODES 1-4

~ operation.

The root causes of the valve mispositioning events are (a) inadequate procedures for-instructing personnel regarding Technical Specification containment isolation requirements while performing operational maintenance checks on the Post Accident Sampling System (PASS), and (b) inappropriate methodology for controlling the use of key locked valves for the valves in question.

LAccordingly, the corrective actions cited below have been or will be implemented to ensure that similar violations will not recur in the future.

(1) - A new Radiation Chemistry Procedure will be implemented to address use of the PASS while performing maintenance checks during power operational modes. This procedure will specifically address (a) initial conditions which allow PASS use, (b) proper administrative controls of all pertinent valves, and (c) initial and final valve line-up conditions'.

This procedure will require a Chemistry Technician verification and sign-off for as-left valve conditions. This action will be completed by.

August 31,1984.

i (2)' The administration of keys used to operate SV-6529,6507G,6540G, and other similar containment isolation valves has been removed from the control of chemistry and maintenance groups and is currently controlled exclusively by Operations. This action was completed on January 30,1984.

(3)

A Facility Change Request has been initiated to modify the key function for SV-6529, 6507G, 6540G, and other similar containment isolation. valves. - The modification will incorporate a captive key feature such that the key can only be removed when the valve is in the closed position.

This will result in more positive control of valve opening evolutions because Operations personnel will have control of

- the number and type of valve evolutions to be performed by Chemistry and' Maintenance personnel. This action will be completed for Unit 1

~ during the spring 1985 and Unit 2 during the fall 1985 refueling outages.

(4)

The ' administrative. requirements for operation-of SV-6529, 6507G, 6540G, and other similar containment isolation valves were reviewed with plant Chemistry, Operations, and Electrical & Controls personnel. This action was completed on April 4,1984.

ti 4

1 v

.w-

,w

- - - - + - - -,.,., -. - -,. -

-..%=-

-- r w

,,m---*r-<,---.ww-+.--=e,-w--v----


e..,e---

ve,-+,wr,,,--

O rd L/

~*

i ENCLOSURE (1)

REPI,Y TO APPENDIX A OF NRC INSPECTION REPORT 50-317/84-01; 50-318/84-01 (3)

Effective as of April 19, 1984, a license amendment was issued modifying Technical Specification Table 3.6-1 to allow intermittent operation (under Administrative Controls) of SV-6507G, 6540G, and other similar containment isolation valves.

(6)

The General Supervisor - Operations Standing Instructions were modified on April 24, 1984, requiring the Control Room Operator to enter the status of these valves in the Control Room I,og whenever the valves are opened.

. m.

.n.

st

,e-n..

L.

  • s..a f.e.,

I f

_ _ _.. _ _,. _.. _. _. _,