ML20094L083

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Provides Summary of Actions Taken as Result of Open Item on Motor Operated Valve Power Factor & Degraded Voltage Performance Identified During Insp Rept 50-483/91-20,in Ref to Generic Ltr 89-10, Safety-Related MOV Testing..
ML20094L083
Person / Time
Site: Callaway 
Issue date: 03/16/1992
From: Schnell D
UNION ELECTRIC CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
GL-89-10, ULNRC-2592, NUDOCS 9203240295
Download: ML20094L083 (3)


Text

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St h n t'c wun fall 6 3 M !M llM March 16, 1992 Dorad F. Schnelt g

U.

S. Nuclear Regulatory Commission

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{'y,3, gyp' Document Control Desk

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Washington, DC 20555 2

ULNRC-2592 Centlemen:

Reply to Open Item, Inspection Report 50-483/91020 Summary of Actions Taken to Resolve

}LOV Deggaded Voltage Performance This letter provides a summary of actions taken as a result of an open item on motor operated valve (MOV) power factor and degraded voltage performance identified during an NRC inspection of Callaway's MOV program.

This inspection assessed Callaway's conformance to requ'roments of NRC Generic Letter 89-10, " Safety-Related Motor-Operated Valvo Testing and Surveillance", (2515/109).

A written response to the open item was requested in your February 13, 1992 transmittal of inspection report number 50-483/9102n(DRS).

In response to the open item, the following actions have been completed:

1)-

The IEEE-399 standard committee was contacted to determine the applicability of a 0.2 power factor for motors-less than_1000 horsepower.

From this discussion, it was determined that the 0.2 pcwer factor listed in IEEE-399 is not valid for fractional horsepower motors.

2)

The valve operator manufacturer (Limitorque) and motor t

manufacturer.(Reliance) were contacted to obtain specific power factor data.

A priority purchase order has been issued to procure this information; however, as of this date, the actual motor data has not been received.

l 3)

Limitorque did provide a table of bounding motor locked rotor power factors'for each motor frame size and polo configuration utilized at Callaway.

These locked rotor power factors ranged from 0.63 to 0.83.

4)

Voltage' drops were recalculated utilizing these bounding locked rotor power factors for all the affected safety-related motor operated valves.

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ULNRC-2592 Page 2 of 3

'4 5)

The results rf these calculations were then input into

.the Limitort:.a sizing equations-to determine valve operability.

6)_

For those valves with unacceptable results, specific ovaluations were performed _as applicable for each valvo using the following methods:

a)

The actual worst-caso voltage at each motor control center was utilized in lieu of the generic worst case voltage of 92% of 460 volts AC.

b)

The actual cable lengths for each valve were utilized in lieu of the computed route lengths.

c)

New calculated voltage drops determined by the adjustments in a) and b) were then input into the Limitorque sizing equation, d)

The design differential pressures (AP) were reviewed and revised to reduce any unnecessary conservatism.

c)-

Justifications were developed for use of valve train coefficient of friction of 0.15.

.Tbc coefficient of friction-of J.15 was input into the sizing equation.

f)

When test data was:available, indicating that an MOV was capable of opening against hydrostatic AP conditions at 80% voltage, running efficiency was used An the sizing. equations.

7)

After completing the acticas described-in item 6),

calculations for two. valves, EM-HV-8923 A and B, indicatedia pctential problem in meeting the stem thrust requirements.= We then applied an alternate method utilizing EPRI-NMAC NP-6660-D to evaluate valve

-operability.

This method provides justification for

. utilizing currentfat rated starting torque versus the locked rotor current. Using the EPRI-NMAC methods, these two valves-were also demonstrated to be operable.

As discussed in_the January 27,1 1992 telecon with the inspection team and other NRC' staff members, these-valves are maintained in the open position and are only required-to isolate a passive failure 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> after an accident scenario. With this as the valve's sole snfety function, there_is time-for taking action to mitigate a passive failure if these valves are not capable of stroking under AP conditions.

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ULNRC-2592 Page 3 of'3 g

The following actions are continuing to address this open item:=

1)

Once actual locked rotor-power factors are received from Limitorque, they will be reviewed against the pou9r factors utilized in the revised calculations to vurify that conservative power factors were used and that all valves remain operable.

2)

As a result of this review, six valves were identified that have a minimum design margin remaining under the currant design bases conditions.

To address this concern, larger actuators will be installed on valves EM-HV-8807A and B, EM-HV-8923A and B, and EG-HV-62. The sixth valve, EM-HV-8924 serves no safety function but is a concern under the "mispositioned valve" scenario.

Accordingly, a design change will be impiamented to permanently block the valve in the open position by electrical de-energization.

These modifications, contingent upon material-receipt, will be pursued for implementation.in our next refuel outage scheduled to start March 20, 1992.

This summarizes the actions completed to date and two ongoing actions.

.ie stand ready to discuss any questions you may have on these actions.

Very truly yours, m

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1/

Donald F.

Schnell

-DFS/CDN/tmw

.cc:

A.

B.

Davis - Regional Administrator,.USNRC Region III R.

L. Hague - Chief,_ Reactor Projects Section 3C, USNRC Region III L.

R. Wharton - USNRC Licensing Project Manager (2 copies)

~

H J.-Miller _

_ Director. Division of Reactor Safety, USNRC~ Region III USNRC_ Document _ Control Desk'(original)

Manager'- Electric Department, Missouri Public Service Commission B.

L.

Bartlett - USNRC. Senior Resident Inspector Shaw, Pittman,'Potts, & Trowbridge l

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