ML20093E479

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Monthly Operating Repts for Aug 1984
ML20093E479
Person / Time
Site: Surry  Dominion icon.png
Issue date: 08/31/1984
From: Jones V, Stewart W
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To: Beebe M
NRC OFFICE OF RESOURCE MANAGEMENT (ORM)
References
551, NUDOCS 8410120134
Download: ML20093E479 (44)


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POW 34 i F VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION _ MONTHLY OPERATING REPORT REPORT NO. 84-09 APPROVED BY: [h - STATION MANAGER I 1 8410120134 840831 t gDRADOCK05000 't.i "

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i Section Page l Operating Data Report - Unit #1 1 Operating Data Report - Unit #2 2 Unit Shutdowns and power Reductions - Unit #1 3 Unit Shutdowns and Power Reductions - Unit #2 45 Load Reductions Due to Environmental Restrictions - Unit #1 6 Load Reductions Due to Environmental Restrictions - Unit #2 7 Average Daily Unit Power Level- Unit #1 g Average Daily Unit Power Level- Unit #2 g Summary of Operating Experience 10-12 Amendments to Facility License or Technical Specifications Facility Changes Requiring NRC Approval g Facility Changes 'Ihat Did Not Require NRC Approval Tests and Experiments Requiring NRC Approval 15 Tests and Experiments That Did Not Require NRC Approval 15 Other Changes, Tests d Experiments 16 Chemistry Report 17 Description of AllInstances Where Thermal Discharge Limits Were Exceeded 18 Fuel Handling 19-20 Procedure Revisions That Changed the Operating Mode Described in the FSAR 21 Description of Periodic Tests Which Were Not Completed Within the Time Limits Specified in Technical Specifications 22

g 11 Section Page Maintenance of Safety Related Systems During Outage or Reduced Power Periods - Unit #1 - Mechanical Maintenance 24-26 Maintenance of Safety Related Systeins During Outage or Reduced Power Periods - Unit #2 - Mechanical Maintenance 28 Maintenance of Safety Related Systems During Outage or Reduced Power Periods - Unit #1 - Electrical Maintenance 30 - Maintenance of Safety Related Systems During Outage or Reduced Power Periods - Unit # 2 - Electrical Maintenance 32 Maintenance of Safety Related Systems During Outage or 34 Reduced Power Periods- Unit #1-Instrument Maintenance Maintenance of Safety Related Systems During Outage or 36 Reduced Power Periods - Unit #2 -Instrument Maintenance 37 Health Physics Summary Procedure Deviations reviewed by Station Nuclear Safety and Operating Committee after Time Limits Specified in T.S. 38 l

an e- , Pa9e 1 bf 38 OPERATICC DATA RT?0?T TCO*.': T ?'C. 50-220 MTE 06 S'? 84 C0"PLE'rP ny .Vivian Jones TELEPRnTF B01.-357-3164 C_DE_P_A_T_I__TC_ _ _____ S_TATUS

1. U:!IT '!A!Z - SURRY UNIT 1
2. REPO?"It?G FFPIOD RO184 "O B3194
                                                                                      ~"~~~l
    .                                                                         ~~
3. LICEi: SED .""-!EF'!AL PO!.TR (%'T) 2441 l~

4 !.'A'TPLATF RATICC iGPOSS 'tT) 847. 5 l ':0TES l 5 DFFIGE ELEC~RICAL RATI?G ("FT !?E) 788-

6. !'AXI':'!" DTPE :PA?LE CAPACITY (G9f'S2 l312) ?11
 -7     "AXI'"!" DEFE"DA?LE CA??CI"! (XE' int)               7*15
8. I' GACEF GCCI'F IN C/DACITY RATICnS  ??/A (ITE' S 3 TUR0!!GE 7) SING LAST FIDD="", GIV" ?IAS0? S
9. DC'TR - LEVFL TO L'?ICH CESTRIr'ED, IF AE! ';/4 (ITT *iT)
10. REAS0!!S FOR ?ESTRICTIONF, IF A?:Y N/A TEIS !'0!!""! YP-TO-DATE CTP'i1LATIIT
11. 90!!?? I! PEPORTING PERIOD 744.0 5855.0 102503.0
12. ? W' REP CF N07PS REACTOR VAS CRITICAL 744.0 4540.8 63633.7
13. REAC*0F RFSERVE SEUTDok7: HOURS 0. 0 9. 3 3774.5 14 200RS GENE?.ATO? 011-LI?:E 744.0 4477.8 62 345,0
15. UPIT PESERTT SHUTDOWN HOURS 0. 0 0. 0 3736.2
16. GROSS TPEPl!AL EXERGY GE!% RATED (!&'?) 1421403.7 9837650.6 144763954.9
17. GPOSS ELECTRICAL E::ERGY GENERATED !?T') u37625.0 3143785.0 46 463628.0
18. ATT ELECTRICAL ENERGY GFNFRATED (!&F) 408268.0 2971195.0 44048931.0-
19. U::IT SERVICE FACTOR 100.O e/* 76.6 e/o ' 6028 * /e 2'0. UNIT AVAILA?ILITY FACTOR 1C0.0 o/o 76.5 e/e 64.5e/o
21. UNIT CAPACITY FACTOR (UEI!:G "DC !!ET) 70.9 e/e 65.5 e/e 55.4 e/o
22. U!!!T CAPACITY FACTOR (USI?:S DER NET) 69.7 e/o 64.4 * /* 54.5 e/o
23. U?IT FORCED OUTAGE RATE 0.0 e/* 4.5 ele 9.0 e/o 24 SHUTD07':S SC::EDULEE CIT? CEXT 6 !'0?:THc PEFUELING 9-28 75 DAYS (TYPE,DATE,AND DURATICT 0? EAC'!)
25. IF S"*!T DOV!? AT E!!D OF REPORT PERIOD, ESTI?' ATE DATE OF STA.%"!?
26. U!!!TE I!: TEST STA."'US FORECAST ACF!IEtTD (PRIOC TO C0""ERCIAL OPERATION)

I!!ITIAL CRITICALITY I??ITIAL ELECTRICITY C0!'"ERCIAL OPEPMIO" l 1 l l l 3

a ." Page 2 of 38 I 0? ERA'IE7 DA'A REPCRT DOCVET ??O. 291 ' DATE 06 SFP 84 C0"DLETEF ny Vivian Jones TELE *?C"E 804-357-3184 OP_ER_A_T_I_!'G _ _ S_TA_T__!!S 1.- U!!IT ??A!T SURRY U?;IT 2 2.~RE?ORTING PEFiOD B01B4 TO 63184

3. LICENSED THERVAL POkTR ( AfrT) 2441 l~~~~~~~~~~~l 4.- NA'5 PLATE RATING (G?OSS !NE) 847.5 l??CTES l
5. DESIG!: ELEC*RICAL RATICG (!TT %T) 788
6. ?:AXI!::c.' DF?El?DA?LE CA=ACITY (GROSS !PE) 811
  . 7. J(AXI!T" DEFE!:DA"LF CA?ACITY (NET ?5T)            775
8. IF CHARGES OCCUP IC CADACITY- RATI?:CS  ?:/A

( TTE!!S 3 THROUG" 7) S!? CE LAST REPORT, GIE RFA50?:S

9. POLTP LEl'EL TO ;!NICH RESTRICTFD, I? A? Y F/A

(!!ET '5T)

10. REAS0!!S FOR RESTRICTIO!?S, I? A??? N/A THIS !!O?!'" YF-TD-DATE CU!ULATIt'E
11. "OU?S I?: REPORTI??C PE?l0? 744.0 5855.0 99303.0
12. ?RP'RER OF HOURS REACTOR V2S CRITICAL 729.3 5087.6 63658.5
13. REACTOR RESERVE Cr!!TX"r!'l HOURS 0. 0 0.0 328.1 14, nrygg GEritpATop on-LINF 727.0 5031.6 62607.6
15. U?;IT RESERVE SHUTDOW? 200RS 0. 0 0. 0 0. 0
 - 16. GROSS THER!'AL EnTRGY GENEFATED (!yM)                  1746844.0    11896464.1 146612337.0
17. GROSS ELECTRICAL ENERGY CENERATED (!3??) 5467e0.0 3785;785.0 47580 644.0 1*. NE." ELECTRICAL ElTEGY GENERATED (!NU) 517816.0 3586 561.0 45093 621.D
19. UNIT SERVICE FACTOR 97.7 e/o '85.9e /o 63.0 e/o
20. U?IT AVAILAPILIT! PACTOR 97.7 olo 85,9e f e 63.0 * /*
21. U?iIT CAPACITY FAC"0? (USI."C '!DC ??E') 89.8 */o 79.0 e/o 50.5 e/o
22. L7?IT CAPACITY FACTOR (UFI:10 DER NET) 88.3 */* 77.7 e/o 57.6 e/o
23. UNIT FORCEC OUTAGE RATE 2.3 */* 14.1 e/o 14.8 e/o 24 SHUTDOF7?S SCHEDULED 01TR NEXT 6 ?'0?TuS 11-9-84 to 11-19-84 iTYPE.DATE.A1D DURATIC" 0F EAC"1 10 DAYS
25. IF SHUT P0h'?! AT END OF REPORT PERIOD, ESTI!' ATE DATE OF STA?"UP
26. U?iITS I!: TEST STATUS FDPECART ACHIEVED

(??10R TO C0!"!EPCIAL CPEPATIO!!) INITIAL CRITICALITY INITIAL ELECT?lCITY CC'CTRCIAL 0DEPA*IO!:

e - a DOCKET NU. 50-280 ,, UNIT sil01tioWNs ant > ROWER RElllM'110Ng IINII~ NAME Surry 1 HA1E 0%O7-84 _ COMrl.E1EH IIy V. H. Jones REI ORT MONill thig.ust,1984 1El.FriloNE 804-357-3164__ i

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UL rsuse A Coseettive i !E 'h

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k. is Nie. Date -{ g gj g II,ent n7 av A,,go, ,,

r.e.e,. i-oa ~  ;-4 Repen , fj$3 R,c.... ns e TIIE 1E WERE NO LINIT SIIUTDOWNS OR POW i:R REDUCTIOb S GRETTER TII AI I 20% DURING Tills REPORTING PERii )D.

                                                        /

l i 8 3 4 0 1 2 Emlill,it G - Instruttisms u Mellonl: t : l'inseJ Reason: 1.Manusi fu, Peepasselon <>f pata o 5: Silicif ulcel A regulpinent ralluie (Emplain) Entry $licets fo I.lcernee Hi 7 Mannst Sesans. II Maintenance ni leil Event Itepmt (l.EIO file INilitt G. w 3 Autunutic Sesam. i C Hefuellog

  • s 4 Otlice (limplain) 0161)

D flegulatiny Restiltilon f E-Opessteis Tosining A liccuse Enaminstion l 5 i F.Ailminlitisilve F11:11:18 I - Same Soust e

G Opcestimeal l'esies (f splain) l*p/17) II Ollies (thplain) i b
                                                                                  -. . - . - ~            - - - _ _ -        ._.    -

50-281 i DCKET NO. tifffT SitUII) OWNS AND FolVER RI.Dt)C110NS t##TNAME Surry II (co_.DJ.)

                                                                                                                                                      <pATE U9-U#~84                   .
  • 004frLETEI) Ry V. H. J_on_cs MlirORf MONill Anm>=t inna 1ELEFIN##E 804-352-3184
                                                       %       3                                                 ~
                             -         3g        3      }, y,Ijoc l.li ensee              l e, gg Conse A Coeeective Asihm tu No. ,       Dste      {       g=           j.                       Event                                 .

E o[ m j gg iterint ir vi te j] f*sevent Recussence 84-20 08-07-84 F 17.0 A 3 84 013 The unit received a turbine runback

'                                                                                                                         to 300 M W's, then two minutes later, received a reactor trip. The cause of the runback was a NIS runback from N-43 when the control power fuse blew while inst. techs. were trouble shooting a failure of the flux meter. The blown
                                                 -                                                                       fuse was caused by using an un,Jrounded

)' = cord on test meter. Inst. Dept. has i discussed this problem with all tech's. to prevent reoccurence. The unit aise received three OT6T runbacks and then l a OPAT trip. These were caused by a decreasing setpoint. The reason for the l I decreasing setpoint is still under investigation. i l f N 3 4 S I I 2 Methnit: E nMiill G . insteurthms u i F: Fmced Reason: ros riepseschm ni psis g A Eigulpment rollwe(Emplein) l Manuel

!         S: Scheduleil                                                                            2 Manuel Screm.                              I:ntry Sheets for t.lcensee              6 ti II Melotensnce of Test                                                                                           Event Repnet (l.ER) File (NilitI(;-      o.

C. Refueling 3 Auloensile Scre.n.

  • j 4 Oileet (Emplain) DI(.1)

D Regulatory Restilction j E-Upessene heining A IJcense Eneminethm $

.                              F Adniinististive                                                                                                E=hihlt I - Ssme Source 1

G Openeihmst I:ssos (Eaplain) j l'l/77) II Othet (Eaplain) I

1 . . e iMKKF T NO 8I '* 1pNiisaltlitsowH5 ANilFOWFR REltilCIH)NS gg - W-07-84 elPA1E 00Mrl.E1Elp ny V.11. Jones , REFORT MONIll Anoust 19&d irI.Fril0NE ._8.04-357-3184

                                                                                                                  ~

u h l.k ensee [*,, *L Cause A Cossective

                                -          {g          "k        } Ej                                                                              Attleen tu j

l W. , liste ( t-gI n g jg jne IIvent Repuel er glf vi o g he,e I Ret.nence t 0.0 4 The unit was reduced to 78% power i 8 & 21 08-15-84 S 11 (570 MW's) to allow removal and cleaning of " A" waterbox. The unit was reduced to 67 % power I 84-22 08-18-P4 F 0.0 A 4 (485 MW's) due to the loss of four circulators at the low level intake. The l circulators tripped off on high water l s

                                                        -'                                                                 level in pit caused by gross leakage from 1-CW-P-ID.          The pump was removed from service and is being repaired.

The unit was reduced to 76% power 84-23 08-21-84 S 0.0 11 4 l (580 MW's) to allow removal and cleaning s of "A" waterbox.

*o 1

30 3 4 f I 2 F alill,Il C . Instinctluns ui Meehs=l:

F renteil Messim

l Manwel Ios reepsistiam ull)sts o 5: Selwiluleil A Figulgmwnt f sifure(limplain) Entry Slicets fue I.leensee l 2-Manust Seesm. w 3 Maintenance os lest 1Antimulle Sessm. I:vens ReporIlt.l R) l' ele INilHIG.

  • O.Itefoeling 4 Utlwe Ilimplaiol Dir.1l l} Regelstney Restilrtimi ET)peestos Tisining A license Essneinathm 5 F Ailministostive ItieMelt I Sainw Sowe(c G Opceselimst f esus (l'agelsin)

II Other IFsplaini rif7il . 1

l Pace 6 of 38 l LOAD PSUCTIONS D'*E TO ENIRONEN~A1. RES~iICTIONS UNIT NO.1 MONTH: August, 1984 LOAD, %' EDUCTIONS. E' M~Id REASON DATE TIME HOURS NCE DURING THIS REPuKdNG PERIOD. l t i

             =e t

9 4 e t i MONTIC.Y TOTid.

                                            ~,-           -- - - , av., --
                                                                             -...+n.--   -
                                                                                               --n   .- - +         , , - . - -c.~     e

Page 7 of - . 38 LOAD REDUCTIONS DUE TO EhTIR0tFhiAL RES"T.ICTIONS UNIT NO.2 MONTE: August, 1984 DATE TI1E HOURS LOAD, Mk' REDUCTIONS, ML' M7d REASON tGE DURING IHIS REPutu143 PERIOD. i 4 4 i e i MO:,IELY TOTAL

Page 8 of 38 DOCEE* NO 50-280 UTIT SURRY I DATE 9-1~84 COMPLETED By V H. Jones ATTRAGE DAILY UNIT POYEP LEVEL M0i:THt ' AUGUST 84 AVEPAGE DAILY POWER LEVEL AVERACE DAILY POWER LEVEL DAI ( PFE-PET) DAY ( MT-!.TT) T 1 432.9 17 552.8 2 500.6 18 546.0 3 565.9 19 549.0 4 564.7 20 549.8 5 553.7 21 546.5 6 560.4 22 538.0 7 549.6 23 555.8 8 544.0 24 560.4 9 556.0 25 I 9. 9 10 555.4 26 535.8 11 550.8 27 P 4.1 12 550.4 28 566.7 13 550.1 29 566.8 14 550.6 30 566.4 15 548.3 31 563.1 16 551.6

 ' DAILY UtiIT PO?!ER LEVEL TOR'? INSTRUCTIONS O!? "71IS FOR'l, LIST THE AVERAGE DAIL? UNIT POWER LEVEL I!! WE-NET FOR EACH DAY IN THE PZPORTING !.*0'!TH. T5!ESE FIGURES VILL PE USED TO PLOT A GRAPH FOR EACH PEPORT-ING M!!TH. NOTE THAT PY USING PAXIM1" DEPENDAPLE CAPACITY POR THE NET ELECTRICAL CATI? 0 0F THE UNIT, THERE ?tAY BE CCCASIO!)S VMEN T4E DAILY AVERAGE POWER EXCEEDS NE 100 */* LINE (OR THE PESTRICTED POVER LEVEL LINE). IN SUCH CASES, 57 AVERAGE
DAILY UNIT POWER CUTPUT SHEET SHOULD BE FOOTNOTED TO EXPLAIN THE APPARENT ANO"ALY.

7 Page 9 of 38 DOCEET ?!O 50-281 UNIT SURRY II DA TE 9-1-64 C0!'vLETED ?? V. H. Jones AVERACE DAILY UNIT POW"R LEVEL

 ' f'OrTHa , AUGUST     84 AVERAGE DAILY POVER LEWL                AVERAGE DAILY POYER LEWL DAY              (WE-NET)               DAY              (MWE-NET) 1                  72C.5               17                  712.4 2                  725.5               19                  671.P 3                  720.1               19                  716.0 4                  720.8               20                  717.0 5                  717.4               21                  683.4 6                  709.8               22                  725.7 7                  429.0               23                  725.5 6                  405.7               24                   724.5 S                  717.1               25                   726.8 10                  721.4               26                   723.5 11                  718.2               27                   730.6 12                  714.7               28                   731.1 13                  706.2               29                   730.0 14                  703.0               30                   715.2 15                  662.9               31                   730.1 16                  714.0 DAILE UNIT POWER LEVEL FOR!'INETRUCTIONS 0?! THIS FORti, LIST THE AVERACE CAILY UtlIT POWER LEVEL I'? WE-NET FOR EACH DAY IN 2??E CEPORTING PDUTH.^ TPESE FIGURES VILL BE USED TO PLOT A GRAPH FOR EACH REPORT-ING ?!053. NOTE TVAT BY USING !!AXIMU'! DEPENDABLE CAPACITY FOR THE NET ELECTRICAL RATING OF THE UNIT, THERE MAY BE OCCASIONS WHEN THE DAILY AVERAGE POWER EXCEEDS THE 800 */* LINE (OR T'fE RESTRICTED P0YER LEVEL LINE). IN SUCH CASES, THE AVERACE DAILY UNIT POWEP CUTPUT SHEET SHOULD BE TOOTNCTED TO EXPLAIN THE APPARENT ANOMALY.

m Pcg 10 of 38

SUMMARY

OF OPERATING EXPERIENCE MONTH / YEAR August,1984 Listed below in chronological sequence by unit is a summary of operating experiences for this month which required load reductions or resulted in significant non-1 cad related incidents. UNIT ONE 08-01-84 0000 This reporting period begins with the unit at 65% power (470 MW's) holding due to 1-FW-P-1A out of service. 02-84 0840 1-F W-P-1A returned to service, commenced increasing power at 3%/ hour. 1340 Holding power at 80% (600 MW's), unit is limited to 80% power due to rod B-6 being stuck. 08-08-84 0949 Unit power rapidly reduced to 62% (440 MW's) due to a loss of 1-FW-P-1A. 1004 1-FW-P-1A returned to service, commenced power increase at 150 MW/hr. 1130 Unit at 80% power (600 MW's). 08-09-84 1052 Two men fatally injured caused by electrocution when one man drilled into a 4160 volt cable from "C" RSS. The other man was killed during his : escue attempt. 08-22-84 0 011 Commenced power decrease for removal of "1D" waterbox from service for cleaning. 0045 Holding power at 70% (500 MW's). 0402 Commenced power increase at 3%/ hour. 0701 Unit at 80% power (600 MW's). 08-24-84 2344 Commenced power decrease for removal of "1D" waterbox from service for cleaning. 08-25-84 0150 Holding power at 76% (530 MW's). 0622 Commenced power increase at 3%/ hour. 0 918 Unit at 80% power (600 MW's). 08-31-84 2400 This reporting period ends with the unit at 80% power (600 MW's). l

                  ^

L____. _ __. . _ _ _ __ __. _ _ . . . _ _ _ _ _ . . . _ . . _ _ _ . . _ _ . _ _ _ _ _ _ _ . _ _ _ _ _ . _ _ _ . _ _ _ _ _ _ _ _ _ _

 
  • Ptg> H of 38

SUMMARY

OF OPERATING EXPERIENCE MONTH / YEAR August.1984 1 Listed below in chronological sequence by unit is a summary of operating I experiences for this month which required load reductions or resulted in significant non-load related incidents. UNIT TWO 08-01-84 0000 This reporting period begins with the unit at 100% power (770 MW's). 08-07-84 1423 Turbine runback caused by NIS rod drop signal from N-43 when control power fuse blew while instrument technicians were trouble shooting failure of flux meter. 1425 . Reactor trip caused by a two out of three OPAT signal, this was initiated because the setpoint was automatically reduced or pen alized following Turbine runback. 08-08-84 0510 Reactor critical. 0723 Generator on the line, commencing a 150 MW/ hour power increase. 1600 Reactor at 100% (760 MW's). 08-14-84 2300 Commenced power decrease for removal of *2A' waterbox from service for cleaning. 08-15-84 0132 Holding at 78% power (570 MW's). 0150 Commenced power increase at 150 MW's/ hour. 0650 Unit at 100% power (760 MW's).

      ~ 08-18-84              1226        Commenced power decrease due to loss of four circulating water pumps at the low levelintake.

1300 Holding power at 67% (485 MW's). l 1408 Commenced power increase at 150 MW's/ hour, circulators returned to service. 1720 Unit at 100% power (760 MW's). 08-20-84 2250 Commenced power decrease for removal of '2A' waterbox from service for cleaning. 2350 Holding power at 76% (580 MW's). 08-21-84 0502 Commenced power increase at 150 MW's/ hour. 0706 Unit at 100% (770 MW's). 08-30-84 0345 Commenced power decrease for removal of '2A" waterbox from service for cleaning.

Page 12 of 38 UNIT TWO (Continued) 08-30-84 0450. Holding power at 84% (640 MW's). 0645 Commenced power increase at 150 MW's/ hour. 0800 Unit at'100% power (770 MW's). 08-31-84 2400 This reporting period ends with the unit at 100% power (770 MW's). .

    *
  • Page 13 of 38 AMENDMENTS TO FACILTTY LICENSE OR TECHNICAL SPECIFICATIONS MONTH / YEAR August,1984 i

The Nuclear Regulatory Commission issued on 6-19-84 Ammendment number (s) 97 and 96 to the Operating License for Surry Power Station, Unit No,'s 1 & 2. This Ammendment is a result of the proposed Technical Specification Change Request No.(s)127 and Changes Radiological Effluent Technical Specifications. T i I r e I u_

Page 14 of 38 FACILITY CHANGES REQUIRING NRC APPROVAL Anaust, 1984 1 l NCEE DURING 'IHIS REKranCa PERIOD. FACILITY CHANGES THAT

    . DID NOT REQUIRE NRC APPROVAL Naaust, 1984 NCEE DLRING THIS REPCRTING PERICD.

B 4 4 e , -9 , _ - . _ . . . _ , , , ,,-_ ._. . . , , _ ,,m .~,-.,m ., m. ,, , ,..~n .-, , , , _ -, , - - . .

r.

    .-                                        Page 15 of 38 TESTS AND EXPERIMENTS REQUIRING NRC APPROVAL Aucust, 1984 NCNE DURING 'IHIS i<EFun'n9G PERIOD.
       . TESTS AND EXPERIMENTS THAT DID NOT REQUIRE NRC APPROVAL Aucrast, 1984 NCNE DURING 'IHIS i<EFudu4G PERICO.
          .e-                                                 ..M4 u. --                        --

s,. e ~a . ~ ae s _ 4 4 m ~ Page 16 of 38  ; f OTHER CHANGES, TES'f5 AND EXPERIMENTS i Aucrust. 1984 t NCNE IL' RING 'INIS REPOfEING PERIOD. I l -f I I l I t I 1 1 l 1 4 I J f l 5 n 4 a 4 J

                                                                                -           . .,,... __.,.,-,,,...- ~ ,.             ...c.,-,,.-,,        , - . , - , .

l l

   *
  • POR 28-06 Page 17 of 38 VIRGINIA ELECTRIC AND POWER CO.UANY SURRY POWER STATION CHEMISTRY REPORT
  • August 19 84
'                                  PRIK                     CODI. ANT                              UNIT NO. 1                                        UNIT NO. 2
                                              -ANALYSIS                                                                                                                                                     .

MAXIMUM' MINIMUM AVIPJGE MAXIMUM MINIMUM AVERAGE  !

                                                                                                                                                -1                          -2                        -2 Gross Radioact., uCi/ml                                                   1.65                       0.92        1.35       1.38E                  1.79E                       7.31
Suspended Solids, pom 0.0 0.0 0.0 0.0 0.0 0.0
                                                                                                  -2                   -2         -2            -1                          -1                           -1

- Gross Tri-lum, nCi/ml 3.95E 3.23E 3.53E 2.25E 1.15E 1.68E

                                                                                                  -2                  -2          -2            -4                          -5                           -4 Iodine 131., uCi/ml                                                      3.00E                       1.22E      2.31E      5.17E                  7.29E                        1.94E I

131 /I 133 0.41 0.14 0.26 0.23 0.04 0.12 Hvdrocen, ec/kg 38.9 21.0 29.9 49.7 27.2 35.0 Lithium, ppm (A) 0.67 0.44 0.57 1.26 0.78 0.96 l Boron-10. ppm

  • 41.6 20.6 26.6 109.4 73.7 83.8 1
                                                                                                                            ~

Oxycen, (D.O.), ppm 50.005 50.005 s0.005 50.005 so.005 50.005 Chloride, epm so.02 so.02 so.02 so.02 so.02 so.02 l pH 8 25'C 7.00 6.77 6.91 6.69 6.49 6.55 i

  • Beron-10 = Total Boron x 0.196

! NON-RADIOACTIVE CHEMICAL ' RELEASES, POUNDS I T.S. 4.13.A.6 (B) Phosphate

                                                                                     ~

Boron. 55 j Sulfate - Chromate nn 4

                                                                  $0% NaOH           -                                    Chlorine i

j REMARKS: (A) Lithite additima m=Aa to unit 42; 690 runn on 9-7; ARO ,wne on 9-9; 210 cimm ! on 8-IPs 100 as on 8-30 Cation bed elaced in service on unit #1 on 8-13, cation bed p1W in service on unit #2 on 8-13 and 8-27 for lithium reroval. (B) The levels of these chicals should create no adverse environmental imact. 4 f

    . _ - , - - . . . . - - . . . _ - _ _ - - _ _ _ . - _ .-- _              _ - -     ,._____.._..~,._,_.-.~.m..,.-                       _ _ . _ - _ _ _ . . - _ _ _ . _ _ _ _ , _ . , . . . _ _ - -
                                                                 )

Page 18 of 38 l DESCRIPTION OF ALLINSTANCES WHERE , THERMAL DISCHARGE LIMITS WERE EXCEEDED  ! Aucust, 1984 NCNE DURING 'IHIS REPORTING PERIOD. i

                                                                )

Page 19 of 3E l FUEL H AND'_ING 1 UNIT # MONTH / YEAR August,1984 DATE NO. OF ANSI NO. NEW OR SPENT FUEL SHIPPED / RECEIVED ASSEMBLIES PER S!!IPMENT INITIAL ENRICHMENT SHIPPING CASK ACTIVITY LE%TL NONE DURING THIS RE PORTING PERIOD. e e

                                                              ,. ,.-_.y. ., ,-           -
                                                                                                      ....e ,

Page 20 of 38 FUEL HANDL!NG UNIT $ U MONTH / YEAR August,1984 DATE NO. OF ANS: No. NEW OR SPENT FUEL SE!PPED/RECE!VEO ASSEMBLIES PER 5$ PMENT INITIAL ENRICHMENT SEIPPING CASF. ACTIVITY LEVEL

            -                              NONE DURING THIS REPORTING PERIOD.

l I

Page 21 of 3g

       'I PROCEDURE REVISIONS THAT CHANGED THE OPERATING MODE DESCRIBED IN THE PSAR Auaust, 1984 NCNE DURING THIS REPCRTING PERIOD.

l 1 1 1 _____ae__---_,-----.--_a- . - -_---__.__----------_a--------

        ..'                                                 Page 22 of 38 DESCRIPTION OF PERIODIC TESTS WHICH WERE NOT COMPLETED WITHIN THE TIME LIMITS SPECIFIED IN TECHNICAL SPECIFICATIONS
              -                    Auaust, 1984 M NU N                    E T*

i

r 1 Page 23 of 36

                            +-                                                 -.

e l M AINTEN ANCE OF SAFETY RELATED SYSTEMS DURING OUTAGE OR REDUCED POWER PERIODS

                                                                                                   -                                                          UNIT NO.1 MECHANICAL MAINTENANCE 4

l l

VEPCO SMETY RELATED DLRING REDU::Eb F0WER SORTED BY UNIT AND KPARTENT Ff:00RM WDT09060 09/10/84 13:06

       .        . FROM 08/01/84 TEU 06/31/84
              .'               LMIT 01 SLERY                                                                     Page 24 of 38 RETIMED TO                       WO KPT     SERVICE      HARK NUMBER     HUMIER           WO TITLE                                         HISTORY SLMtARY 08/16/84 01-CC -E     -1D     003650 CLEAN D CC HX      '

CLEAED OUT 1D EAT EXCHMOER GOT 1 BAG OF TRASH OUT R03 06/27/94 01-CH -P -2D 003658 FUPF SE/L LEES BADLY OVERHALLED OLD TYM Pt#F AND REFtAC ED Pl#F.REFLACED IPPELLER SHAFT SLE EVE SEAL DIL SEAL APG SHAFT. REPLACE D STL7 TING BOX.HAD TO SHIM LP Q.D T YPE Pt9F WITH A 1 1/2 PLATE. R03 06/30/94 01-CC - -130 004270 BASEFLATE BOLT LOOSE--EEDS TO TOROUE NUT TO 140 FT LB AS PER PERCEDURE R03 06/09/94 01-SW -P -1C 003444 FUMP IS INOPEPABLE DE TO IM- DIVERS aIAED SUCTION PIPE OPS CECKED OK R03 06/13/84 01-MS -SOV -102A 003038 VALVE LIES BY SEAT CAUSING FC REPLACED GASKETS IN VALVE.TD BODY TO 90PeET BOLTS TO 165 FT LW GASKET SET SET STOCK NLMBER 1740362 TOOLS:TOROUE WRENCH 1311 R03 06/15/84 01-MS -SOV -1029 003039 VALVE LEAKS BY SEAT CAUSING PU REPLACED BODY TO 90PeET GA9KET AND GASKETS IN VALVE TQ BODY TO 90PeET BOLTS TO 165 FT LDS INSTALLED EW G ASKETS AND TOREED VALVE BOP 4ET TO 165 FT LDS R03 06/17/84 01-CH -P -2A 002916 REPLACE FASTDERS ON INGLLATION COVER ORIGINALLY KSIGK

              -                                                                         D TO K ELD T00ETER BY FINGER TIG HT BOLTS.BOLN HAVE MEN REFLACED.

R03 06/20/84 01-EG -C -2 003749 AIR COPPRESSOR RtMS CDP (TINT)- OPDED CECK VALVE PWtf AND FOUND F LUID OPDED LP EAD MD FOLMD INCOR RECT KTEEN 9 PACER AND CYLINER OP EN W EAD FOUPS K0hN MAD GASKET REPLsGD LP/W GASKETS MD IRAIPED R03 06/20/84 01-MS -#RV -101C 003741 FtRMMITE PACKING LEAK IN,ECTED PACKING (LAND WITH FlRMMI TE NLnIAR (RADE FIBER CART LOT 101 2 Wt NO.045024 SUBMITTED TO RETURN j TO ORIGINAL R03 06/22/64 01-BS -HSS -NA 002166 DISASSD9LE AND INSKCT SNUBK INSPECTED SWBKR AND RETIRED SmWr R03 06/22/94 01-BS -HSS -NA 002167 DISASSOGLE MD INSPECT SNUBE IN9rtCTED SP4JBER AND AETIRED Snubber R03 06/22/84 01-3S -HOS -NA 002168 DISASSD9LE AND INSPECT 9NUBE DISA89DOLD NS INSKCTED SWBER MD Retired Snubber R03 08/22/84 01-95 -HSS -la 002169 DISASSO 9LE AND INSPECT SPAD E DISA89 DOLED MD INSPECTED SNUBER MD RETIRED Snubber R03 08/22/94 01-BS -HS$ -NA 002170 DISASSO9LE AND INSPECT SNUBK LISAS909LE AND INBPECTED SWBKR AND RETIRED Snubber R03 08/22/84 01-CC -E -1A 003557 TUK LEAK REMOVED END KLL.1 TUK RtPT1 RED,Ft UDOED SAE.MAK EW GASKET CLEAED NUTS MD BOLTS MD LUBRICATED.INSTA > LLED END KLL AND CLOSED MANWAY

,   R03    06/22/84 01-CV -P      -1A    003602 Pt9F RLMS NOISY                              REPLACED PtBF WITH SPARE MBF R03    06/22/84 01-EG -C     -2      003436 REPAIR FITTING ON $1 K OF                    REFtAED EAD GAGETS AND REED VALV E ON COPPE300R R03    08/22/94 01-IA -C      -1     003120 REMOVE /E INSTALL BELTS FOR MOT EINSTALL MLTS MS N.10N Mi1EY
                                                                                                           .2-_,  - . _ _ . , . _ _ _ . _ , . . . , . .
                       ' '~                         +         -                , . - . - _ .         ,,.y                       -

VEPCO SAFITY RELATD DURI'D Rmrrn P0hER 90RTD BY UNIT AND KF'ARTNENT PROGRM WT09860 09/10/94 15t06

                .'      FROM OS/01/64 Tietu 06/31/64 UNIT 01 SURRY                                                     Fago 25 cf 38 RETthED TO                        WD DEPT ERVICE            M K NUMER      MMER                  WO TITLE                    HISTORY 

SUMMARY

R03 06/22/64* C1-SW -P -19 003410 REMJ1LD PUPF LOW DISCHEGE FLO REMOVED PUMP DISASSEMBLED SUCTION BELL AND IPPELLER REPUED KLL WITN EW.REASSEMBLID WITN .011 IN. CLEARANCE IPPELLER TO DELL. SUCTION STRAIER CLOGOG.REPLACD W/LAR0ER R03 06/22/94 01-VS -E -4A 002857 CHILLER TRIPS ON LOW SUCTION PLUDGED 8 CON KNK R TUIES MAKING A TOTAL OF 11 TU KS PLUGOED DRIED M01 STURE OUT OF REFRIGERANT SYSTEM REC HAR0ED MD STETD UNIT R03 08/23/94 01-M -HSS -m 002719 DISASSDeLE/ INSPECT SWfPKR (S DISAS9EMKED MD INSPECTD SNUDER AND FETIE ' Snubber-R03 06/25/89 01-CH -MOV -1381 003928 PACKING EEDS ADJUSTING OR ADASTD PACK!NG 3 FLATS R03 06/27/94 01-VS -F -T9 003856 KLTS OR Fu1IYS MKING EXCES- ADASTEC KLTS R03 06/26/94 01-CV -P -1$ 004312 LMCOLFLE/RECOUPLE FOR ELECT. VOID!LISTEED TO PLbF RtN. NO AbN0h MAL N0!$E NEMtD. TE MIK TOU MAY KAR IS NORMAL. R03 08/29/94 01-M6 - -196 003495 VALW IIAKS T)ftU G.0K MVE VO!D! WORK TO K C0FFtET D ON WO 9003390 R03 06/29/94 01-MS -PCV -102A 004169 VALVES LEM BY FU 1ED DONNET ON VALVE REPLACED GAShETS AND TO BODY TO 90>eCT BOLTS TO 165 FT LDS RO'3 06/29/84 01-MG -PCV -102) 004160 M VE LEMS BY PULLED DON ET ON VALVE.PEFtACED GASKETS MD TO 90DY 10 DONDET BOLTS TO 165 FT LDS i R03 06/30/94 01-M -H6S -m 002704 DISASSD ELE IrG TCT SNUB ER INSFECTD SNUDKR MD RETIRED Snubber R03 08/30/04 01-M -HBS -NA 002705 DISASSO9LE SNUDKR IN9FECT IN9PECTD $ NUDER MD RET!O Snubber C3 06/30/94 01-DS -HBS -M 002706 D!$ASSDOLE SNUDER INS 8tCT IN9PECTD SNUDER MD RETIRED $nutber R03 08/30/94 01-M -HSS -M 002707 DISASSDRE SMlDKk INSPECT IN9FTCTD SNUDtut M RETIRD $nubber R03 08/30/94 01-M -NES -NA 002700 D!SA8SDSLE IN9PECT SNUDKR IN9TCitD SMJDKR M RETIRED Snobber R03 08/30/94 01 M -NB3 -M 002709 DISA6KMblE INSFTCT SNUPKR IN9FTCTD SNUDKR MD KT!KD $nubber - RC3 08/30/94 01-M -HBS -m 002T10 D!iAS3 DELE !N9PECT SNUDKrt DISASSDRED M IN9PTCTD 96KR MD KTIED Snubber

                .      .                                                                                 Page 26 of 38 VEFC0         SAFETY RELATED DURING REDLCED POWER SDRTED BY UNIT AND DEPARTMENT             FS:0 GRAM L*T09360 09/10/84 15:06   ,.

FR0rt 08/01/B4 THRU 08/31/B4

     .                           LPi1T 01 SURRY RETLRNED TO                        WO DEPT     SERVICE       Wie NuribER      NUMBER           WO TITLE                             HISTORY 

SUMMARY

R03 08/30/84 01-35 .HSS -NA 002711 DISASSESLE INSPECT SNUBBER INSPECTED SNUBBER AND RETIRED Snubber 1

                                                                                             .                                      I R03      08/30/84 01-PS -HSS -NA         002712 DISASCEMBLE INSPECT SNUBBER         DISASSEMBLE SNUBBER AND RETIRED Snubber R03      08/30/B4 01-BS -HSS -NA         002713 DISASSEMBLE INSPECT SNUBBER         INSPECTED SNUBBER AND RETIRED     Snubber R03      08/30/84 01-PS -HSS -HA         002714 DISASSEMBLE INS ~ICT SNUEBER        DISASSEMBLED SNUBBER INSFECTED AND RETIRED SNUBBER R03      08/30/84 01-PS -HSS -HA         002715 LISASSDL%E INSFECT SNUBBER          DISASSEMBLED AND INSDECTED SNUBBER AND RETIRED Snubler R03      08/30/84 01-BS -HSS -NA         002716 DISASSEMBLE / INSPECT SNUBBER (S DISASSEMBLED AND INCDECTED SNUBBER AND RETIRED         5nuble r R03      08/30/84 01-BS -HSS -NA         002717 DISASSEMBLE / INSPECT SNUBBER (S DISASSEMBLED AND INSPECTED SN'JBBER AND RETIRED Snubber R03      03/30/g4 01.PS -HSS -NA         002718 DISASSEMBLE / INSPECT SNUBBER (S DISASSEMBLED AND INSPECTE SNUBBER AND RETIRED         Snubber R03      034 0/84 01-CH -RV -1203 003006 REI:UILD SPARE RELIEF VALVE               D'KRHAULED VALVE REPLACED SPINDLE GUIIE, GASKETS. DISC. CLEANED LAPFED P ERFORMED PT 12.2 FOUND DISC DAMAGED SPINDLE BENT K03      08/30/84 01-EE -RV -104         002412 EWR B4-179 EXISTING RV DOES NO TEST NEW UALVE AS FER PT-12.2 THE4 REFLACE OLD VALVE WITH NEW VALVE AS PER EWR-84-179 R03      c.8/30/84 01-EE -RV -106        002413 EWR B4-179 EXISTING RV DOES NO TESTED VALVE AS PER PT-12.2 REPLACED VALVE TOOLS: PIPE WRENCH 12"10" CRECENT R03      .M/30/84 01-EE -RV -107         002415 EWR B4-179 EXISTING RV ICES NO TEST NEW RELIEF VALVE AS PER PT-12.

2 AND REPLACED OLD UALVE WITH NEW TESTED VALVE AS PER EWR-84-179 R03 eG/30/84 01-EE -RV -108 002414 EWR 84-179 EXISTING RV DOES NO TESTED VALVE AS FER PT-12.2 REPLACED VALVE i R03 N/31/84 01-CC -E -1A 004442 1-CC-E-1A HAS TUBE LEAKS PLEAS CECKED 1-CC-E-1A FOR TUBE LEAK F00 ND NO TUBE LEAK HAD OFS VERIFY PCTE DEWITT AND LOU JONES 403 N/31/84 01-CH -P -1B 002620 OIL LEAK BELOW BULL EYE REFuCED BULLS EYE O rv - .

    .. ,                                                                Page 27 of 38 I

MAINTENANCE OF SAFETY RELATED SYSTEMS DURING OUTAGE OR REDUCED POWER PERIODS UNIT NO. 2 MECHANICAL MAINTENANCE 1 l l i l i 1

      .       .-                                                                                                                        ,                                                                                         Page 28 of 38 VEPCO'     SAFETY RELATED DLRING REDUCED POWER SORTED BY UNIT AND DEFARTMENT                                                                                                                                            PROGRAM WPT09860 09/10/84 15 06 FROM 08/01/34 Ts u 08/31/84 UNIT 02 SURRY FETURNED TO                       WO DEPT    SERVICE       MARK NUMBER     NLMBER                                                    WO TITLE                                                                                                                  HISTORY 

SUMMARY

R03 08/13/84 02-CH -FCV -2114B 003579 CHECK TRAVEL OF VALVE WENT TO TE BORIC ACID FLATS AND IS OLATED TE AIR TO THE VALVE.WE THEN

  • BLED TE AIR OFF DOME TO CECK SEE IF UALVE WOLLD MOVE IT DIDN'T.VLV IS LEAKING Tsu MECH PROBLEM R03 08/20/84 02-MS -TV -201A 003740 FURMANITE RIGHT SIDE - PACKING DRILL AND TAP PACKING GLAND AND INJ ECTED WITH FURMANITE COMFOUND NUCLE AR GRAIE FIBER CART LOT 1012 WR NO.045026 SUBMITTED TO RETURN TO ORIGINAL R03 09/22/84 02-CH -FCV -2114B 003578 ADJUST STROKE REPLACED DIAFWAGM IN VALVE FOUND N OTHING WRONG WITH OLD DIAFtiRAGM l

R03 08/22/84 02-SHF-HSS -17 0035F2 LOW LEVEL IN ESERVOIR CECK SNUBBER RESERVOIR.BEFORE l FILLING 75% FILL TO 95X t l R03 08/27/04 02-MS - -377 003985 FURMANITE REINJECT FACKING REINJECTED VALUE PACKING WITH FlRMA NITE NUCLEAR GRAIE COMPOUND N-FIBER ! CART LOT # 1011 TO STOP LEAK.WD l SUBMITTED TO REPAIR 6098630 R03 08/27/84 02-MS - -381 003971 NIGH PRESSURE STEAM LEAK ON DRILLED TAPED AND INJECTED VALVE B0 NNET WITH FURMANITE NUCLEAR GRADE C OMFOUND F 83 NEW LOT till TO STOP LEAK. WO SUBMITTED TO REPAIR WO WO $098631 R03 08/27/84 02-MS -HSS -34A 004204 FLUID LEVEL LOW FLEASE REFILL FOUND RESERVOIR 4/5 FULL AND ADDED 160UNCES OF SNUBBER FLUID TO RESERVOIR R03 08/29/84 02-CS - -069 004129 3/4" LINE COMING OFF 0F 2-CS-0 REh0VED PIFECAP REMGJED OLD TEEAD DOPE.USED FILE TO REMOVE BtRS FROM TmEADS.USED NEW TR EAD DOPE AND p REINSTALLED PIPE CAP R03 08/30/84 02-CH -P -1A 004356 REPLACE AUX OIL FUMP REMOVED OLD AND INSTALLED EW I AUXILIARY DIL FUF AND ADD AFTROX l 1 GALLEN OF OIL (IND 68) TO RESERVOIR O h e 9

t Page .29 of 38 O MAINTENANCE OF SAFETY RELATED SYSTEMS DURING OUTAGE OR REDUCED POWER PERIODS UNIT NO.1 l

              .                                                                                   ELECTRICAL MAINTENANCE                                                 ,

1 4

                                                                                                                                                                       +

o

                                                                                                                                         ------Page 30 of .38. -

VEPCO SAFETY RELATED DLRING REILCED PulER SORTED BY LMIT AVO DEPARTPENT FROM 08/01/84 Tistu 08/31/84 PROGRAM F T09860 09/10/94 15I06

        .                                     LMIT 01 SLRRY RETtstpED TO                                     WD DEPT SERVICE              MARK NLMBER              NLMBER                    WO TITLE             _

HISTRY SL39WtY R04 08/10/84 01-EPH- -IC 003504 REPLACE 1C RSS LEAD FROM TRANS PERFUDED "HI-POT" TEST ON CABLES F CR C RSS XFP5t DECKED ALL CABLES AN D FDLMD 1F1PH9 (M C 0 TO IE BAD 8/10/B4 R04 08/13/94 01-NI -REL -IRBYB 003431 RELAY IS ET PICKED LP SELLD REPLACED COIL AND RELAY AS!EMBLY AS PER EPP-C-RT-24 9-9-64 R04 08/16/94 01-EE -90/ -104 003679 Sp/ WILL ET (PEN REPLACED COIL AfE AUX CIMTACT R.DCK IN 1-EE-P-1C M.C.C. R04 08/16/94 01-EPL-BKR -1912 003559 CIRCUIT BREAKER TRIPS AND BRIDGED AND EDGERED AC 9.2 AB 8.67 BC 9.2 PEG (ED 1000M 'A' CAUSES BREA KER TO TRIP TEST BKR SAT SUSPECT 'A

                                                                                                                             ' PHASE AS PROBLEM 8-12-94 EATER SE
                                                                                                                                                                                                                         ~ ~

EMS TO BE SAT EST TAG BKR 1481-2  ; R04 08/16/84 01-IA -C -4B 003036 AIR COPP BKR TRIPS n4EN CDPRE PERFIRED PMS ON 1-IA-C-4B AND TEST l RAN SAT,ND PROR. EMS FOUE WITH TE 4 BREAKER TRIPPIE l R04 08/1484 01-IA -D -4B 001993 HI(M TDP ALARM IN lMILE PERF(RMING PMS ON 1-IM-4B l TE AIR DRYER DEIXED OUT SAT AND D i ID DOT TRIP TE BREAKER 9-14-64 l R04 08/16/84 01-MS -SOV -102A 003336 ELEC. DISC 0f0ECT/ RECD 9ECT DISC 30ECT SOV B-14-64 INSTALL AND AD.1ET LIMIT (M SOV 102A B-15-64 R04 08/16/94 01-MS -SOV -102B 003335 ELECT. DISCOP0ECT/RECOP6ECT DISCDGECTED SOV'S DEED 20" (F #1 LIRIID TIINT FOLMD LIQUID TISHT BROCKEN.INSTALLAND AILRJST LIMIT ON SOY 102B 9-15-64 R04 08/16/B4 01-SW -MOV -105C 003733 DO NOT DET CLOSED INDICATION C REAILXJS1ED' LIMIT SWITDES AND TESTE D SAT 9-16-44 R04 08/21/B4 01-NI -DET -32 003521 REPLACE PRE-#P REPLACED PRE APP AND PERFIRPED PT-1

                                                                                                                             . 4 ON ERAlER TO RETLRN TO SERVICE R04 08/22/B4 01-RC -PT '-456                        003432 ALARM IS SPtRIOUS AND IS BEI E REPLA 2 D PC-456A PC-456B PC-456C PC
                                                                                                                         .  -456D AND PM-456 AND PM-456A DECKE D F(R LOOSE C0f0ECTICMS BUT FEMD N GE.PERFIRPED PT-2.4A SAT IO(ITIR L O(P WITH RECGtIER 90 SPINES R04 08/23/94 01-01 -P                     -2D      003669 REMOVE INSLLATION/DISCD9ECT                                 llEEVED EAT TAPE AND DISCWSECTED 9-20-84.IIEINSTALLED EAT TRACE REPAIRED FLEX 31 STRIP EATERS 9-23-94 R04 08/23/84 01-RC -                      -4GSC 003998 ALARM IN 90LLD ET E IN                                        "DE KF RELAY 15B3 AS FGMD READIES lERE ACCEPTABLI BUT DLE TO LDEXPLAN (PERATIONS TE RELAY 1%S BEEN REPLA -

CED WITH STOCK PARE KF R04 08/29/94 01-EE -BKR -1H12 004228 BREAKER 15 ICT 1ABELED AND IS SWlE

  • 1I04 '88/30/94 41-EPH-tKR -15J10 004121 REPLACE PIN AND 9'RIE IDFLETED INSTALLATION IF CL(ME '

i

          ~

1AltH ANTI SED 1PRIIG AND 4EW

            ^

COTTER KEY LEIM PRG2R5lE TDP-C-E PH-129 BLEAKER TESTED F29-94 SATIS

                                                                                                                           'TACTGtY                                                                    ,

e 4104 -08/30/94 01-4E -PCV -102A 404316 SISCDGECT/IEIDGECT ILECT. LIMIT SIITDES afb SOV 185LTED FR0 fl YALUE 8-29-64. LIMIT SIITDES AfS p  :- .. NIV 4ERE AUEADY IM UALVE DEDO

p. , 70 MAKE E5lE EVERTHIIE ABEINED E F1104 ~ M /94 01-95 -PCV -102B 004315 SISC30EL7/IEIDGECT ELECT LIMIT SIITDES AND SOV LIGELTED L . fit 0M UALUE 4-29-94 l 4 LIMIT SWITDES AND 1mV nERE ALflEADY

' 1

       .1 _                                                                                                                     ML1ED LP DECRED TO SEE IF ABENED g
                                                                                                                                                                                                                       ~

l er - -- e y ww - --.----e,.,, ,ee -- w-+-+ --w-c-s-~ew e e--'w wso-'-ve--w----+--%,e -ewvv--eav--we*-we--wwwe-=-e~= = - = w

3 Page 31 of 38 4 MAINTENANCE OF SAFETY RELATED SYSTEMS DURING ~ OUTAGE OR REDUCED POWER PERIODS UNIT NO. 2 ELECTRICAL MAINTENANCE l

                                    . ~ . . _ . . _ . _ _ _ . _ - . _ , . .  . . _ . . . _ _ . _ . . . . . . _ _ _ _ .

O

        *
  • P ge 32 of 38 -

WPC0 SAFETY RELATED ILRING REDLCED POWER SDRTED BY UNIT AND DEPARTMENT PROGRAM F T09860 09/10/84 FROM 08/01/84 Tmu 08/31/84 UNIT 02 SURRY RETLRNED TO WD ICPT SERVICE MARK NUMBER NUMBER WO TITLE HISTORY

SUMMARY

ADJUSTED LIM 5T SWITCH ARM ON IFFER R04 08/10/84 02-CH -FCV -2113A 003417 INTEREDIATE INDICATION SWITCH TO GIVE OPEN LIGHT FAILURE MDIE: INCORRECT LIGHT INDICATIONS: FAILURE MECHANISM: LIMIT SWITCHES OUT OF ANUSTMENT AFitIED HEAT AT 1930 CHECKED WITH R04 08/1l 94 02-DA -LS -121B 003707 HI LEVEL ALARM WILL NOT CLEAR OFS AND ALARM 13 NOW CLEARED 003698 14:EAKER TRIPS AND WILL STAY BRIDGE AND MEGGER SAT BKR STILL TRI R04 08/17/84 02-RC -BKR -4/4 PS 8-15-84 70 AMP (W) CAT 3 EHL3070 A TIMING CIRCUIT ADDED TO A+B BREAKER R04 08/17/04 02-RP -IKR -A/B 002784 INSTALL TIMING CIRCUITRY IN S AND INST TECH PT 81 CONFtETE RETURNED TO NORMAL OFS 8-16-84 001833 ALARM WILL NOT INDICATE BULBS JUHFER CONTACT TO GIVE ALARM IN R04 08/20/34 02-RI -ANN -AA7 CONTROL ANN BOARD. REPLACED CAER NO CECK ALARM SAT 4 004016 POWER FAILURE LIGHT IS ON FUES FOUND TO BE BAD ORDERED NEW FU R04 08/22/84 02-FP -PNL -2 SE MIN 5 STOCK 40325214 INSTALLED F USE AND RESTORED FT)WER TO DETECTOR IELUGE PNL.CECKED WITH CONTROL R00 M OPERATOR TO CLEAR ALARM 003905 t#CERTEMP INDICATION LIGHT IS CKT 55 NOT IN SERVICE THIS MODULE i R04 08/23/84 02-HS -PNL -2A1 ' IS A SPARE CKT 53 IS TE LAST CNT L ISTED IN BOOK 2A1 f EXISTING RELAY REMOVED EW RELAY R04 08/30/84 02-MS -LC -497BX 004029 RELAY IS CHATTERING INSTALLED

                                   -1A      004494 AUX OIL PUPF DRAWS HIGH          FOUND THE EATERS WERE TO SMALL R04    08/31/84 ObCH -P                                                       MOT (R PtLLS .86 MS HAETERS 111 i                                                          GOOD FCR .598 1115 HEATERS WERE
                         ,                                                          FUT IN.                ,

b t e o f  ! t

                                                        . , , .            ---         . . . - - - - , - -           -- , , , , , , ,                  ,-       ,a -

Page 33cof'38 MAINTENANCE OF SAFETY RELATED SYSTEMS DURING OUTAGE OR REDUCED POWER PERIODS UNIT NO.1 INSTRUMENT MAINTENANCE I e y- g * - m, w- ,-g w-w - - y ++gaw, g w-+ -- wr-y-,- y- ,-w-----,m-------w---g,r -, --tw, w-g-g.,,e----v-,+w-y-, m,e g g ,- r- g-N-,

VEPCD $ SAFETY JtELATD ILRINO REDU::D PDER SDRTD BY UNIT AE DEPARTENT PkDGRM IFT09860 09/10/84 15tC6

             .                         FROM 08/01/94 T)stU 06/31/94 UNIT 01 SURRY                                                                       Page 34 of 38 RETIKeED TD                                     61 0
      . DEPT SERVIE                     MARK E SER       NLMBER               WO TITLE                        HISTORT SUPMARY T22 08/03/84 01-RP -MISC-FB                        003153 IRFI F-B STLI:K                    REMOVED AND AD.1JSTD POINTER AND RE INSTALLED IEICATIONS CECK 0000 T22      08/13/94 01-RM -SV -111                   002976 MONIT(R SPIKING CAUSING HI ALE MONITDRED PROBLEM Ftm 7 DAYS COLLD DCT DET PROBLEM TO IAP ICATE RETLRNItG PENIT!R TO SERVICE l

T22 08/16/94 01-RP -MISC-D4 002133 VERY INRATIC DEDICATION PLACD .AAPER IN ROD BUTTOM BISTABL E MONITGIED ROD VELTE FOR SEVERAL DAYS. REEVED . ASPER ON BISTABLE DE CKED AND RETLAtED TD SERVICE TOOLS 1 V(LTETER VO-24

 . T22 08/16/B4 01-51 -PT -929                        002697 RECALIBRATE/LARGE DEVIATION BE DECKD CALIBRATION OF INDICATER SAT T22 08/16/94 01-SI -PT -931                       002698 RE:ALIBRATE/LAR(E DEVIATICH BE DEKED CALIlutATION (F INDICATOR SAT    PROCEDL5tE SENT TO ENDIEIRIE TO(LS DMW VO-15 T22 06/20/84 01-RP -MISC-N/A                      003421 CPUT SETPOINT LENT LD INVESTI- VOID SNE AS 3902003422 l       T22 06/21/84 01-CS -LI -100D 002B40 CHIV RWST LEVEL READS LulER TH AILEJSTED INDI:ATOR AS PER PT.219A DECKED SAT PT SEh7 TD EE T22 06/21/B4 01-RC -TI -467                       003870 TDPERATINtE IEICATOR FIR P         DECKED TE CALIBRATION OF TE LIN-LEVEL NFLIFIER AND INDICATER ALSD DECED TE RTD RESISTMCE ALL IGij LES NE WITHIN SPEEIFICATION DECKE D SAT T22 06/22/94 01-CV -P1 -101A 003805 ) .1 DP DIFFERENCE BEThED 1-C 2ERO SHIFTED ON TRANSMITTERS.PERFOR ED TRANSMITTER CALIBRATION DEKD SAT (BOTH CHAl#ELS P-CV-101A & 101 B) PT"S SENT TO DEIMIRIE T22 06/22/94 01-ftM -RI -160                      003603 IENITER FAILD                      TIOHTDED FLEE DEUER DEKED SAT T22 06/22/94 01-VG -4tM -130/2 OC2230 REPLA 2 PLPP                                           REPLACED PUPP                               ELETRICIANS TA0(E
                                                                                                 . D BREAER AND REMOVED LEADS TD PL7F i

T22 06/24/94 01-BR -LI -103A 002103 CALIBRATE EVEL IEICATIR PERFORED CALIBRATION COPPLITELY MA DE MDER AD.AJSTENTS AS EESSARY (PS SAT - T22 08/24/94 01-BR -LI -103C 002104 CAJBRATE PETER (FUPP CAVITATED PERFORPED CALIBRATION PR6CEILFC CDPITELY MADE MINOR AILAETENTS AS REDUIRD l i (PS SAT l

   , T22 08/24/94 01-CH -+CV -1104 003863 C BAST RE::IRC VALE WILL E T                              REPUGD RESTRICTER PLIE ABSY T22 08/24/94 01-HI -YI -100C 003963 LITT BAR (N LIMI9t4PH ET                                 REPLACED IIISPLAfDMt AND DEKED LLMI9tAPH T2_2 0.8../24/B4 01-RC -TR .4099     -      -

003182 RED PEN IS DIRATIC REPLA2D REI:0RDER SERVO ETOR,CALIB

                                                                                                                                                                      ~

T22 08/24/94 01-51 -PI -1943 00372B GALDE PCT POLNTD TD BRACKET ICLNTED Id7D E150lET T22 08/24/94 01-SI -PI -1944 003727 94 LIE ET POLNTED ON BRACKET 1CLNTED GLMOE TD 3 RACKET IPS SAT T22 418/30/94 01-RM -4tR -150 004258 RE-IE REIUtDER IE PAD REPLACED LTtNT PRINTDE TE PADS PADS PN 430735591-501 30735591-506 30735591-503 122 48/30/94 01-YS -IET -100B 004095 4AAIINIIG ALARM WILL POT CLEAR PERFUtPED CAL 41HTIND CALIIRATION CARD REIEf! RED AILAJSTIENT. AD.AETED SAPE-{P SAT 722 08/31/94 01-CC -PI -1139A 002593 lIISCHARIE PREES SALIE fEDIED H CALIBRATD IISICATER m 08/31/94 11-Di -P --2B -003866 84 LIE TEDS 701E ItECALIBRATED REPLACED RAE 1PS SAT

     'T22 38/31/94 D1-Di-PI -1151 903359 #EALIBATE SMLIFY AND ASSIGIE PERFUDED PT 40 SALIE JPS SAT 722 9B/31/94 01-eW -H34 -102                      004196 IMPECT & ltEPAIR A6 IEIESSARY INSTALLD EW ADtCMG OUTPUT 4GILLE AND CALIBRATD IT. VELTIETER SIE212
 * .,                                                                                           Page 35 of 38 i

MAINTENANCE OF SAFETY RELATED SYSTEMS DURING OUTAGE OR REDUCED POWER PERIODS UNTT NO. 2 INFTRUMENT MAINTENANCE I s

    *     '*                                                                                    Page 36 of 38 VEFC0      - SAFETY RELATED IllRING REDUCED FSER SORTED BY UNIT AND IEPARTMENT         PROGRAM IFT09860 09/10/84 15:06 FROM 08/01/84 T}RU 08/31/89 UNIT 02 SURRY RETURNED TO                        WO IEPT    SERVICE      MARK NUMBER      NLFBER            WO TITLE                          HISTORY 

SUMMARY

T22 08/16/84 02-CH -FCV -2114A 003158 REMOVE REINSTALL INSTRUMENTATI REFLACED INSTRUMENTATION ON VALVE AND STROKED FROM CONTROL ROOM T22 08/16/84 02-CH -FCV -2114B 003159 REMOVE REINSTALL INSTR'JMENTATI REMOVED INSTRUMENTATION FOR VLAVE MAINTENANCE 8-10-84 REFLACED INSTRUMENTATION T22 08/16/84 02-FW -FT -2486 003664 TRANSMITTER INDICATING LOW REPLACED FM-486 AND PERFORMED IMP-C - -RP-009 AND PT-2-10A ON NEW MODULE T22 08/21/84 02-RI -MISC-422B 003422 HM-2-422B FUNCTION GENERATOR REF1. ACED FUNCTION GENERATOR AND CHE CKED CALIBRATION PT SENT TO ENGINEERING T22 08/21/84 02-RM -RMS -260 003525 ALARM SETFOINT 11% HIGHER THAN CHECKED SETFOINST IN ACCORDANCE WITH CALIBRATOR PROCEDURE T22 08/23/84 02-NI -MISC-NA 003925 PERM. STATUS LIGHT NOT LIT. REPLACE RELAY i PRB-XB 8-21-84 T22 08/24/84 02-IC -IC -B 003673 REFtACE INCORE DETECTOR 'B' REPLACED B" INCORE IETECTOR T22 08/31/84 02-RC -MISC-408 002802 TONE READS 21/2 F HIGER FERFORMED REPLACEMENT OF TAVE AM-PLIFER VEPCO STOCK 1430252. OP CK AND CALIBRATION SAT. PART ?4739932 END OF REPORT 1

m. - - - - -

Page 37 of 30 HEALTH PHYSICS I Aucust, 1984

                            'Ihere was no single release of radioactivity or radiation exposure
                           - specifically associated with an cutace that accounted for more than ten percent of the allowable annual values in 10CER20.

F 9 l l

I

          -     -                                                          Page 38 of 38             I e     .

PROCEDURE DEVIATIONS REVIEWED BY STATION NUCLEAR SAFETY AND OPERATING COMMITTEE AFTER TIME LIktn SPECIFIED IN TECHNICAL SPECIFICATIONS August,1984 Number Unit Title Date Date Rev. Deviated g SNSOC EMP-C-EPL-70 1 Replacing Terminal Block 3-2-83 8-23-84 Termination with Raychem WCSF-N Type In Line Field Splices MMP-C-HSS-023 1,2 Corrective Maintenance Procedure 4-2-84 8-21-8 4 for 8" and 10" Grinnell Hydraulic Suppressors Dual Bleed Orifice MMP-C-CN-132 1 Replacement of Condenser 9-27-83 8-28-84 Expansion Icint Rubber Belt 1-SC-CN-1A M MP-C-CN-132 1 Replacement of Condenser 9-27-83 8-28-84 Expansion Joint Rubber Belt 1-SC-CN-1B

o ..

      +

.g t t 1 I ) l . This is a corrected page for July '84 Monthly Operating Report for Surry Power Station

                                                                                        .                                             1 9/14/84                                                  l
                  .                                                              MD 1

1

o' ee Pagul0 of 36

SUMMARY

OF OPERATING EXPERIENCE -

  -                                                                                    Corrected ' Copy   l MONTH / YEAR          July,1984 Listed below in chronological sequence by unit is a summary of operating
         ' experiences for this month which required load reductions or resulted in significant non-load related incidents.

UNIT TWO 07-01-84 0000 This reporting period begins with the unit at 100% power (775 MW's). 07-08-84 0356 Commenced power reduction for load following at 150 } MW's/HR. 0453 Holding power at 84% (660 MW's). 0710 Commenced power increase at 150 MW's/HR. 0800 Unit at 100% power (775 MW's). 07-09-84 0041 Commenced power reduction for load following at 150 MW's/HR. 0143 Holding power at 84% (660 HW's/HR). 0440 Commenced power increase at 150 MW's/HR. 0550 Unit at 100% (775 MW's). 07-16-84 0847 Turbine bearing indicating a vibration problem with #2 L.P. Turbine. 07-17-84 1930 Commenced plant shutdown at 150 MR's/HR to allow balancing #2 L.P. Turbine. 07-18-84 014 9 Unit off the line. 0221 Reactor shutdown. 1525 Reactor critical. 2005 Unit on the line. 2054 Unit at 35% power (230 MW's), holding for chemistry. 2234 Commenced power increase. 2340 Holding at 60% power (420 MW's) for return of "E" main feedpump. 07-19-84 0500 Commenced power increase. 0759 Unit at 100% power (770 MW's). 07-31-84 - 2410 This reporting period ends with the unit at 100% power (770 MW's). i l 1 _ l

0 e x~n . .n . VIRGINIA 1$LECTRIC AND' Powsu COMPANY Ricnwown,VamoxxrA 20261 -

                ' W.L.Stawaar
             . f,2*,",$"""","L                                                          September 14,:1984 Mr. Maurice R. Beebe                                                                                                                  Serial No. 551 Office of Resource Management                                                                                                         N0/JDH:acm U. S. Nuclear Regulatory Commission                                                                                                   Docket Nos. 50-280 Washington, D. C. 20555                                                                                                                           281 License Nos. DPR-32

Dear Mr. Beebe:

DPR-37 VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION UNIT NOS. 1 AND 2 MONTHLY OPERATING REPORT Enclosed is the Monthly Operating Report for Surry Power Station Unit Nos. I and 2 for the month of August, 1984. ry.... t ru urs.

                                                                                                                                              \

s W. L. Stewart Enclosure (3 copies) cc: Mr. R. C. DeYoung. Director (12 copies) Office of Inspection and Enforcement Mr. James P. O'Reilly (1 copy) Regional Administrator Region II Mr. D. J.-Burke NRC Resident Inspector Surry Power Station l

  ._.               .      _ _ _ _ _             - _ - _ _ _ _ _ - _ - -            _ _ - - _ _ - - _ - - _ _ _ _ - _ _ - _ _ _ - _ _ _ _ _ .                           _ ____ -          ___ -}}