ML20092L768
| ML20092L768 | |
| Person / Time | |
|---|---|
| Site: | Crane |
| Issue date: | 05/31/1984 |
| From: | Hukill H, Casey Smith GENERAL PUBLIC UTILITIES CORP. |
| To: | NRC OFFICE OF RESOURCE MANAGEMENT (ORM) |
| References | |
| 5211-84-2145, NUDOCS 8407020005 | |
| Download: ML20092L768 (7) | |
Text
'
)
OPERATING DATA' REPORT DOCKET NO.
50-289 DATE June 15,1984 COMPLETED BY c, g,rh TELEPHONE (717uap_gs;1 OPERATING STATUS NOTES 1.-UNIT NAME:
THREE MILE ISLAND UNIT 1
- 2. REPORTING PERIOD:
MAY
,1984.
g 3.. LICENSED THERMAL POWER (MWT):
2535.
4.xNAMEPLATE-RATING (GROSS MWE):
871.
- 15. DESIGN ELECTRICAL RATING (NET MWE):.
819.
6.: MAXIMUM DEPENDABLE CAPACITY (GROSS MWE):
824.
- 7. MAXIMUM l DEPENDABLE CAPACITY - ( NET L'WE ) : '
776.
t k
V
- 8l. IF CHANGES OCCUR IN'(ITEMS 3-7) SINCE LAST REPORT, GIVE REASONS:
1 9'.
POWER LEVEL TO WHICH RESTRICTED, IF ANY (NET MWE) 110. REASONS FOR' RESTRICTIONS, IF ANY:
l
=
THIS MONTH YR-TO-DATE CUMMULATIVL fil.-HOURS IN REPORTING PERIOD 744.
3647.
85440
-12. NUMBER'OF HOURS REACTOR WAS CRITICAL 0.0 0.0 31731.0 13.fREACTOR RESERVE SHUTDOWN HOURS 0.0 0.0 838.5
':14. HOURS-GENERATOR ON-LINE 0.0 0.0 31180.9
- 15. UNIT RESERVE SHUTDOWN HOURS 0.0 0.0 0.0
-16.; GROSS-THERMAL, ENERGY GENERATED (MWH)
O.
O.
76531071.
- 17. GROSS ELECTRICAL ENERGY GENERATED (MWH)
O.
O.
25484330 18.. NET ELECTRICAL ENERGY GENERATED (MWH)
O.
O.
23840053.
- 19. UNIT SERVICE FACTOR 0.0 0.0 36.5 20 UNIT AVAILABILITY FACTOR 0.0 0.0 36.5
- 21. - UNIT CAPACITY FACTOR (USING MDC NET) 0.0 0.0 35.6 22.SUNIT CAPACITY-FACTOR (USING DER NET) 0.0 0.0 34.1
- 23. UNIT FORCED OUTAGE RATE 100.0 100.0 60.1
[24 SHUTDOWNS SCHEDULED OVER:NEXT 6 MONTHS (TYPE, DATE, AND DURATION OF EACH
- 25. IF SHUT.DOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTi1P:
G D
DO O
O R
40 t
l
. o-.
l AVERAGE DAILY UNIT POWER LEVEL
~
,l-DOCKET NO.
50-289 UNIT TMI-1 4
DATE June 15, 1984 COMPLETED BY C. Smyth
.8 TELEPHONE (717)948-8551 p
i
= MONTH:
-MAY i.
I
-- DAY AVERAGE DAILY POWER LEVEL DAY-AVERAGE DAILY POWER LEVEL l
l (MWE-NET)
(MWE-NET) l 1-O.
17 0.
- 2' O.
18 0.
j
- 3 0.
19 0.
l 4
0.
20-O.
l
- 5 O.
21 0.
6 0
22 0
j
-7 0
23 0.
8 0.
24 0.
q~~
9 0.
25 0.
10 0.
- 26 0.
. 11 0
27 0.
i 12 0.
- 28 0
, O.
29 0.-
~
14-O.
30 0.
15 0
31 0
. 16~
~
0..
9 9
4*
4 9
4
+
e
3.
=,
y
=,
~1 a
f 50-289-UNIT SilVTDOWNS AND POWER REDUCTIONS DOCKET NO.
UNIT NAME TM1-1 DATE M ma 14-lona COMPLETED BY c_ w_ %f-h
' REPORT MONTH Mg TELEPHONE r71 n nin-nqqi 4
e.
e n
3_e g
.2 _e s
g.E ;i Licensec ge,,
5;wl, Cause & Corrective No.
Date g
3g g
,g g 5 Event
- w E.1
- Action to 33 5
jigg ReporI a r$0 0
Prevent Recurrence d
9 Regulatory Restraint Order i
i 1
84/01/01 F
744 D
1 N/A ZZ ZZZZZZ I
I 2
3 4
F: Forced Reason:
Method:
Exhibit G-Instructions S: Scheduled A Equipment Failure (Explain)
I-Manual for Preparation of Data B-Maintenance of Test 2 Manual Scram.
Entry Sheets for Licensee C. Refueling 3 Automatic Scram.
Event Report (LER) File (NUREG.
D Regulatory Restriction 4-Other (Explain) 0161)
E-Operator Training & License Examination F. Administrative 5
G Operasjonal Error (Explain)
Exhibii 1. Same Source Il-Other (Explain)
. - -.~,.-.
.. = -
g, ;
i
.2:-
June 13, 1984 3200-84-211
~ OPERATIONS
SUMMARY
l LThe unit was shutdown the entire month by order of the NRC.
Core cooling
. as provided by the' Decay', Heat Removal System _except as described below.
i w
The following evolutions were. performed during the month to support Hot Functional Testing:
+
L5/7/84
' Started Circ Water System.
9 /9/84'- ~ Filled Condensate System.
5 5/14/84 - Partially drained both OTSGs.
~
~ 5/16/84 :- Established seal ~ injection to-RCPs.
Established RCS cleanup.
Commenced pressurizing RCS to 312 psig.
Started up Condens.te System.
Established vacuun in condensors.
5/21/84 - Set. containment:-integrity.
ur
~
'5/22/84 - Commenced-RCS heatup.
'5/23/84 - RCS at 525 F~, 2155 psig.
TheIfollowing testing was performed as part of Hot Functional Testing:
i' 8thLstage heaters operational hydro.
RCS-leak rate measurement.(new procedure and new computer program).
.-Hanger. expansion 1 tests for head vents and high point vents.
.. HPI cross-connect flow check..
=:
A7
. PORV ratesta(refurbished valve and modified. spring assembly).
.. Reactor coolant pump vibration analyses and-setting.
. Operational-hydro for:
..:.RCP Pump 1B, p-
^
All.0TSG primary.manways,;
.. - - Decay heat; drop line. tap,
- p
- .. ' Head vent, DHV-1,
... Main. steam relief valves setting.
No-major'~ problems were identified during this; testing.- On May 26,.1984 RCS cooldown was commenced and the plant remained in cold shutdown on Decay
- 1 Heat Removal for the remainder of the month.
' A Reactor Building' Integrated Leak' Rate Test was ~ performed on 5/8/84.
LThe test met the acceptance criteria with very_few problems encountered.
t
~
4:~
MAJOR SAFETY RELATED MAINTENANCE
]'
~
- During the month the following major maintenance items were completed.
u-m
^
- m y
Pi'
~ ~ =
t-
_3 June 1:,.1984 2200-E;-223
. i Reactor Coolant Puro Balancing
~
. R'C-P1A/B/C & D were satisf actorily balanced following repair work on RC-PIB, and realignment of R C-P-1)( C & D.
Local Leak ' Rate-Testing Leak Rate. Valves LR-V2 and 3, the Reactor. Building Fire Service and the OTSG Drain Penetrations-were tested satisfactorily.
Intermediate
~ Cooling Valve IC-V3 failed its leak test and was tested satisfactorily following repairs to the valve seat and gate.
(Co=nonent'Retorquing During HFT, bolts were retorqued on the OTSG manway and handhcle covers as were bonnets on pressure segl valves CF-VIA/B, CF-V4A/B, DH-V1, 2 and 22A..
Main Steam Safety Valve Testing All main steam safety valves were tested satisfactorily during EFT.
L a
Waste Gas Pump Overhaul WG-P1A was overhauled following failure to pump to rated capacity.
The failure was attributed to moisture related corrosion and errosion l o f ' internals". Following' repairs the pump was tested with satisfactory results.
ESAS Relav Reolacement All LSAS relays were replaced because of the unreliability of the
-previously installed Clark relays. This work was performed to resolve problems identified in LER 83-24
~
Atmoseheric Dumo Valve's Replaced MS-V4A/B were replaced with a different model (Fisher Valves) because of a history of leaking by.
Prior to installation the g
internals were modified. _ Work also included valve operator inspection, weld NDT,' flush and hydro testing.
3 9
77 e
-.s REFUELING INFOR!ULTION REQUEST
,O_
T 1.-'Name of:Fae311ty:
Three Mile Island Nuclear Station, Unit 1 2.
Scheduled date for next refueling shutdown:
Unknown 3
Scheduled date for restart following refueling:
i Unknown
- k. ' Will refueling or resumption of operation thereafter require a technical specifi',ation change or other license amendment?
If answer is yes, in gener6h, uhat vill these be?
~
If answer is no, has the reload fuel design and core configuration been reviewed by your Plant Safety Review Co=mittee to determine whether any_ unreviewed safety questions are associated with the core reload (Ref. 10 CFR Section 50 59)?
I If no such review has taken_ place, when is it scheduled?
Amendment No. 50, Cycle 5 reload, was approved on 3-16-79 s.+
'5 Scheduled date(s)' for submitting proposed licensing action and supporting
'information:
N/A 6... Lmportant licensing considerations associated with refueling, e.g. new or different fuel design or supplier, unreviewed design or performance analysis methods, significant changes in fuel design, new operating procedures:
N/A' 7
The ' number of fuel ' assemblies (a) it. th'e core, and (b) in the spent fuel storage pool:
(, a) 177 (b) 208
'8.
TDae present. licensed spent fuel pool storage _ capacity and the size of any increase in licensed storage capacity. that has been requested or is planned,-in number of fuel assemblies:
The present licensed capacity is 752. There are no planned increases at this time.
-9 The projected date of the last refueling that can be discharged to the spent fuel pool assuming the present licensed capacity:
- 1988 is the last refueling discharge which allows full core.off-load capacity (177 fuel assemblics).
e
GPU Nuclear Corporation 198r Post Office Box 480 Route 441 South Middletown, Pennsylvania 17057-0191 717 944 7621 TELEX 84 2386 Writer's Direct Dial Nurnber:
June 15, 1984 5211-84-2145 Office of Management Information and P.
Control Attn:
W. C. Mcdonald c/o Distribution Services Branch.DPC, ADM U. S. Nuclear Regulatory Commission Washington, D.C. 20555
Dear Mr. Mcdonald:
Three Mile Island Nuclear Station, Unit I (TMI-1)
Operating License No. DPR-50 Docket No. 50-289 May Monthly Operating Report Enclosed please find two (2) copies of the May Operating Report for Three Mile Island Nuclear Station Unit.l.
Since: ely, H. D. Hukill, Director, TMI-i
. HDHamle Attachments cc:
V. Stello Dr. E. T. Murley 8
g31G'A 4
Cedifi"a $7 y6 I
\\
GPU Nuclear Corporation is a subsidiary of the General Public Utilities Corporation L..
%