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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217D5211999-09-30030 September 1999 Informs That Remediating 3D Monicore Sys at Pbaps,Units 2 & 3 & 3D Monicore/Plant Monitoring Sys at Lgs,Unit 2 Has Been Completed Ahead of Schedule ML20216J3981999-09-29029 September 1999 Submits Comments for Lgs,Unit 1 & Pbaps,Units 2 & 3 Rvid,Rev 2,based on Review as Requested in GL 92-01,rev 1,suppl 1, Reactor Vessel Structural Integrity ML20212J6561999-09-29029 September 1999 Informs of Completion of mid-cycle PPR of Limerick Generating Station on 990913.Identified No Areas in Which Licensee Performance Warranted Addl Insp Beyond Core Insp Program.Historical Listing of Plant Issues Encl ML20212H6401999-09-24024 September 1999 Forwards Revised Epips,Including Rev 11 to ERP-101 & Rev 18 to ERP-800.Copy of Computer Generated Rept Index Identifying Latest Revs of LGS Erps,Encl ML20212E7941999-09-22022 September 1999 Requests Authorization for Listed Licensed Operators to Temporarily Suspend Participation in Licensed Operator Requalification Program at LGS ML20212E8081999-09-22022 September 1999 Provides Notification That Listed Operators Have Been Permanently Reassigned to Duties That Do Not Require Maintaining Licensed Operator Status,Per 10CFR50.74 ML20212F5481999-09-20020 September 1999 Forwards Response to NRC Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing, for Pbaps,Units 2 & 3 & Lgs,Units 1 & 2 ML20212F8991999-09-17017 September 1999 Provides Written Confirmation That Thermo-Lag 330-1 Fire Barrier Corrective Actions at Lgs,Units 1 & 2 Have Been Completed 05000353/LER-1999-010, Forwards LER 99-010-00,re Manual Actuation of Esf.Main CR Ventilation Sys Was Placed in Chlorine Isolation Mode Due to Rept of Faint Odor of Chlorine in Unit 2 Reactor Encl1999-09-16016 September 1999 Forwards LER 99-010-00,re Manual Actuation of Esf.Main CR Ventilation Sys Was Placed in Chlorine Isolation Mode Due to Rept of Faint Odor of Chlorine in Unit 2 Reactor Encl ML20216F7821999-09-16016 September 1999 Forwards Insp Repts 50-352/99-05 & 50-353/99-05 on 990713-0816.One Violation Noted & Being Treated as NCV, Consistent with App C of Enforcement Policy.Violation Re Inoperability of Automatic Depression Sys During Maint ML20212A8751999-09-13013 September 1999 Forwards Safety Evaluation of First & Second 10-year Interval Inservice Insp Plan Request for Relief ML20211N5061999-09-0909 September 1999 Forwards TSs Bases Pages B 3/4 10-2 & B 3/4 2-4 for LGS, Units 1 & 2,being Issued to Assure Distribution of Revised Bases Pages to All Holders of TSs ML20212A0091999-09-0909 September 1999 Provides Notification That Licenses SOP-11172 & SOP-11321, for SO Muntzenberger & Rh Wright,Respectively,Are No Longer Necessary as Result of Permanent Reassignment ML20211P8571999-09-0808 September 1999 Forwards Reactor Operator Retake Exams 50-352/99-303OL & 50-353/99-303OL Conducted on 990812 ML20211P3891999-09-0303 September 1999 Informs That During 990902 Telcon Between J Williams & B Tracy,Arrangements Were Made for NRC to Inspect Licensed Operator Requalification Program at Plant.Insp Planned for Wk of 991018 05000352/LER-1999-009, Forwards LER 99-009-00,providing 30-day Written follow-up Rept Re Performance of Maint That Affected Safeguard Sys for Which Compensatory Measures Had Not Been Employed1999-09-0101 September 1999 Forwards LER 99-009-00,providing 30-day Written follow-up Rept Re Performance of Maint That Affected Safeguard Sys for Which Compensatory Measures Had Not Been Employed ML20211H2571999-08-26026 August 1999 Informs of Individual Exam Result on Initial Retake Exam on 990812.One Individual Was Administered Exam & Passed ML20211E9191999-08-24024 August 1999 Forwards fitness-for-duty Program Performance Data for Jan-June 1999 for PBAPS & LGS IAW 10CFR26.71(d).Data Includes Listed Info ML20211E9731999-08-23023 August 1999 Forwards LGS Unit 2 Summary Rept for 970228 to 990525 Periodic ISI Rept Number 5, Per TS SRs 4.0.5 & 10CFR50.55a(g) ML20211D6761999-08-20020 August 1999 Forwards non-proprietary Revised Emergency Response Procedures (Erps),Including Rev 29 to ERP-110, Emergency Notification & Rev 17 to ERP-800, Maint Team & Proprietary App ERP-110-1.App Withheld Per 10CFR2.790(a)(6) ML20210T4271999-08-13013 August 1999 Informs That NRC Revised Info in Rvid & Releasing Rvid Version 2 as Result of Review of 980830 Responses to GL 92-01 Rev 1,GL 92-01 Rev 1 Suppl 1 & Suppl Rai.Tacs MA1197 & MA1198 Closed ML20210U2211999-08-10010 August 1999 Forwards Insp Repts 50-352/99-04 & 50-353/99-04 on 990525-0712.One Violation Occurred & Being Treated as NCV, Consistent with App C of Enforcement Policy.Violation Re Late Performance of off-gas Grab Sample Surveillance 05000353/LER-1999-005, Forwards LER 99-005-00,re Actuation of Primary Containment & Reactor Vessel Isolation Control Sys,Esf.Fuse Failed Due to Mechanical Failure of Cold Solder Joint1999-08-10010 August 1999 Forwards LER 99-005-00,re Actuation of Primary Containment & Reactor Vessel Isolation Control Sys,Esf.Fuse Failed Due to Mechanical Failure of Cold Solder Joint ML20211B7881999-08-10010 August 1999 Transmits Summary of Two Meetings with Risk-Informed TS Task Force in Rockville,Md on 990514 & 0714 ML20210M7571999-08-0404 August 1999 Forwards Response to Requesting Addl Info Re Status of Decommissioning Funding for Lgs,Pbaps & Sngs. Attachment Provides Restatement of Questions Followed by Response ML20210P4191999-08-0404 August 1999 Forwards Initial Exam Repts 50-352/99-302 & 50-353/99-302 on 990702-04 (Administration) & 990715-22 (Grading).Six of Limited SRO Applicants Passed All Portion of Exam NUREG-1092, Informs J Armstrong of Individual Exam Results for Applicants on Initial Exam Conducted on 990702 & 990712-14 at Facility.All Six Individuals Who Were Administered Exam, Passed Exam.Without Encls1999-08-0303 August 1999 Informs J Armstrong of Individual Exam Results for Applicants on Initial Exam Conducted on 990702 & 990712-14 at Facility.All Six Individuals Who Were Administered Exam, Passed Exam.Without Encls ML20210L2011999-07-28028 July 1999 Forwards Final Personal Qualification Statement (NRC Form 398) for Reactor Operator License Candidate LB Mchugh ML20211F2641999-07-27027 July 1999 Forwards Three Copies of Rev 12 to LGS Physical Security Plan, Rev 4 to LGS Training & Qualification Plan & Rev 2 to LGS Safeguards Contingency Plan. Without Encls 05000352/LER-1999-008, Forwards LER 99-008-00 Re 990623 Failure of Plant HPCI Sys to Start Due to Failure of HPCI Turbine,Hydraulic Actuator1999-07-23023 July 1999 Forwards LER 99-008-00 Re 990623 Failure of Plant HPCI Sys to Start Due to Failure of HPCI Turbine,Hydraulic Actuator 05000353/LER-1999-004, Forwards LER 99-004-00 Re 990701 Discovery of Pressure Setpoint Drift of Thirteen Mss SRV Due to Corrosion Induced Bonding within SRVs1999-07-23023 July 1999 Forwards LER 99-004-00 Re 990701 Discovery of Pressure Setpoint Drift of Thirteen Mss SRV Due to Corrosion Induced Bonding within SRVs ML20210E6211999-07-22022 July 1999 Submits Rev to non-limiting Licensing Basis LOCA Peak Clad Temps (Pcts) for Limerick Generating Station (Lgs),Units 1 & 2 & Pbaps,Units 2 & 3 ML20216D3081999-07-19019 July 1999 Requests Renewal of OLs for Listed Individuals,Iaw 10CFR55.57.NRC Forms 398 & 396,encl for Applicants.Without Encl ML20216D8041999-07-19019 July 1999 Submits Summary of Final PECO Nuclear Actions Taken to Resolve Scram Solenoid Pilot Valve Issues Identified in Info Notice 96-007 05000352/LER-1999-006, Forwards LER 99-006-00 Re 990614 Discovery That Grab Sample of Plant Offgas Sys Was Not Obtained within Time Limit Required by TS 3.3.7.12,Action 110 Due to Personnel Error1999-07-12012 July 1999 Forwards LER 99-006-00 Re 990614 Discovery That Grab Sample of Plant Offgas Sys Was Not Obtained within Time Limit Required by TS 3.3.7.12,Action 110 Due to Personnel Error ML20209F6341999-07-0909 July 1999 Submits Supplemental Response to GL 94-03, Intergranular Stress Corrosion Cracking of Core Shrouds in Bwrs, for Unit 2.Rev 0 to 1H61R & GE-NE-B13-02010-33NP Repts & Revised Pages to Summary Rept Previously Submitted,Encl ML20209G9121999-07-0909 July 1999 Informs That Ja Hutton Has Been Appointed Director,Licensing for PECO Nuclear,Effective 990715.Previous Correspondence Addressed to Gd Edwards Should Now Be Sent to Ja Hutton ML20209C9041999-07-0808 July 1999 Forwards Monthly Operating Repts for June 1999 for Limerick Generating Station,Units 1 & 2 & Revised Monthly Repts for May 1999 ML20210B4441999-07-0808 July 1999 Forwards Preliminary NRC Form 398 & NRC Form 396 for Reactor Operator for License Candidate LB Mchugh.Candidate Failed Category B Portion of Operating Exam Given at LGS During Week of 990315.Tentative re-exam Has Been Scheduled 990812 05000353/LER-1999-003, Forwards LER 99-003-00,re Bypass of RW Cleanup Leak Detection Sys Isolation Function on Three Separate Occasions.Bypass of Safety Function Was Caused by Inadequate Review & Approval of Change to Procedure1999-07-0707 July 1999 Forwards LER 99-003-00,re Bypass of RW Cleanup Leak Detection Sys Isolation Function on Three Separate Occasions.Bypass of Safety Function Was Caused by Inadequate Review & Approval of Change to Procedure ML20209D8821999-07-0707 July 1999 Submits Estimate of Number of Licensing Actions Expected to Be Submitted in Years 2000 & 2001,as Requested by Administrative Ltr 99-02.Renewal Applications for PBAPS, Units 2 & 3,will Be Submitted in Second Half of 2001 ML20209D2671999-07-0202 July 1999 Responds to NRC 990322 & 0420 RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20196J6301999-07-0101 July 1999 Requests Addl Info Re Status of Decommissioning Funding for Limerick Generating Station,Units 1 & 2,Peach Bottom Atomic Power Station,Units 1,2 & 3 & Salem Nuclear Generating Station,Units 1 & 2 05000352/LER-1999-004, Forwards LER 99-004-00,re Inoperability of Automatic Depressurization Sys Portion of Eccs.Condition Resulted from Incomplete Impact Review of Isolating Portion of ADS Nitrogen Backup Supply on Operability of ECCS Sys1999-07-0101 July 1999 Forwards LER 99-004-00,re Inoperability of Automatic Depressurization Sys Portion of Eccs.Condition Resulted from Incomplete Impact Review of Isolating Portion of ADS Nitrogen Backup Supply on Operability of ECCS Sys ML20209B7001999-06-30030 June 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20212J5401999-06-28028 June 1999 Discusses Completion of Licensing Action for NRC Bulletin 96-003, Potential Plugging of ECC Suction Strainers by Debris in Bwrs. Bulletin Closed for Unit 2 by NRC ML20207H8271999-06-24024 June 1999 Informs NRC That Util Has Completed Core Shroud Insps for LGS Unit 2.Proprietary Rept GE-NE-B13-02010-33P & non-proprietary Rev 0 to 1H61R,encl.Proprietary Rept Withheld,Per 10CFR2.790(a)(4) ML20196G7041999-06-24024 June 1999 Forwards Insp Repts 50-352/99-03 & 50-353/99-03 on 990413- 0524.No Violations Noted.Nrc Concluded That Licensee Staff Continued to Operate Both Units Safely ML20196A5641999-06-15015 June 1999 Provides Info Re Util Use of Four Previously Irradiated LGS, Unit 1,GE11 Assemblies in Unit 2 Cycle 6.Encl 990518 GE Ltr Provides Objective of Lead Use Assemblies Program & Outlines Kinds of Measurements That Will Be Made on Assemblies ML20195J6831999-06-11011 June 1999 Provides Proprietary Objectives for Lgs,Units 1 & 2,1999 Emergency Preparedness Exercise Scheduled to Be Conducted on 990914.Licensee Identifies Which Individuals Should Receive Copies of Info.Proprietary Info Withheld 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217D5211999-09-30030 September 1999 Informs That Remediating 3D Monicore Sys at Pbaps,Units 2 & 3 & 3D Monicore/Plant Monitoring Sys at Lgs,Unit 2 Has Been Completed Ahead of Schedule ML20216J3981999-09-29029 September 1999 Submits Comments for Lgs,Unit 1 & Pbaps,Units 2 & 3 Rvid,Rev 2,based on Review as Requested in GL 92-01,rev 1,suppl 1, Reactor Vessel Structural Integrity ML20212H6401999-09-24024 September 1999 Forwards Revised Epips,Including Rev 11 to ERP-101 & Rev 18 to ERP-800.Copy of Computer Generated Rept Index Identifying Latest Revs of LGS Erps,Encl ML20212E7941999-09-22022 September 1999 Requests Authorization for Listed Licensed Operators to Temporarily Suspend Participation in Licensed Operator Requalification Program at LGS ML20212E8081999-09-22022 September 1999 Provides Notification That Listed Operators Have Been Permanently Reassigned to Duties That Do Not Require Maintaining Licensed Operator Status,Per 10CFR50.74 ML20212F5481999-09-20020 September 1999 Forwards Response to NRC Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing, for Pbaps,Units 2 & 3 & Lgs,Units 1 & 2 ML20212F8991999-09-17017 September 1999 Provides Written Confirmation That Thermo-Lag 330-1 Fire Barrier Corrective Actions at Lgs,Units 1 & 2 Have Been Completed 05000353/LER-1999-010, Forwards LER 99-010-00,re Manual Actuation of Esf.Main CR Ventilation Sys Was Placed in Chlorine Isolation Mode Due to Rept of Faint Odor of Chlorine in Unit 2 Reactor Encl1999-09-16016 September 1999 Forwards LER 99-010-00,re Manual Actuation of Esf.Main CR Ventilation Sys Was Placed in Chlorine Isolation Mode Due to Rept of Faint Odor of Chlorine in Unit 2 Reactor Encl ML20212A0091999-09-0909 September 1999 Provides Notification That Licenses SOP-11172 & SOP-11321, for SO Muntzenberger & Rh Wright,Respectively,Are No Longer Necessary as Result of Permanent Reassignment 05000352/LER-1999-009, Forwards LER 99-009-00,providing 30-day Written follow-up Rept Re Performance of Maint That Affected Safeguard Sys for Which Compensatory Measures Had Not Been Employed1999-09-0101 September 1999 Forwards LER 99-009-00,providing 30-day Written follow-up Rept Re Performance of Maint That Affected Safeguard Sys for Which Compensatory Measures Had Not Been Employed ML20211E9191999-08-24024 August 1999 Forwards fitness-for-duty Program Performance Data for Jan-June 1999 for PBAPS & LGS IAW 10CFR26.71(d).Data Includes Listed Info ML20211E9731999-08-23023 August 1999 Forwards LGS Unit 2 Summary Rept for 970228 to 990525 Periodic ISI Rept Number 5, Per TS SRs 4.0.5 & 10CFR50.55a(g) ML20211D6761999-08-20020 August 1999 Forwards non-proprietary Revised Emergency Response Procedures (Erps),Including Rev 29 to ERP-110, Emergency Notification & Rev 17 to ERP-800, Maint Team & Proprietary App ERP-110-1.App Withheld Per 10CFR2.790(a)(6) 05000353/LER-1999-005, Forwards LER 99-005-00,re Actuation of Primary Containment & Reactor Vessel Isolation Control Sys,Esf.Fuse Failed Due to Mechanical Failure of Cold Solder Joint1999-08-10010 August 1999 Forwards LER 99-005-00,re Actuation of Primary Containment & Reactor Vessel Isolation Control Sys,Esf.Fuse Failed Due to Mechanical Failure of Cold Solder Joint ML20210M7571999-08-0404 August 1999 Forwards Response to Requesting Addl Info Re Status of Decommissioning Funding for Lgs,Pbaps & Sngs. Attachment Provides Restatement of Questions Followed by Response ML20210L2011999-07-28028 July 1999 Forwards Final Personal Qualification Statement (NRC Form 398) for Reactor Operator License Candidate LB Mchugh ML20211F2641999-07-27027 July 1999 Forwards Three Copies of Rev 12 to LGS Physical Security Plan, Rev 4 to LGS Training & Qualification Plan & Rev 2 to LGS Safeguards Contingency Plan. Without Encls 05000352/LER-1999-008, Forwards LER 99-008-00 Re 990623 Failure of Plant HPCI Sys to Start Due to Failure of HPCI Turbine,Hydraulic Actuator1999-07-23023 July 1999 Forwards LER 99-008-00 Re 990623 Failure of Plant HPCI Sys to Start Due to Failure of HPCI Turbine,Hydraulic Actuator 05000353/LER-1999-004, Forwards LER 99-004-00 Re 990701 Discovery of Pressure Setpoint Drift of Thirteen Mss SRV Due to Corrosion Induced Bonding within SRVs1999-07-23023 July 1999 Forwards LER 99-004-00 Re 990701 Discovery of Pressure Setpoint Drift of Thirteen Mss SRV Due to Corrosion Induced Bonding within SRVs ML20210E6211999-07-22022 July 1999 Submits Rev to non-limiting Licensing Basis LOCA Peak Clad Temps (Pcts) for Limerick Generating Station (Lgs),Units 1 & 2 & Pbaps,Units 2 & 3 ML20216D3081999-07-19019 July 1999 Requests Renewal of OLs for Listed Individuals,Iaw 10CFR55.57.NRC Forms 398 & 396,encl for Applicants.Without Encl ML20216D8041999-07-19019 July 1999 Submits Summary of Final PECO Nuclear Actions Taken to Resolve Scram Solenoid Pilot Valve Issues Identified in Info Notice 96-007 05000352/LER-1999-006, Forwards LER 99-006-00 Re 990614 Discovery That Grab Sample of Plant Offgas Sys Was Not Obtained within Time Limit Required by TS 3.3.7.12,Action 110 Due to Personnel Error1999-07-12012 July 1999 Forwards LER 99-006-00 Re 990614 Discovery That Grab Sample of Plant Offgas Sys Was Not Obtained within Time Limit Required by TS 3.3.7.12,Action 110 Due to Personnel Error ML20209F6341999-07-0909 July 1999 Submits Supplemental Response to GL 94-03, Intergranular Stress Corrosion Cracking of Core Shrouds in Bwrs, for Unit 2.Rev 0 to 1H61R & GE-NE-B13-02010-33NP Repts & Revised Pages to Summary Rept Previously Submitted,Encl ML20209G9121999-07-0909 July 1999 Informs That Ja Hutton Has Been Appointed Director,Licensing for PECO Nuclear,Effective 990715.Previous Correspondence Addressed to Gd Edwards Should Now Be Sent to Ja Hutton ML20210B4441999-07-0808 July 1999 Forwards Preliminary NRC Form 398 & NRC Form 396 for Reactor Operator for License Candidate LB Mchugh.Candidate Failed Category B Portion of Operating Exam Given at LGS During Week of 990315.Tentative re-exam Has Been Scheduled 990812 ML20209C9041999-07-0808 July 1999 Forwards Monthly Operating Repts for June 1999 for Limerick Generating Station,Units 1 & 2 & Revised Monthly Repts for May 1999 05000353/LER-1999-003, Forwards LER 99-003-00,re Bypass of RW Cleanup Leak Detection Sys Isolation Function on Three Separate Occasions.Bypass of Safety Function Was Caused by Inadequate Review & Approval of Change to Procedure1999-07-0707 July 1999 Forwards LER 99-003-00,re Bypass of RW Cleanup Leak Detection Sys Isolation Function on Three Separate Occasions.Bypass of Safety Function Was Caused by Inadequate Review & Approval of Change to Procedure ML20209D8821999-07-0707 July 1999 Submits Estimate of Number of Licensing Actions Expected to Be Submitted in Years 2000 & 2001,as Requested by Administrative Ltr 99-02.Renewal Applications for PBAPS, Units 2 & 3,will Be Submitted in Second Half of 2001 ML20209D2671999-07-0202 July 1999 Responds to NRC 990322 & 0420 RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves 05000352/LER-1999-004, Forwards LER 99-004-00,re Inoperability of Automatic Depressurization Sys Portion of Eccs.Condition Resulted from Incomplete Impact Review of Isolating Portion of ADS Nitrogen Backup Supply on Operability of ECCS Sys1999-07-0101 July 1999 Forwards LER 99-004-00,re Inoperability of Automatic Depressurization Sys Portion of Eccs.Condition Resulted from Incomplete Impact Review of Isolating Portion of ADS Nitrogen Backup Supply on Operability of ECCS Sys ML20209B7001999-06-30030 June 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20207H8271999-06-24024 June 1999 Informs NRC That Util Has Completed Core Shroud Insps for LGS Unit 2.Proprietary Rept GE-NE-B13-02010-33P & non-proprietary Rev 0 to 1H61R,encl.Proprietary Rept Withheld,Per 10CFR2.790(a)(4) ML20196A5641999-06-15015 June 1999 Provides Info Re Util Use of Four Previously Irradiated LGS, Unit 1,GE11 Assemblies in Unit 2 Cycle 6.Encl 990518 GE Ltr Provides Objective of Lead Use Assemblies Program & Outlines Kinds of Measurements That Will Be Made on Assemblies ML20195J6831999-06-11011 June 1999 Provides Proprietary Objectives for Lgs,Units 1 & 2,1999 Emergency Preparedness Exercise Scheduled to Be Conducted on 990914.Licensee Identifies Which Individuals Should Receive Copies of Info.Proprietary Info Withheld ML20195G4591999-06-10010 June 1999 Forwards MORs for May 1999 & Revised Repts for Apr 1999 for LGS Units 1 & 2 ML20195H0531999-06-0909 June 1999 Forwards Revised Bases Pages B3/4 10-2 & B3/4 2-4 for LGS Units 1 & 2,in Order to Clarify That Requirements for Reactor Enclosure Secondary Containment Apply to Extended Area Encompassing Both Reactor Enclosure & Refueling Area ML20195E7701999-06-0707 June 1999 Provides Notification of Change to NPDES Permit PA0052221, for Bradshaw Reservoir Facility Which Supports Operation of Lgs,Units 1 & 2,per EPP Section 3.2 ML20195C7631999-06-0101 June 1999 Notifies NRC That PECO Energy Has Completed Installation of New Large Capacity,Passive Strainers on RHR & Core Spray Sys Pump Suction Lines at Lgs,Unit 2,in Response to Ieb 96-003 ML20195D5381999-05-26026 May 1999 Forwards 1998 Occupational Exposure Tabulation Rept for LGS Units 1 & 2. Encl Is Diskette & Instructions.Rept Is Being re-submitted to Reset 12 Month Time Period.Without Disk ML20195B2821999-05-24024 May 1999 Requests That NRC Distribution Lists for LGS Be Updated. Marked-up Distribution List Showing Changes Is Attached ML20196L2891999-05-20020 May 1999 Provides Status Update of Thermo-Lag 330-1 Fire Barrier Corrective Actions,Iaw Commitments Made in ML20195B2951999-05-20020 May 1999 Forwards Rev 0 to LGS Unit 2 Reload 5,Cycle 6 COLR, IAW TS Section 6.9.1.12.Values Listed Have Been Determined Using NRC-approved Methodology & Are Established Such That All Applicable Limits of Plants Safety Analysis Are Met 05000352/LER-1999-003, Forwards LER 99-003-00,re Rps,Pcrvics Actuations.Ler Contains Special Rept Info for HPCI & Reactor Core Isolation Cooling Sys Injections Into Rv1999-05-19019 May 1999 Forwards LER 99-003-00,re Rps,Pcrvics Actuations.Ler Contains Special Rept Info for HPCI & Reactor Core Isolation Cooling Sys Injections Into Rv 05000353/LER-1999-002, Forwards LER 99-002-00,automatic Actuations of Primary Containment & Reactor Vessel Isolation Control Sys & Other Common Plant ESF Due to Loss of Power to a Rps/Ups Power Distribution Panel on 9904191999-05-18018 May 1999 Forwards LER 99-002-00,automatic Actuations of Primary Containment & Reactor Vessel Isolation Control Sys & Other Common Plant ESF Due to Loss of Power to a Rps/Ups Power Distribution Panel on 990419 ML20206E2001999-04-28028 April 1999 Forwards 1998 Annual Environ Operating Rept (Non- Radiological) for Limerick Generating Station,Units 1 & 2. Rept Submitted IAW Section 5.4.1 of App B of Fols,Epp (Non- Radiological) & Describes Implementation of EPP for 1998 ML20206D8801999-04-27027 April 1999 Forwards Rev 2 to LGS Unit 1 Reload 7,Cycle 8 COLR, IAW TS Section 6.9.1.12.COLR Provides cycle-specific Parameter Limits for Noted Info ML20206A5461999-04-21021 April 1999 Responds to Conference Call Between Util & NRC on 990420,re TS Change Request 98-07-2,revising TS Section 2.0 to Incorporate Revised MCPR Safety Limits.Attached Ltr Contains Info Requested ML20205T0441999-04-17017 April 1999 Forwards 1998 Annual Radiological Environ Operating Rept 15, IAW TS Section 6.9.1.7.REMP for 1998,confirmed That LGS Environ Effects from Radioactive Release Were Well Below LGS TSs & Other Applicable Regulatory Limits ML20205Q7581999-04-15015 April 1999 Forwards Response to RAI Re ISI Program First & Second 10-Yr Interval Relief Requests.Revs to Identified by Vertical Bar in Right Margin 1999-09-09
[Table view] |
Text
n 10 CPR 2.201
. , PIIILADELPHIA ELECTRIC COMPANY LIMERICK GENERATING STATION P. O. BOX 2300 POITS1GVN, PA 19464-0920 (215) 3271200, EXT. 3000 February 12, 1992 uwen$$c78((swxw Docket Nos. 50-352 50-353 License Nos. NPP-39 NPF-85 U.S. Nuclear Regulatory Commission Attn Document Control Desk Washington, DC 20555
SUBJECT:
Limerick Generating Station, Units 1 and 2 Reply to a Notice of Violation NRC Inspection Report Nos. 50-352/91-22 and 50-353/91-23 Attached is Philadelphia Electric Company's reply to a Notice of Violation for Limerick Generating Station (LGS) Units 1 and 2, which was
-contained in the NRC Inspection Report Nos. 50-352/91-22 and 50-353/91-23 dated December 27, 1991 and received on January 8, 1992.
The Notice of Violation identifies an event involving failure to maintain control of surveillance testing. The violation concerns the failure to.promptly identify and declare the 'A' Emergency Service Water subsystem inoperable following an unsatisfactory survell3ance test.
The attachment to this letter provides a restatement of the violation identified during an NRC inspection conducted between October 6, 1991,
.through November 16,-1991, at LGS, Units 1 and 2, followed by our response.
An extension of-five days to the prescribed response time was requested of T J. Kenny and granted to verify the effectiveness of these corrective cctions.
'If you have any questions or require additional information, please contact us.
Very truly yours, 7s 1
KOS:cah-Attachment cc: T. T. Martin, Administrator, Region I, USNRC T. J. Kenny, USNRC Senior Resident Inspector, LGS 9202210305 920212 PDR ADOCK 05000352 G PDR f g6(t_
lll
e' 4
.bec t. D. M. Smith -
52C-7 J.iDoering, Jr..- ADMS-1 D.:R.-Helwig 63C J . .- W. - Du rham -
S26-1 G. A. Hunger, Jr. - SMB1-1 R. E Boyce -
ADMS-1 L.-A. Hopkins .
ADMS-1
-J. A.-Muntz -
-ADM5-1 l ISEG Supt. -
SMB3-2 G.-J. Madsen -
SSB3-4
-J. P. O'Rourke -
SSB4-3 R. N. Charles -
51A-1 G. J. Beck,'Jr., - 52A-5 Secretary, NCB -
SIA-13 Correspondence Release Point - SMB1-2 DCC PA DER.BRP Inspector - SMB2-2 ,
t 4
f 4
I L . _ , . - . . . . ~ . . , _ . _ , . _ . , . - , _ . . _ _ _ . . ~ _ . - - . , , _ . , - - . _ _ _ _ _ _ _ . . _ - _ . . - _ _
' Attachment
. Page'l of 7
. Inspection Report Nos. 50-352/91-22
. -1 50-353/91-23 Reply to a Notice of Violation Restatement of the Violation As a result of an inspection conducted from October 6 to November 16, 1991, and in accordance with NRC Enforcement Policy (10 CPR 2,
-Appendix C), the following examples of a violation of Plant Technical Specification Administrative Controls were identified.
These failures to follow procedures resulted in-a failure to formally declare a test unsatisfactory and the subsystem inoperable.
Plant Technical Specification 6.8.1 requires, in part, that written procedures shall be established and implemented.
- 1. Administrative Procedure A-26 " Procedure for Plant Maintenance Using the Maintenance Request Form," paragraph 5.1, states that all personnel are responsible for the p;ompt identification and documentation of conditions adverse to plant safety, such as failure or malfunctions. This process is performed by the initiation of a Maintenance Request Form.
Contrary to>the-above on-October 25, 1991, during the performance of Surveillance Test ST-6-Oll-231-0 "A Loop ESW Pump Valve and' Flow Test," an operator identified the failure .
of check valve 11-0063; but, failed to document the malfunction with the initiation of a Maintenance Request Form.
- 2. Surveillance Test ST-6-011-231-0 " Loop ESW Pump Valve and-Plow Test," step "B" of the test results page states that, when the test is considered.a failure immediately notify the senior plant staff member.-
Contrary to the above on October 25, 1991, the senior plant staff member was not notified of the event'until the following day and the procedure portion marked "date/ time notified" was not completed until October 28, 1991.
The above examples of failure to implement administrative controls over pump and valve surveillance testing are collectively a Severity level IV violation (Supplement l).
RESPONSE
Admission of Violation Philadelphia Electric Company (PECo) acknowledges the violation.
~l Attachment 1 Page'2 of 7- ,
. Inspection Report Noa. 50-352/91-22 50-353/91 '
Background
On October 25,'1991, during the afternoon snift, Surveillance Test (ST) procedure ST-6-Oll-231-0, "A Loop Emergency Service Water Pump, Valve, and Flow Test," was being performed for its normally scheduled quarterly performance by a non-licensed operator. This .
ST procedure contains an Inservice Inspection (I) step (i.e., step 4 6.4.40) that verifies-proper operation of the safety related Emergency Service Water (ESW) system check valve, 11-0063. This check valve provides one isolation point between the non-safety related Service Water'(SW) system and the ESW system. This check valve is one of the components relied upon to ensure ESW system piping integrity under accident conditions and allows the SW system to supply cooling water to the Unit 2 Reactor Core Isolation ,
Cooling (RCIC) system room coolers during normal operating conditions (See Figure 1).
The purpose of ST procedure step 6,4.40 la to ensure that valve 11-0063 checks flow by verifying that no pressurized flow exists from the ESH system line to the SW system line. Proper operation of the check valve is verified by opening drain valve 11-2075 and observing no pressurized water flow with valve 11-2013 closed (See Figure 1). The non-licensed operator properly performed this ST t procedure step; however, he observed that pressurized flow did exist from the drain valve. The licenned operations Floor Supervisor was immediately made aware of this condition by the non-licensed operator as required by the ST procedure. The non-licensed operator was then instructed by the operations Ploor Supervisor to place a note in the ST procedure identifying this discrepancy in accordance with the procedure. A note was placed in the ST procedure stating that, " pressurized flow exists from valve 11-2075 as it did the~1ast time the ST was performed." The non-licensed operator's note was referring to the last time he had performed the ST procedure in May 1991, at which time the check valve was replaced in kind. The non-licensed operator then informed the Main Control Room (MCR) Chief Operator (CO), a licensed operator, that the drain valve had pressurized flow. The non-licensed operator completed the ST procedure and returned it to the MCR CO. The MCR CO signed the ST procedure as unsatisfactory a at 2310 hours0.0267 days <br />0.642 hours <br />0.00382 weeks <br />8.78955e-4 months <br /> and left the Independent Verification of Restoration (IVOR) section of the ST procedure to be completed by the licensed MCR CO on midnight shift.
Early on October 26, 1991, during the midnight shift, the MCR CO had the IVOR section of-the ST procedure completed, and gave the failed ST procedure to the licensed MCR Shift Supervisor for review. The licensed MCR-Shift Supervisor reviewed the ST '
procedure and then_ discussed the results with the licensed MCR
! Shift Manager and non-Licensed Shift Technical Advisor (STA).- They I
could not be certain whether the check valve had failed or the SW-system manual isolation valve 11-2013-was leaking. As.a result of the non-licensed operator's note, the MCR Shift Manager, MCR Shift Supervisor, and STA assumed that corrective actions and an
. Attachment Page 3 of 7
. Inspection Report Nos. 50-352/91-22 50-353/91-23 operability determination had previ,usly been addressed. However, the MCR peraonnel did not verify that adequate corrective actions had been initiated. They also discussed that the failed ST procedure step was an (I) step, not an asterisk (*) step. An asteriak step in a procedure dentees action required to maintain Technical Specifications (TS) requ2rements. Therefore, MCR personnel determined that tnere was no insediate operability concern.
The Shift Manager reported the failed ST procedure to the on duty Senior Plant Staf f men.ber , on the morning of October 26, 1991.
However, the ST procedure was not signed off by the Senior Plant Staff member at that time because questions arose regarding a separate plant issue which required immediate attention. The failed ST procedure was set aside for further review by the Senior Plant Staff Member to occur on Monday, October 28, 1991. On October 28, 1991, at 0830 hours0.00961 days <br />0.231 hours <br />0.00137 weeks <br />3.15815e-4 months <br />, the ST procedure was signed off unsatisfactory by the Senior Plant Staff member. On October 29, 1991, during routine review of the failed ST procedure, a technical staff member determined that, since the 11-0063 valve serves as a boundary between the ESW and SW syt.tems, reverse leakage through the valve would render the 'A' Loop of the ESW system inoperable.
Based on this determination, the technical staff member immediately notified the licensed MCR Shift Supervisor. At 1430 hours0.0166 days <br />0.397 hours <br />0.00236 weeks <br />5.44115e-4 months <br />, further troubleshooting was performed and the system engineer verified that the leakage through the 11-0063 check valve was above the Inservice Testing (IST) program limit of 10 gpm. Following the troubleshooting, operations personnel closed manual valve 11-2070 at 1600 hours0.0185 days <br />0.444 hours <br />0.00265 weeks <br />6.088e-4 months <br /> and isolated the SW to ESW system interface (See Figure 1). This restored the 'A' Loop of the ESW system and associated equipment to an operable status, meer Reason for the Violation The causes of the failure to document the malfunction of check valve 11-0063 with the initiation of a Maintenanc Request Form (MRF) were personnel errors where operations personnel failed to follow procedures. This event identified several weaknesses in the surveillance test program as contributing causal factors.
The initiation of prompt corrective actions was identified as a weakness during this event. MCR personnel failed to review the equipment history of the system check valve and assumed that the condition was previously identified. Consequently, no Equipment Trouble Tag (ETT) was initiated to document this deficient condition.
The licensed operators and senior licensed operators did not have an appreciation for the significance of surveillance test criteria designated as (I). Furthermore, the understanding of this criteria was not viewed with the same priority in terms of system
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.- Attachment Page 4 of 7
. ' Inspection Report Nos. 50-352/91-22 50-353/91-23 operability /as: criteria that meet specific TS requirements, designated by an-asterisk (*). This condition was' attributed to less than adequate training associated with the IST program.
The reporting of surveillance test failures-to the on duty Senior Plant Staff member was found to be deficient. The test-failure identified by this violation was reported to the on duty Senior Plant' Staff member on the following morning. Because the staff member' failed to sign the test after being distracted by nontelated plant events, the test was_placed in a bin for signature on Monday morning. A review of station administrative controls identified.a weakness in-the definition of what constitutes an immediate notification for test failures and the expectations of on duty Senior Plant Staff members with regard to test failures. The process-of notifying or. duty Senior Plant Staff members is a-final barrier for assuring that proper considerations have been given to 1
establishing operability determinations and initiation of appropriate corrective actions.
Corrective Action and Results Achieved A Maintenance Request Porm was written on October 29, 1991, and the ESW system check valve 11-0063, was repaired on November 19, 1991.
Corrective Actions Taken to Avoid Future Non-Compliance The following corrective actions were developed in response to two y separate incidents involving failures _to initiate corrective actions. The other event occurred in September, 1991 and involved the_RHRSW system. The corrective actions described below were taken.in response to both events and began'on October 30, 1991.
These have been reported in our response to NRC violation 50-352/91-18-01, 50-353/91-19-01 dated December 9, 1991, with the !
exception of the corrective actions concerning (I) steps, which are specific to this ESW system event.
o- In immediate response to this event, on October 30, 1991, operations personnel were informed of the event via Shift Night Orders and a recorded phone message. emphasizing the importance of promptly initiating corrective actions. The requirement to promptly. determine component operability if an (I) step fails was also' stressed.
o On November 4, 1991, a letter from the Plant Manager to all
-licensed Senior Reactor Operator operations personnel was issued 1 reiterating management's expectations of initial response-to equipment malfunctions. This letter stated that 1) equipment deficiencies must immediately be captured in the corrective action process which assures that an appropriate
L Attachment l Page 5 of 7 e Inupection Report Nos. 50-352/91-22 50-353/91-23 ;
response-is taken, 2) notations concerning equipment problems- :
on ST procedures are_not' adequate corrective actions, 3) failed (I) steps require that an immediate operability determination i
be made, and 4) when equipment included in the TS is concidered operable while an operability determination is in process, the operations organization is responsible to assure that the evaluation is done as quickly as possible. This information -
was discussed at an operations shift supervision meeting on November 5, 1991 and during licensed operator requalification training. A second letter was issued by the Plant Manager to all Senior Plant Staff members reminding them to take a critical, objective view when evaluating tailed surveillance tests, o On November 4,-1991, a Por Your Information (PYI) notice was developed and distributed to first line supervision. This PY1 '
notice provided a clear and concise set of written management expectations regarding the immediate corrective actions '
required to be promptly implemented upon discovery of deficient plant equipment. First line supervision then disseminated the expectations of management in this PYI to appropriate station personnel to-heighten their awareness of the requirements and management's expectations.
o On December 1,-1991, Limerick Generating Station implemented the' Plant Information Management System (PIMS). - This system ensures that an ETT that is generated for an equipment problem results in a computerized Action Request. The Action Request !
must be evaluated by the responsible organization and, if necessary, a Work Order is generated. This ensures tracking of problem investigation even before sufficient information is available to generate a specific work order, o On January 30, 1992, operations management clarified the immediate reporting requirements for failed surveillance tests in that on duty Senior Plant Staff members are to be notified within nominal eight hours of test failure. Management
-re-emphasized the need to clearly document unacceptable-surveillance test data. This information has been communicated to all~ licensed and non-licensed operators as well as. Senior Plant Staff. '
o On February 6, 1992, due to a concern with the proper operation of a-motor operated valve, operations management reaffirmed the need to_ initiate prompt corrective actions (e.g., issue an ETT) for any equipment problems that are encountered. This information was issued for all licensed and non-licensed operators to read and sign.
o Licensed operator initial and requalification training will be revised to incorporate training relevant to implementation of the IS? program requirements through ST procedures. This is expected. to be completed-by March 31, 1992.
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Attachment ..
Page 6 of 7 l Inspection Report Nos. 50-352/91-22 50-353/91-23 o TOperations Manual: Chapter 6.1, " Operations Surveillance Testl
' Guidelines," will be revised _by February 28, 1992._ This-revision will provide guidance to Shift Management for issuing i notifications to Senior Plant Staff members on-call.regarding- ,
, surveillance test failures. This guidance will include a definition of what constitutes an immediate notification for test failures. ;
o Administrative Guideline AG-41, " Staff Duty Stander," will be revised by February 28, 1992 to include management's expectation to ensure immediate-operability determinations !
following the failure of (I) steps and to ensure corrective action measures are initiated, o Administrative-procedure, A-26, " Procedure for Plant Maintenance Using the Maintenance Request Form," has been reviewed, along with operations personnel training on'A-26, and both the procedure and the training were determined to be-adequate.
Date When Full Compliance was Achieved [
Full compliance was achieved on October 29, 1991, when a MRF was ,
written on valve 11-0063; the valve was repaired and declared operable on November 19,-1991.
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AttGehment
. Page 7 of 7
. Inspection Report hos. 50-352/91-22 50-353/91-23 I
B3ure 1 I
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