ML20092A751

From kanterella
Jump to navigation Jump to search
Forwards Response to NRC Re Violations Noted in Insp Repts 50-352/95-10 & 50-353/95-10 on 950523-0718. Corrective Actions:Increased Surveillance of Tools at Tool Rooms
ML20092A751
Person / Time
Site: Limerick  Constellation icon.png
Issue date: 09/05/1995
From: Walter MacFarland
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9509110179
Download: ML20092A751 (5)


Text

_

s-1 Walter G. MacFarland,1U, P.E.

Voe Pre *.&nt A

LimerKk Generatng Statw;n

=

PECO ENERGY erco - c -

PO Bom 2300 Sanataja. PA 19464 o920 61o 718 3000 Fax 61o 718 3008 Per 1800 352 4732 *8320 to CFR 2.201 September 5,1995 Docket Nos. 50-352 50-353 License Nos. NPF-39 NPF-85 U.S. Nuclear Regulatory Commissbn Attn: Document Control Desk Washington, DC 20555

SUBJECT:

Limerick Generating Station, Units 1 and 2 Reply to a Notice of Violation NRC Combined Inspection Report Nos. 50-352/9510 and 50-353/95-10 Attached is the PECO Energy Company reply to a Notice of Violation for Limerick Generating Station, Units 1 and 2, that was contained in your letter dated August 7,1995. The violation concerned contamination monitoring of personnel and materials leaving the radiological controlled area. The attachment to this letter provides a restatement of the violation followed by our reply.

If you have any questions or require additional information, please contact us.

Very truly yours,

[

l r

G.jh ( &

3w J

i GHS Attachment cc:

T. T. Martin, Administrator, Region I, USNRC w/ attachment N. S. Perry, USNRC Senior Resident inspector, LGS I

lfr,h

"*n lLUd.

79 950905 I l

[hjCK05o00352 PD D

PDR

Attachment Docket N6s. 50-352 and 50-353 September 5,1995 Page 1 of 4 Benly to a Notice of Violation B931steInanLof the Violation During an NRC inspection conducted on May 23-July 18,1995, a violation of NRC requirements was identified. In accordance with the

  • General Statement of Policy and Procedure for NRC Enforcement Actions," (60 FR 34381; June 30,1995), the violation is listed below:

Technical Specification 6.11.1 requires in part, that procedures for personnel radiation protection shall be adhered to for cl! operations involving personnel radiation exposure.

Radiation protection procedure No. HP-C-810, revision 0, requires in section 7.5.1, that all material shall be monitored prior to release from the radiological controlled area (RCA) as specified therein and shall meet the conditions for release also specified therein.

Radiation protection procedure HP-C-818, revision 0 (dated January 1,1994) and revision 1 (dated April 10,1995), require in section 5.1 that plant personnel are responsible for monitoring themselves la accordance with the procedure and for notifying health physics when contamination is detected during monitoring, and requires in section 7.1.5 that radiation protection personnel may approve release of personnel if personnel contamination is less than 100 counts per minute above background.

Contrary to the above, procedures for personnel radiation protection were not adhered to as evidenced by the following examples:

1.

On February 9,1995, a worker attempting to exit the Unit 1 refuellrg floor was identified with fixed contamination on the individual's underwear. Subsequent licensee review indicated the Individual had previously exited the RCA and, due to inappropriate monitoring, did not detect the contamination.

2.

On or about March 17,1995, a worker was identified to have been released by radiation protection personnel with contamination of the right and left shoes of 150 and 400 counts per minute (respectively) abovo background.

3.

On or about March 27,1995, a seconci worker was identified to have been released by radiation protection personnel with contamination of the ri ht and left shoes of 1500 counts per minute C

above background.

4.

On April 3,1995, approximately 12 contaminated miscellaneous items (eg., tools and material) were identified cutside the RCA in various tool rooms that did not meet the conditions for release specified in procedure HP-C-810. Specifically, the items exhibited radioactive contamination above the limits specified therein.

5.

On June 29,1995, radiation protection personnel approved release of an individual who was later determined that day to exhibit personnel contamination of the skin of 600 counts per minute above background and 120 counts per minute above background on a shoelace.

~.

t i

e Attachment Docket N6s. 50452 and 50-353 l

September 5,1995 Page 2 of 4 i

6.

Between July 7 and July 17.1995, approximately 60 items (eg., tools and material) were identifled outside the RCA that did not meet the conditions for release specified in procedure HP-C-810. Specifically, the items exhibited radioactive contamination above the limits specified therein.

t This is a Severity Level IV Violation (Supplement IV).

i

RESPONSE

Admission of the Violation PECO Encrgy Company acknowledges the violation.

Benson for the Violation Management and workers were not sensitive enough to the need to minimize the amount of tools and equipment taken into and out of the RCA. The high volume of items routinely handled at the plant access points challenged our controls and was a significant contributor to this violation.

In response to previous contamination control issues, small article monitors (SAMs) had been purchased and installed at all plant access points. During 1993, use of the SAM for release of hand carried items was transferred from Health Physics to the individual workers. However, the limitations of the SAMs r

were not effectively communicated to the workers. In addition, the postings on the SAMs did not provide adequate detall to ensure proper use.

Limerick Generating Station (LGS) practice allowed release of material with a frisker even if it had previously alarmed a SAM. Since frisker effectiveness is highly dependant on how it is used, this effectively introduced some inconsistency in our process for the release of material from the RCA.

Corrective Actions Taken and Results Achieved l

As referenced in Section 5.1.6, " Radioactive Material and Contamination Controls,* of NRC Inspection Report Nos. 50-352/95-10 and 50-353/95-10, the following corrective actions were implemented.

l Surveillance of tools at the tool rooms were increased from quarteriy to monthly and the sample size was increased from 25 to 75 after discovery of miscellaneous tools with fixed contamination.

Health Physics (HP) procedure HP-C-818 was revised on April 21,1995, to require material to be dry before final monitoring.

A 100% survey of all tools in the tool rooms was pe

. hen two additional contaminated tools were found in tool rooms on July 5,1995.

On July 10,1995, frisking of tools to be issued to personnel from tool rooms was initiated.

Attachment Docket N6s. 50-352 and 50-353 September 5,1995 Page 3 of 4 On July 11,1995, a memorandum was issued to all station personnel regarding worker responsibility for contamination control.

On July 11,1995, the "5" line (Unit 1) RCA exit point was closed down. The Unit 2 269' Turbine building monitoring location was also closed down. Station personnel v.ere also informed that no tools or materials were to be removed from the protected area.

On July 12,1995, a " station standdown" was held with all appropriate personnel to discuss contamination control concems. There was significant management interest in the review and resolution of the identified concoms.

As of thla date, the "5"line (Unit 1) RCA access point remains closed. The Unit 2 269' Turbine Building access is reopened. Radiation Protection personnel are required to observe station workers frisking material to be removed from the RCA.

In addition to the above actions, analysis of the contaminated items previously released, including dose consequences, have been completed. The results of the analysis indicate that there was no significant offect on station workers or the public.

CogIgg1[ygactions to Avoid Future Noncomoliance Construction of a new in-plant tool room is currently in progress. This facility is a long-planned step to minimize the need to routinely carry tools into and out of the RCA at LGS, and is scheduled to be opened by the end of 1995.

A Contamination Ccntrol improvement Plan has been developed and actions are underway to fully understand the circumstances which led up to this event and to make process changes to prevent recurrence. The following is a summary of the plan and the actions being taken.

Evaluate Instrumentation and Response to LGS isotopic Mix This portion of the plan involves three separate actions. The first action was to send representative samples of contamination found throughout various areas of the plant offsite for Isotopic analysis (complete). The second action was to use the results of the isotopic analysis to determine the officiencies of LGS instrumentation to detect the radionuclides present (complete). The third action will involve performing a review of the calibration and response of LGS instrumentation to the results of the isotopic analysis, and designating the preferred instrument for free release from the RCA. This review will include the following devices: dosimeters, portal monitors, small article monitors, bag monitor, tool monitor, friskers and survey instrumentation. This action will be completed by September 30,1995.

Review of the LGS Contamination Control Practices This portion of the plan requires a comprehensive review of LGS facilities, procedures, protective clothing, the Routine Surveillance program and a reassessment of LGS performance in the area of contamination control over the past 3 years. Specific elements of this review are described below.

Evaluate plant exit point flow path, release points and process.

Evaluate fuel floor flow path.

.-. --~_- --

r Attachment j

Docket N6s. 50-352 and 50-353 Septe'mber 5,1995 Page 4 of 4 e

Evaluate all outside buildings.

Evaluate laundry (scrubs and protective clothing) as a source of personnel contaminations.

e e

Evaluate Performance Enhancement Program (PEP) reports from the last three years for generic concems.

i Review corMmination control practices at step off pads, including the role of the Advanced e

Radiation Worker (ARW) program.

investigate desensitization to personnel contamination monitor (PCM) alarms due to Noble Gas.

e e

Review outage critique items.

l e

Benchmark current LGS practices against the industry, including Peach Bottom Atomic Power l

Station.

e Upgrade cameras and communications at the plant exits.

e Evaluate the Routine Surveillance program and plant changes.

r e

Review Administrative Procedure A-30.6, " Control of Plant Contaminated Tools,' for consistency with new program.

e Review ARW contamination control practices.

The goal of this review is to identify and remove factors which challenge the effectiveness of the contamination control program. Any required procedure revisions or other contamination control i

program changes based on the results of this review will be implemented by September 30,1995.

Communications and Training Any further improvements to the contamination control program will be communicated to the station work force. In addition, training of the HP technicians rad station workers to effectively implement such improvements will be conducted as necessary. These actions will be completed by September 30,1995.

Date When Full Compliance was Achieved Full compliance was achieved on July 25,1995, when the survey of all tools outside of the RCA was completed and all tools that were identified as being contaminated were returned to the RCA.

,t

-