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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217D5211999-09-30030 September 1999 Informs That Remediating 3D Monicore Sys at Pbaps,Units 2 & 3 & 3D Monicore/Plant Monitoring Sys at Lgs,Unit 2 Has Been Completed Ahead of Schedule ML20216J3981999-09-29029 September 1999 Submits Comments for Lgs,Unit 1 & Pbaps,Units 2 & 3 Rvid,Rev 2,based on Review as Requested in GL 92-01,rev 1,suppl 1, Reactor Vessel Structural Integrity ML20212J6561999-09-29029 September 1999 Informs of Completion of mid-cycle PPR of Limerick Generating Station on 990913.Identified No Areas in Which Licensee Performance Warranted Addl Insp Beyond Core Insp Program.Historical Listing of Plant Issues Encl ML20212H6401999-09-24024 September 1999 Forwards Revised Epips,Including Rev 11 to ERP-101 & Rev 18 to ERP-800.Copy of Computer Generated Rept Index Identifying Latest Revs of LGS Erps,Encl ML20212E7941999-09-22022 September 1999 Requests Authorization for Listed Licensed Operators to Temporarily Suspend Participation in Licensed Operator Requalification Program at LGS ML20212E8081999-09-22022 September 1999 Provides Notification That Listed Operators Have Been Permanently Reassigned to Duties That Do Not Require Maintaining Licensed Operator Status,Per 10CFR50.74 ML20212F5481999-09-20020 September 1999 Forwards Response to NRC Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing, for Pbaps,Units 2 & 3 & Lgs,Units 1 & 2 ML20212F8991999-09-17017 September 1999 Provides Written Confirmation That Thermo-Lag 330-1 Fire Barrier Corrective Actions at Lgs,Units 1 & 2 Have Been Completed 05000353/LER-1999-010, Forwards LER 99-010-00,re Manual Actuation of Esf.Main CR Ventilation Sys Was Placed in Chlorine Isolation Mode Due to Rept of Faint Odor of Chlorine in Unit 2 Reactor Encl1999-09-16016 September 1999 Forwards LER 99-010-00,re Manual Actuation of Esf.Main CR Ventilation Sys Was Placed in Chlorine Isolation Mode Due to Rept of Faint Odor of Chlorine in Unit 2 Reactor Encl ML20216F7821999-09-16016 September 1999 Forwards Insp Repts 50-352/99-05 & 50-353/99-05 on 990713-0816.One Violation Noted & Being Treated as NCV, Consistent with App C of Enforcement Policy.Violation Re Inoperability of Automatic Depression Sys During Maint ML20212A8751999-09-13013 September 1999 Forwards Safety Evaluation of First & Second 10-year Interval Inservice Insp Plan Request for Relief ML20211N5061999-09-0909 September 1999 Forwards TSs Bases Pages B 3/4 10-2 & B 3/4 2-4 for LGS, Units 1 & 2,being Issued to Assure Distribution of Revised Bases Pages to All Holders of TSs ML20212A0091999-09-0909 September 1999 Provides Notification That Licenses SOP-11172 & SOP-11321, for SO Muntzenberger & Rh Wright,Respectively,Are No Longer Necessary as Result of Permanent Reassignment ML20211P8571999-09-0808 September 1999 Forwards Reactor Operator Retake Exams 50-352/99-303OL & 50-353/99-303OL Conducted on 990812 ML20211P3891999-09-0303 September 1999 Informs That During 990902 Telcon Between J Williams & B Tracy,Arrangements Were Made for NRC to Inspect Licensed Operator Requalification Program at Plant.Insp Planned for Wk of 991018 05000352/LER-1999-009, Forwards LER 99-009-00,providing 30-day Written follow-up Rept Re Performance of Maint That Affected Safeguard Sys for Which Compensatory Measures Had Not Been Employed1999-09-0101 September 1999 Forwards LER 99-009-00,providing 30-day Written follow-up Rept Re Performance of Maint That Affected Safeguard Sys for Which Compensatory Measures Had Not Been Employed ML20211H2571999-08-26026 August 1999 Informs of Individual Exam Result on Initial Retake Exam on 990812.One Individual Was Administered Exam & Passed ML20211E9191999-08-24024 August 1999 Forwards fitness-for-duty Program Performance Data for Jan-June 1999 for PBAPS & LGS IAW 10CFR26.71(d).Data Includes Listed Info ML20211E9731999-08-23023 August 1999 Forwards LGS Unit 2 Summary Rept for 970228 to 990525 Periodic ISI Rept Number 5, Per TS SRs 4.0.5 & 10CFR50.55a(g) ML20211D6761999-08-20020 August 1999 Forwards non-proprietary Revised Emergency Response Procedures (Erps),Including Rev 29 to ERP-110, Emergency Notification & Rev 17 to ERP-800, Maint Team & Proprietary App ERP-110-1.App Withheld Per 10CFR2.790(a)(6) ML20210T4271999-08-13013 August 1999 Informs That NRC Revised Info in Rvid & Releasing Rvid Version 2 as Result of Review of 980830 Responses to GL 92-01 Rev 1,GL 92-01 Rev 1 Suppl 1 & Suppl Rai.Tacs MA1197 & MA1198 Closed ML20210U2211999-08-10010 August 1999 Forwards Insp Repts 50-352/99-04 & 50-353/99-04 on 990525-0712.One Violation Occurred & Being Treated as NCV, Consistent with App C of Enforcement Policy.Violation Re Late Performance of off-gas Grab Sample Surveillance 05000353/LER-1999-005, Forwards LER 99-005-00,re Actuation of Primary Containment & Reactor Vessel Isolation Control Sys,Esf.Fuse Failed Due to Mechanical Failure of Cold Solder Joint1999-08-10010 August 1999 Forwards LER 99-005-00,re Actuation of Primary Containment & Reactor Vessel Isolation Control Sys,Esf.Fuse Failed Due to Mechanical Failure of Cold Solder Joint ML20211B7881999-08-10010 August 1999 Transmits Summary of Two Meetings with Risk-Informed TS Task Force in Rockville,Md on 990514 & 0714 ML20210M7571999-08-0404 August 1999 Forwards Response to Requesting Addl Info Re Status of Decommissioning Funding for Lgs,Pbaps & Sngs. Attachment Provides Restatement of Questions Followed by Response ML20210P4191999-08-0404 August 1999 Forwards Initial Exam Repts 50-352/99-302 & 50-353/99-302 on 990702-04 (Administration) & 990715-22 (Grading).Six of Limited SRO Applicants Passed All Portion of Exam NUREG-1092, Informs J Armstrong of Individual Exam Results for Applicants on Initial Exam Conducted on 990702 & 990712-14 at Facility.All Six Individuals Who Were Administered Exam, Passed Exam.Without Encls1999-08-0303 August 1999 Informs J Armstrong of Individual Exam Results for Applicants on Initial Exam Conducted on 990702 & 990712-14 at Facility.All Six Individuals Who Were Administered Exam, Passed Exam.Without Encls ML20210L2011999-07-28028 July 1999 Forwards Final Personal Qualification Statement (NRC Form 398) for Reactor Operator License Candidate LB Mchugh ML20211F2641999-07-27027 July 1999 Forwards Three Copies of Rev 12 to LGS Physical Security Plan, Rev 4 to LGS Training & Qualification Plan & Rev 2 to LGS Safeguards Contingency Plan. Without Encls 05000352/LER-1999-008, Forwards LER 99-008-00 Re 990623 Failure of Plant HPCI Sys to Start Due to Failure of HPCI Turbine,Hydraulic Actuator1999-07-23023 July 1999 Forwards LER 99-008-00 Re 990623 Failure of Plant HPCI Sys to Start Due to Failure of HPCI Turbine,Hydraulic Actuator 05000353/LER-1999-004, Forwards LER 99-004-00 Re 990701 Discovery of Pressure Setpoint Drift of Thirteen Mss SRV Due to Corrosion Induced Bonding within SRVs1999-07-23023 July 1999 Forwards LER 99-004-00 Re 990701 Discovery of Pressure Setpoint Drift of Thirteen Mss SRV Due to Corrosion Induced Bonding within SRVs ML20210E6211999-07-22022 July 1999 Submits Rev to non-limiting Licensing Basis LOCA Peak Clad Temps (Pcts) for Limerick Generating Station (Lgs),Units 1 & 2 & Pbaps,Units 2 & 3 ML20216D3081999-07-19019 July 1999 Requests Renewal of OLs for Listed Individuals,Iaw 10CFR55.57.NRC Forms 398 & 396,encl for Applicants.Without Encl ML20216D8041999-07-19019 July 1999 Submits Summary of Final PECO Nuclear Actions Taken to Resolve Scram Solenoid Pilot Valve Issues Identified in Info Notice 96-007 05000352/LER-1999-006, Forwards LER 99-006-00 Re 990614 Discovery That Grab Sample of Plant Offgas Sys Was Not Obtained within Time Limit Required by TS 3.3.7.12,Action 110 Due to Personnel Error1999-07-12012 July 1999 Forwards LER 99-006-00 Re 990614 Discovery That Grab Sample of Plant Offgas Sys Was Not Obtained within Time Limit Required by TS 3.3.7.12,Action 110 Due to Personnel Error ML20209F6341999-07-0909 July 1999 Submits Supplemental Response to GL 94-03, Intergranular Stress Corrosion Cracking of Core Shrouds in Bwrs, for Unit 2.Rev 0 to 1H61R & GE-NE-B13-02010-33NP Repts & Revised Pages to Summary Rept Previously Submitted,Encl ML20209G9121999-07-0909 July 1999 Informs That Ja Hutton Has Been Appointed Director,Licensing for PECO Nuclear,Effective 990715.Previous Correspondence Addressed to Gd Edwards Should Now Be Sent to Ja Hutton ML20209C9041999-07-0808 July 1999 Forwards Monthly Operating Repts for June 1999 for Limerick Generating Station,Units 1 & 2 & Revised Monthly Repts for May 1999 ML20210B4441999-07-0808 July 1999 Forwards Preliminary NRC Form 398 & NRC Form 396 for Reactor Operator for License Candidate LB Mchugh.Candidate Failed Category B Portion of Operating Exam Given at LGS During Week of 990315.Tentative re-exam Has Been Scheduled 990812 05000353/LER-1999-003, Forwards LER 99-003-00,re Bypass of RW Cleanup Leak Detection Sys Isolation Function on Three Separate Occasions.Bypass of Safety Function Was Caused by Inadequate Review & Approval of Change to Procedure1999-07-0707 July 1999 Forwards LER 99-003-00,re Bypass of RW Cleanup Leak Detection Sys Isolation Function on Three Separate Occasions.Bypass of Safety Function Was Caused by Inadequate Review & Approval of Change to Procedure ML20209D8821999-07-0707 July 1999 Submits Estimate of Number of Licensing Actions Expected to Be Submitted in Years 2000 & 2001,as Requested by Administrative Ltr 99-02.Renewal Applications for PBAPS, Units 2 & 3,will Be Submitted in Second Half of 2001 ML20209D2671999-07-0202 July 1999 Responds to NRC 990322 & 0420 RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20196J6301999-07-0101 July 1999 Requests Addl Info Re Status of Decommissioning Funding for Limerick Generating Station,Units 1 & 2,Peach Bottom Atomic Power Station,Units 1,2 & 3 & Salem Nuclear Generating Station,Units 1 & 2 05000352/LER-1999-004, Forwards LER 99-004-00,re Inoperability of Automatic Depressurization Sys Portion of Eccs.Condition Resulted from Incomplete Impact Review of Isolating Portion of ADS Nitrogen Backup Supply on Operability of ECCS Sys1999-07-0101 July 1999 Forwards LER 99-004-00,re Inoperability of Automatic Depressurization Sys Portion of Eccs.Condition Resulted from Incomplete Impact Review of Isolating Portion of ADS Nitrogen Backup Supply on Operability of ECCS Sys ML20209B7001999-06-30030 June 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20212J5401999-06-28028 June 1999 Discusses Completion of Licensing Action for NRC Bulletin 96-003, Potential Plugging of ECC Suction Strainers by Debris in Bwrs. Bulletin Closed for Unit 2 by NRC ML20207H8271999-06-24024 June 1999 Informs NRC That Util Has Completed Core Shroud Insps for LGS Unit 2.Proprietary Rept GE-NE-B13-02010-33P & non-proprietary Rev 0 to 1H61R,encl.Proprietary Rept Withheld,Per 10CFR2.790(a)(4) ML20196G7041999-06-24024 June 1999 Forwards Insp Repts 50-352/99-03 & 50-353/99-03 on 990413- 0524.No Violations Noted.Nrc Concluded That Licensee Staff Continued to Operate Both Units Safely ML20196A5641999-06-15015 June 1999 Provides Info Re Util Use of Four Previously Irradiated LGS, Unit 1,GE11 Assemblies in Unit 2 Cycle 6.Encl 990518 GE Ltr Provides Objective of Lead Use Assemblies Program & Outlines Kinds of Measurements That Will Be Made on Assemblies ML20195J6831999-06-11011 June 1999 Provides Proprietary Objectives for Lgs,Units 1 & 2,1999 Emergency Preparedness Exercise Scheduled to Be Conducted on 990914.Licensee Identifies Which Individuals Should Receive Copies of Info.Proprietary Info Withheld 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217D5211999-09-30030 September 1999 Informs That Remediating 3D Monicore Sys at Pbaps,Units 2 & 3 & 3D Monicore/Plant Monitoring Sys at Lgs,Unit 2 Has Been Completed Ahead of Schedule ML20216J3981999-09-29029 September 1999 Submits Comments for Lgs,Unit 1 & Pbaps,Units 2 & 3 Rvid,Rev 2,based on Review as Requested in GL 92-01,rev 1,suppl 1, Reactor Vessel Structural Integrity ML20212H6401999-09-24024 September 1999 Forwards Revised Epips,Including Rev 11 to ERP-101 & Rev 18 to ERP-800.Copy of Computer Generated Rept Index Identifying Latest Revs of LGS Erps,Encl ML20212E7941999-09-22022 September 1999 Requests Authorization for Listed Licensed Operators to Temporarily Suspend Participation in Licensed Operator Requalification Program at LGS ML20212E8081999-09-22022 September 1999 Provides Notification That Listed Operators Have Been Permanently Reassigned to Duties That Do Not Require Maintaining Licensed Operator Status,Per 10CFR50.74 ML20212F5481999-09-20020 September 1999 Forwards Response to NRC Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing, for Pbaps,Units 2 & 3 & Lgs,Units 1 & 2 ML20212F8991999-09-17017 September 1999 Provides Written Confirmation That Thermo-Lag 330-1 Fire Barrier Corrective Actions at Lgs,Units 1 & 2 Have Been Completed 05000353/LER-1999-010, Forwards LER 99-010-00,re Manual Actuation of Esf.Main CR Ventilation Sys Was Placed in Chlorine Isolation Mode Due to Rept of Faint Odor of Chlorine in Unit 2 Reactor Encl1999-09-16016 September 1999 Forwards LER 99-010-00,re Manual Actuation of Esf.Main CR Ventilation Sys Was Placed in Chlorine Isolation Mode Due to Rept of Faint Odor of Chlorine in Unit 2 Reactor Encl ML20212A0091999-09-0909 September 1999 Provides Notification That Licenses SOP-11172 & SOP-11321, for SO Muntzenberger & Rh Wright,Respectively,Are No Longer Necessary as Result of Permanent Reassignment 05000352/LER-1999-009, Forwards LER 99-009-00,providing 30-day Written follow-up Rept Re Performance of Maint That Affected Safeguard Sys for Which Compensatory Measures Had Not Been Employed1999-09-0101 September 1999 Forwards LER 99-009-00,providing 30-day Written follow-up Rept Re Performance of Maint That Affected Safeguard Sys for Which Compensatory Measures Had Not Been Employed ML20211E9191999-08-24024 August 1999 Forwards fitness-for-duty Program Performance Data for Jan-June 1999 for PBAPS & LGS IAW 10CFR26.71(d).Data Includes Listed Info ML20211E9731999-08-23023 August 1999 Forwards LGS Unit 2 Summary Rept for 970228 to 990525 Periodic ISI Rept Number 5, Per TS SRs 4.0.5 & 10CFR50.55a(g) ML20211D6761999-08-20020 August 1999 Forwards non-proprietary Revised Emergency Response Procedures (Erps),Including Rev 29 to ERP-110, Emergency Notification & Rev 17 to ERP-800, Maint Team & Proprietary App ERP-110-1.App Withheld Per 10CFR2.790(a)(6) 05000353/LER-1999-005, Forwards LER 99-005-00,re Actuation of Primary Containment & Reactor Vessel Isolation Control Sys,Esf.Fuse Failed Due to Mechanical Failure of Cold Solder Joint1999-08-10010 August 1999 Forwards LER 99-005-00,re Actuation of Primary Containment & Reactor Vessel Isolation Control Sys,Esf.Fuse Failed Due to Mechanical Failure of Cold Solder Joint ML20210M7571999-08-0404 August 1999 Forwards Response to Requesting Addl Info Re Status of Decommissioning Funding for Lgs,Pbaps & Sngs. Attachment Provides Restatement of Questions Followed by Response ML20210L2011999-07-28028 July 1999 Forwards Final Personal Qualification Statement (NRC Form 398) for Reactor Operator License Candidate LB Mchugh ML20211F2641999-07-27027 July 1999 Forwards Three Copies of Rev 12 to LGS Physical Security Plan, Rev 4 to LGS Training & Qualification Plan & Rev 2 to LGS Safeguards Contingency Plan. Without Encls 05000352/LER-1999-008, Forwards LER 99-008-00 Re 990623 Failure of Plant HPCI Sys to Start Due to Failure of HPCI Turbine,Hydraulic Actuator1999-07-23023 July 1999 Forwards LER 99-008-00 Re 990623 Failure of Plant HPCI Sys to Start Due to Failure of HPCI Turbine,Hydraulic Actuator 05000353/LER-1999-004, Forwards LER 99-004-00 Re 990701 Discovery of Pressure Setpoint Drift of Thirteen Mss SRV Due to Corrosion Induced Bonding within SRVs1999-07-23023 July 1999 Forwards LER 99-004-00 Re 990701 Discovery of Pressure Setpoint Drift of Thirteen Mss SRV Due to Corrosion Induced Bonding within SRVs ML20210E6211999-07-22022 July 1999 Submits Rev to non-limiting Licensing Basis LOCA Peak Clad Temps (Pcts) for Limerick Generating Station (Lgs),Units 1 & 2 & Pbaps,Units 2 & 3 ML20216D3081999-07-19019 July 1999 Requests Renewal of OLs for Listed Individuals,Iaw 10CFR55.57.NRC Forms 398 & 396,encl for Applicants.Without Encl ML20216D8041999-07-19019 July 1999 Submits Summary of Final PECO Nuclear Actions Taken to Resolve Scram Solenoid Pilot Valve Issues Identified in Info Notice 96-007 05000352/LER-1999-006, Forwards LER 99-006-00 Re 990614 Discovery That Grab Sample of Plant Offgas Sys Was Not Obtained within Time Limit Required by TS 3.3.7.12,Action 110 Due to Personnel Error1999-07-12012 July 1999 Forwards LER 99-006-00 Re 990614 Discovery That Grab Sample of Plant Offgas Sys Was Not Obtained within Time Limit Required by TS 3.3.7.12,Action 110 Due to Personnel Error ML20209F6341999-07-0909 July 1999 Submits Supplemental Response to GL 94-03, Intergranular Stress Corrosion Cracking of Core Shrouds in Bwrs, for Unit 2.Rev 0 to 1H61R & GE-NE-B13-02010-33NP Repts & Revised Pages to Summary Rept Previously Submitted,Encl ML20209G9121999-07-0909 July 1999 Informs That Ja Hutton Has Been Appointed Director,Licensing for PECO Nuclear,Effective 990715.Previous Correspondence Addressed to Gd Edwards Should Now Be Sent to Ja Hutton ML20210B4441999-07-0808 July 1999 Forwards Preliminary NRC Form 398 & NRC Form 396 for Reactor Operator for License Candidate LB Mchugh.Candidate Failed Category B Portion of Operating Exam Given at LGS During Week of 990315.Tentative re-exam Has Been Scheduled 990812 ML20209C9041999-07-0808 July 1999 Forwards Monthly Operating Repts for June 1999 for Limerick Generating Station,Units 1 & 2 & Revised Monthly Repts for May 1999 05000353/LER-1999-003, Forwards LER 99-003-00,re Bypass of RW Cleanup Leak Detection Sys Isolation Function on Three Separate Occasions.Bypass of Safety Function Was Caused by Inadequate Review & Approval of Change to Procedure1999-07-0707 July 1999 Forwards LER 99-003-00,re Bypass of RW Cleanup Leak Detection Sys Isolation Function on Three Separate Occasions.Bypass of Safety Function Was Caused by Inadequate Review & Approval of Change to Procedure ML20209D8821999-07-0707 July 1999 Submits Estimate of Number of Licensing Actions Expected to Be Submitted in Years 2000 & 2001,as Requested by Administrative Ltr 99-02.Renewal Applications for PBAPS, Units 2 & 3,will Be Submitted in Second Half of 2001 ML20209D2671999-07-0202 July 1999 Responds to NRC 990322 & 0420 RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves 05000352/LER-1999-004, Forwards LER 99-004-00,re Inoperability of Automatic Depressurization Sys Portion of Eccs.Condition Resulted from Incomplete Impact Review of Isolating Portion of ADS Nitrogen Backup Supply on Operability of ECCS Sys1999-07-0101 July 1999 Forwards LER 99-004-00,re Inoperability of Automatic Depressurization Sys Portion of Eccs.Condition Resulted from Incomplete Impact Review of Isolating Portion of ADS Nitrogen Backup Supply on Operability of ECCS Sys ML20209B7001999-06-30030 June 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20207H8271999-06-24024 June 1999 Informs NRC That Util Has Completed Core Shroud Insps for LGS Unit 2.Proprietary Rept GE-NE-B13-02010-33P & non-proprietary Rev 0 to 1H61R,encl.Proprietary Rept Withheld,Per 10CFR2.790(a)(4) ML20196A5641999-06-15015 June 1999 Provides Info Re Util Use of Four Previously Irradiated LGS, Unit 1,GE11 Assemblies in Unit 2 Cycle 6.Encl 990518 GE Ltr Provides Objective of Lead Use Assemblies Program & Outlines Kinds of Measurements That Will Be Made on Assemblies ML20195J6831999-06-11011 June 1999 Provides Proprietary Objectives for Lgs,Units 1 & 2,1999 Emergency Preparedness Exercise Scheduled to Be Conducted on 990914.Licensee Identifies Which Individuals Should Receive Copies of Info.Proprietary Info Withheld ML20195G4591999-06-10010 June 1999 Forwards MORs for May 1999 & Revised Repts for Apr 1999 for LGS Units 1 & 2 ML20195H0531999-06-0909 June 1999 Forwards Revised Bases Pages B3/4 10-2 & B3/4 2-4 for LGS Units 1 & 2,in Order to Clarify That Requirements for Reactor Enclosure Secondary Containment Apply to Extended Area Encompassing Both Reactor Enclosure & Refueling Area ML20195E7701999-06-0707 June 1999 Provides Notification of Change to NPDES Permit PA0052221, for Bradshaw Reservoir Facility Which Supports Operation of Lgs,Units 1 & 2,per EPP Section 3.2 ML20195C7631999-06-0101 June 1999 Notifies NRC That PECO Energy Has Completed Installation of New Large Capacity,Passive Strainers on RHR & Core Spray Sys Pump Suction Lines at Lgs,Unit 2,in Response to Ieb 96-003 ML20195D5381999-05-26026 May 1999 Forwards 1998 Occupational Exposure Tabulation Rept for LGS Units 1 & 2. Encl Is Diskette & Instructions.Rept Is Being re-submitted to Reset 12 Month Time Period.Without Disk ML20195B2821999-05-24024 May 1999 Requests That NRC Distribution Lists for LGS Be Updated. Marked-up Distribution List Showing Changes Is Attached ML20196L2891999-05-20020 May 1999 Provides Status Update of Thermo-Lag 330-1 Fire Barrier Corrective Actions,Iaw Commitments Made in ML20195B2951999-05-20020 May 1999 Forwards Rev 0 to LGS Unit 2 Reload 5,Cycle 6 COLR, IAW TS Section 6.9.1.12.Values Listed Have Been Determined Using NRC-approved Methodology & Are Established Such That All Applicable Limits of Plants Safety Analysis Are Met 05000352/LER-1999-003, Forwards LER 99-003-00,re Rps,Pcrvics Actuations.Ler Contains Special Rept Info for HPCI & Reactor Core Isolation Cooling Sys Injections Into Rv1999-05-19019 May 1999 Forwards LER 99-003-00,re Rps,Pcrvics Actuations.Ler Contains Special Rept Info for HPCI & Reactor Core Isolation Cooling Sys Injections Into Rv 05000353/LER-1999-002, Forwards LER 99-002-00,automatic Actuations of Primary Containment & Reactor Vessel Isolation Control Sys & Other Common Plant ESF Due to Loss of Power to a Rps/Ups Power Distribution Panel on 9904191999-05-18018 May 1999 Forwards LER 99-002-00,automatic Actuations of Primary Containment & Reactor Vessel Isolation Control Sys & Other Common Plant ESF Due to Loss of Power to a Rps/Ups Power Distribution Panel on 990419 ML20206E2001999-04-28028 April 1999 Forwards 1998 Annual Environ Operating Rept (Non- Radiological) for Limerick Generating Station,Units 1 & 2. Rept Submitted IAW Section 5.4.1 of App B of Fols,Epp (Non- Radiological) & Describes Implementation of EPP for 1998 ML20206D8801999-04-27027 April 1999 Forwards Rev 2 to LGS Unit 1 Reload 7,Cycle 8 COLR, IAW TS Section 6.9.1.12.COLR Provides cycle-specific Parameter Limits for Noted Info ML20206A5461999-04-21021 April 1999 Responds to Conference Call Between Util & NRC on 990420,re TS Change Request 98-07-2,revising TS Section 2.0 to Incorporate Revised MCPR Safety Limits.Attached Ltr Contains Info Requested ML20205T0441999-04-17017 April 1999 Forwards 1998 Annual Radiological Environ Operating Rept 15, IAW TS Section 6.9.1.7.REMP for 1998,confirmed That LGS Environ Effects from Radioactive Release Were Well Below LGS TSs & Other Applicable Regulatory Limits ML20205Q7581999-04-15015 April 1999 Forwards Response to RAI Re ISI Program First & Second 10-Yr Interval Relief Requests.Revs to Identified by Vertical Bar in Right Margin 1999-09-09
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10 CPR 2.201
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^ . PHILADELPHIA ELECTRIC COMPANY LIMERICK GENERATING STATION P. O. BOX 2300 POITSTOWN, PA: 19464-0920 - ;
(215) 327-1200, EXT. ;*000 January 30, 1992_-
- GRAHAM M. LENCH vcemesotwr Docket Nos. 50-352 wm arm santw 50-353 i License Nos.-NPF-39 NPF-85 L U.S. Nuclear Regulatory Commihsion ,
Attn: Document-Control-Dese Washington, DC 20555 SDBJECT: Limerick Generating Station, Units 1-and 2 Reply to a Notice of Violation NRC Inspection Report Nos. 50 '52/91-81 and 50-353/91-81 Attached is Philadelphia Electric Compny's reply to a Notice- of . ~
. Violation for_ Limerick Generating Station (LGS) Units 1 and 2, which was
-contained =in the NRC Inspection Report Nos. 50-352/91-81.and.50-353/91 .81 Jdated December 12, 1991.
-The Notice of VioAation identifies two areas that. indicate a weakness with personnel.recogni,ing and initiating corrective actions for conditions
-adverse to quality. The first area concerned a lack of attention to detail' by; station personnel'in the documentation and analysic of indicated anomalies
-.in Emergency Diesel Generator test results. The second area concerned the failure to=maintrin emergency lighting installed for safe shutdown in laccordance with NRC requirements.
~ ~
.. The attachment to this' letter provides'a restatement of the. violations Eidentified'during an NRC inspection conducted between' July 8, 1991, through' DJuly:19,'1991, at LGS, Units 1 and-2, followed by our responses.
An extension of two-weeks to the prescribed response time was requested and granted to allow clarification of the violaticn regarding emergency lighting.
If you have any' questions or require additional information, please contact us.
-Very truly yours, 030023 O}T7> ,,fy,Q. t1 iDMS/dCS:cah / -- I., .
y
Attachment:
{g cc: 'W.-T. Russell, Administrator, Region I, USNRC / k T. J Kenny,-USNRC Senior Resident Inspector, LGS- jk 9202040003 920130 PDR ADOCX 05000352 G
-PDR ,
~ . . - - -~. - . _ - .
-- . . . _ __ . - . - . - - _ . _ _ . _ _ . _ _ . _ . . _ _ . - . . = . . _ . . _ . . _ ~ _ _ .
bcc t- D. M. Smith -
52C-7 J. Doering, Jr. -
ADMS-1 D. R.-Helwig -
63C 1 J. W..Durham- -
S26-1 G. A. Hunger, Jr. - SMB1-1 R. W.-Boyce -
ADMS-1 L. A.-Hopkins -
ADMS-1 J. A. Muntz -
.ADMS-1 D. G. Miller -
BTC ISEG Supt. -
SMB3-2 G. J. Madsen -
SSB3-4 J. F. O'Rourke -
SSB4-3
- d. ". Charles -
51A-1 G. J. Beck, Jr., - 52A-5 Secretary, NCB -
51A-13 Correspondence Release Point - SMB1-2 DCC PA DER BRP Inspector - SMB2-2 a.
s
,. - s. -
.- . .- - - , --- .,-y
At achment 3;
Page 1 of 5 m
Inspection Report.Nos. 50-352/91-81 50-353/91-81 Reply to a Notice of Violation Violation A Restatement of the Violation 10 CFP 50 Appendix B, Criterion XVI, states, in part, " Measures shall.be established to assure'that conditions adverse to quality...are promptly identified and corrected...and corrective accion taken to preclude repetition."
- 1. Limerick Generating Station Procedure PMO-020-010, Section 7.21.7, requires that the acceptance criteria for_the emergen;y diesel engine fuel injactor timing not exceed (+/-) 1/2 degrees between control side.and opposite control side.
Contrary to the above, on February 19, 1991, the emergency diesel generator _2D-G501-DR did not meet the fuel injector t'n 'ng acceptanct criteria. This was recorded during the test but not identified as beyond the acceptance criteria.
-2. Limerick Generating Station Procedure PMQ-020-010, Section 7.13.8, provides acceptance criteria for crankcase straits measurements of .0015 inches maximum.
Contrary to the above, on_ April 25, 1990, the crankcase strain value1of-.0025 was measured and recorded which exceeds the -
acceptance criteria of .0015 inches. No corrective actions were taken.
Collectively, these constitu e a Severity Level lV Violation.
(Supplement 1)
RESPONSE
Admission of Violation Philadelphia Electric Company (PEco) acknowledges the violation.
Reason for the Vloiation The cause of the violation is a lack of attention to detail on the part of the individuals who performed and reviewed the preventive maintenance procedures coupled with a less than adequate communication of expectations from management regarding attention to
-detail and procedure compliance. Additionally, Preventive Maintenance procedure PMQ-020-010 ontained an unclear acceptance criteria value for the fuel injector timing differences.
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. Attachment Page 2 of 5 Inspection Report Nos. 50-352/91-81 50-353/91-81 Corrective Action and Results Achieved A Nonconformance Report (NCR), number L91192, was initiated on July 17, 1991, which evaluated fuel injector timing readings for a similar problem identified for the Emergency Diesel Generator (EDG)
D22, where EDG D22 also did not meet the acceptance criteria contained in procedure PMQ-020-010. An evaluation performed by the Maintenance Engineering Staff for r3G D24, supported by the NCR for EDG D22, concluded that the actual setting for EDG 024 aas outside of the manufacturer's recommended setting; however, this recommendation is based upon fuel consumption criteria to achieve maximum efficiency and not upon safety or reliability concerns. The evaluation concluded that the current settings, although slightly out of tolerance, are acceptable for an interim period until the 3 .
settings could be adjusted during the next performance of procedure PMQ-020-010 for EDG D24 scheduled for February 24, 1992.
Additionally, the evaluation concluded that an acceptance criteria of one degree difference for fuel injecter timing was in accordance with the vendo- recommendations. Procedure PMO-020-010 was revised on September s, 1991, where the injectot timing acceptance criteria was clarified to read the difference between control side and j opposite control side timing shall not exceed one degree.
A NCR, number L91191, was initiated on July 15, 1991, and evaluated the crankshaft strain reading for EDG D14 that did not meet the acceptance criteria contained in procedure PMO-020-010. Based epon interviews with the individuals who performed the procedure, and an analysis of the performance of EDG D14, the NCR evaluation concluded that the reading was an inadvertent error in entry. The actual crankshaft strain reading should actually be .00025 inches, which is within the acceptance criteria, As a reGult of the two items identified above, the Limerick Generating Station (LGS) Nuclear Quality Assurance (NOA) Division perforced a review of Maintenance Request Form (MRF) work packages and their associated documenta ion completed during the period of 4 July 15, 1990, through July 15, 1991, by Quality Control (QC) inspectors. Of the one-hundted and sixty (160) MRFs reviewed, fifty-two (52) MRFs had concerns or problems. NOA concluded that the identified weaknesses represent a lack of attention to detail by all involved LGS organizations, but did not represent any equipment concerns. To strengthen the oversight of QC activities, the following actions were implemented by NQA.
o Prccedure NOA-4-Sll, " Management Oversicht of the Quality Control Program," was developed to define the methodology and responsibilities to be utilized in the performance of management oversight of the QC program, o Procedure NQA-4-S6, "MRP Planning and Review," was revised to further emphasize the need for attention to all, and to ensure the appropriate performance of required verifications are implemented by QC inspectors during inspection activities.
Attachment Page 3 of 5 Inspection Report Nos. 50-352/91-81 50-353/91-81 Corrective Actions Taken to Avoid Future Non-Compliance J. On July 12. 1991, a For Your Information (FYI) notice was developed and distributed to first line supervision. This FYI notice provided a clear and concie et of written management expectations regarding attention to detail required in performance of any task performed. The FYI notice clearly states that the individual is responsible to self-check the work performed and to ensure that each detail of any task performed is correct and complete. First line supervision then disseminated the expectations of management in this FYI notice to station personnel to heighten their awareness of the requirements and management's expectations.
- 2. The program for the control of FYI notices contains a provision to have the first line supervisors periodically re-examine the issued FYI's and to determine if any notices should be reviewed again with the work group based on unacceptable observations or personnel changes in the group.
- 3. Attention to Cetail training has been provided to Maintenance Craft and NQA personnel through the continuing training program.
This traiaing further explained the expectations regarding attention to detail while pc-forming work activities and completing procedures, and til be repeated during future contit.uing training cycles.
- 4. The LGS policy, as described in Administrative Guideline AG-82, "Self Assessment," is that station personnel, groups, and organizations compare theic performance against standards and expectations. The guideline explains that one method to accomplish this is to develop performance indicators (PI). An example of a PI that has been created to monitor the concern identified in this violation is one that monitors the error rate in the performance of procedures and tasks. The station self assessment program recommends that the PIs be trended and evaluated by first line supervisors and upper management, and that corrective actions be initiated if a PI-negative trend is observed. The station self assessment prcgram a]so includes a provision to periodically re-evaluate the PIs to determine whether any PI needs to be revised.
Date When Full Compliance was Achieved Full compliance was achieved on July 18, 1991, when the NCR evaluations were ccmpleted concluding that the fuel injector timing setting and the crankshaft strain readings were acceptable, and that no iramediate corrective actions were required.
0- Attachment
- Page 4 of 5 Inspection Report Nos. 50-752/91-81 50-353/91-81 Reply to a Notice of Violation Violation B Restatement of the Violation The License condition-3.a of Limerick Generating Station, Unit 1 requires that the licensee shall maintain in effect all provisions of the approved fire protection program as described in the Final Safety Analysis Report for the facility through Revision 34 and as approved in the SER through Supplement 2, and in the Fire Protection Evaluation Report through Revision 6, subject to provisians b and c below.
The Limerick Generating Station Fire Protection Evaluation Report states, in part, that emergency lighting of 1/2 foot candle will be provided for all areas that must be manned for safe shutdcwn.
Contrary _to the above, on July 19, 199., the emergency lighting in 2
areas' required for safe shutdown were not maintained as required, in that the battery powered emergency lighting fixtures were inoperable and inadequate to provide 1/2 foot candle of illumination as required. This conlition remained unidentified until discovered by the K3C.
This is a Severity Level IV Violation. (Supplement I)
RESPONS2 Admissior of Violation Philadelphia Electric Company (PECo) acknowledges tist a violation of NRC requirements (e.g., 10CFR50, Appendix B) occur ed as a result of the identified condition cf the battery powered emergency lighting fixtures.
10CFR50, Appendix B, Criterion XVI requires that "Measuces shall be establishad to assure that conditions adverse to quality... are promptly icentified and corrected ... and cocrective action taken to
. preclude repetition." The condition of certain of the battery units was not identified and corrective action was not ta..an.in other cases.
It is our position that the unavailability of an installed component required for fire safe shutdown due to component failure or maintenance does not const it ite a violation of License Condition 3.a. Failure to translate sne fire protection information from the UFSAR correctly into plant documents (drawings, procedures, etc)-
would be considered a violation of the License Condition. For example, failure to install battery units in the plant due to a failure-to identify the battery units on plant drawings would be considered a failure to maintain in effect all provisions of the approved fire protection program.
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Attachment
_lnspection Report Nos. 50-352/91-81
. . -- 50-353/91-81 Reason for the Violation The reason for the degraded condition of the emergency lighting fixtures was informal work practices in the identification and correction of deficiencies associated with the emergency lighting fixtures. Previous work practices involved identification of failed fixtures with an Equipment' Trouble Tag, generation of a Maintenance Request Form (MRF) and subsequent inclusion of the repair in a generic MRP for all lighting fixtures prior to completion of repairs. This method did not facilitate trending of individual-failures.
Corrective Action Taken and Results Achieved Following identification of certain failed emergency lighting '
fixtures by the NRC, the system engineer performed a complete walkdown of emergency lieb'ing fixtures. All failed emergency lighting fixtures identified by either the NRC or station personnel in the Emergency Diesel Generator enclosures, were repaired by July 10, 1991.
Correct-ive Actions Taken to Avoid Future Non-Compliance Al .te safe shutdown emergency lighting fixtures are now ide., titled in and periodically tested as part of Surveillance Test (ST) procedetes. These ST procedures specifically identify remote head lighting fixtures to ensure complete testing of all types of
- fixtures. Each id?ntified failure will result in generation of an individual work order which will only close upon completior. of the work and re-testing. _These individual work orders will permit tracking and-trending of failures. Individuel failures of tested lighting fixtures will result in failure of the ST procedure. The ST procedure will be_ required to be partially performed upon -
complation of the associated work order and can only be passed upon demonstration of satisfactory performance of all fixtures.
Additionally, the testing methodology pre 6cribed in the ST ,
. procedures has been expanded to include verification of the battery-pack chargers.
i
~ Date When Full Compliance was Achieved Full compliance was achieved upon completion af all repairs and approval of the new ST procedures by August 1, 1991.
i:
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