ML20091M375
| ML20091M375 | |
| Person / Time | |
|---|---|
| Site: | Grand Gulf |
| Issue date: | 05/31/1984 |
| From: | Mcgaughy J MISSISSIPPI POWER & LIGHT CO. |
| To: | James O'Reilly NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| References | |
| REF-PT21-84-312-000 AECM-84-2-0009, PT21-84-312-000, NUDOCS 8406110268 | |
| Download: ML20091M375 (2) | |
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MISSISSIPPI POWER & LIGHT COMPANY Helping Build Mississippi
- N BOX 1640 J ACKSON, MISSISSIPPI 39205 JAMES P. McGAUGHY, JR.
May 31, 1984
..........m U. S. Nuclear Reguls.cory Commission Region 11 101 Marietta Street, N.W.
Suite 2900 Atlanta, Georgia 30303 Attention:
Mr. J. P. O'Reilly, Regional Administrator
Dear Mr. O'Reilly:
SUBJECT:
Grand Gulf Nuclear Station Unit 2 Docket No. 50-417 License No. NPF-13 File 0260/15525/15526/16694.4 PRD-84/04, Interim Report No.
2 for Unit 2, Failure o f ASC0A Deluge Valves AECM-84/2-0009
Reference:
AECM-84/0212, 4/6/84 On March 19, 1984, Mississippi Power & Light Company notified Mr. P.
Fredrickson, of your office, of a Reportable Deficiency at the Grand Gulf Nuclear Station (GGNS). The deficiency concerns the. failure of two Automatic Sprinkler Corporation of America ( ASCOA) deluge valves to open upon receipt of an actuation signal.
Although the fire protectica system deluge valves were procured and installed as non-safety related equipment, the fire protection system for the diesel generator building is included in the MP&L Operational Quality Assurance Program. Due to the possible ef fect on safety related equipment in the diesel generator rooms, MP&L has concluded that the failure of the diesel generator room deluge valves is reportable under the provisions of 10CFR21 for Unit 1.
Determination of reportability for this deficiency for Unit 2 is still under way at this time. We expect to submit a Final Report on Unit 2 by June 14, 1985.
No ASC0A deluge valves have bean received for use on Unit 2.
Our Architect / Engineer has requested Automatic Sprinkler Corporation of America to inspect all Grand Gulf Unit 2 deluge valves for the noted deficiency prior to shipping. Also, an inspection will be performed by our Architect / Engineer once the valves arrive on site for use on Unit 2.
If any deficiency is found, a safety evaluation will be performed at that time.
8406110268 840531 PDR ADOCK 05000416 S
PDR 1C M -
Member Middle South Utilities Systam 47 d M I
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Mr. J. P. 0'Reilly.
AECM-84/2-0009 NRC.
Page 2 Our previous report on Unit I stated that QAR-F-451 would track the deficiency on Unit 2.
This document has been closed and the deficiency is now being tracked by Deficiency Report (DR) 2578.
Yours truly,
$3ee' J. P. NkGaughy, Jr.
KDS:dr cc:
Mr. J. B. Richard Mr. R. B. McGehee Mr. Nicholas S. Reynolds, Esq.
Bishop, Liberman, Cook, Purcell & Reynolds 1200 Seventeenth Street, N. W.
Suite 700 Washington
.D. C. 20036 Mr. Richard C. DeYoung, Director Of fice of Inspection & Enforcement U. S. Nuclear Regulatory Commission Washington, D.C. 20555 Mr. G. B. Taylor South Miss. Electric Power Association P. O. Box 1589 Hattiesburg, MS 39401 e
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