ML20091M375

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Interim Unit 2 Part 21 & Deficiency Rept Re Failure of Automatic Sprinkler Corp Deluge Valves to Open Upon Receipt of Signal.Initially Reported on 840319.Final Rept Expected by 850614.Reportable Under Part 21 for Unit 1
ML20091M375
Person / Time
Site: Grand Gulf  Entergy icon.png
Issue date: 05/31/1984
From: Mcgaughy J
MISSISSIPPI POWER & LIGHT CO.
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
REF-PT21-84-312-000 AECM-84-2-0009, PT21-84-312-000, NUDOCS 8406110268
Download: ML20091M375 (2)


Text

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e MISSISSIPPI POWER & LIGHT COMPANY Helping Build Mississippi

  • . N BOX 1640 J ACKSON, MISSISSIPPI 39205 JAMES P. McGAUGHY, JR. May 31, 1984

..........m U. S. Nuclear Reguls.cory Commission Region 11 101 Marietta Street, N.W.

Suite 2900 Atlanta, Georgia 30303 Attention: Mr. J. P. O'Reilly, Regional Administrator

Dear Mr. O'Reilly:

SUBJECT:

Grand Gulf Nuclear Station Unit 2 Docket No. 50-417 License No. NPF-13 File 0260/15525/15526/16694.4 PRD-84/04, Interim Report No.

2 for Unit 2, Failure o f ASC0A Deluge Valves AECM-84/2-0009

Reference:

AECM-84/0212, 4/6/84 On March 19, 1984, Mississippi Power & Light Company notified Mr. P.

Fredrickson, of your office, of a Reportable Deficiency at the Grand Gulf Nuclear Station (GGNS). The deficiency concerns the. failure of two Automatic Sprinkler Corporation of America ( ASCOA) deluge valves to open upon receipt of an actuation signal.

Although the fire protectica system deluge valves were procured and installed as non-safety related equipment, the fire protection system for the diesel generator building is included in the MP&L Operational Quality Assurance Program. Due to the possible ef fect on safety related equipment in the diesel generator rooms, MP&L has concluded that the failure of the diesel generator room deluge valves is reportable under the provisions of 10CFR21 for Unit 1.

Determination of reportability for this deficiency for Unit 2 is still under way at this time. We expect to submit a Final Report on Unit 2 by June 14, 1985.

No ASC0A deluge valves have bean received for use on Unit 2. Our Architect / Engineer has requested Automatic Sprinkler Corporation of America to inspect all Grand Gulf Unit 2 deluge valves for the noted deficiency prior to shipping. Also, an inspection will be performed by our Architect / Engineer once the valves arrive on site for use on Unit 2. If any deficiency is found, a safety evaluation will be performed at that time.

8406110268 840531 PDR ADOCK 05000416 -

S PDR 1C M - I Member Middle South Utilities Systam 47 d M

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Mr. J. P. 0'Reilly. AECM-84/2-0009 NRC. Page 2 Our previous report on Unit I stated that QAR-F-451 would track the deficiency on Unit 2. This document has been closed and the deficiency is now being tracked by Deficiency Report (DR) 2578.

Yours truly,

$3ee' J. P. NkGaughy, Jr.

KDS:dr cc: Mr. J. B. Richard Mr. R. B. McGehee Mr. Nicholas S. Reynolds, Esq.

Bishop, Liberman, Cook, Purcell & Reynolds

, 1200 Seventeenth Street, N. W.

Suite 700 Washington .D. C. 20036 Mr. Richard C. DeYoung, Director Of fice of Inspection & Enforcement U. S. Nuclear Regulatory Commission Washington, D.C. 20555 Mr. G. B. Taylor South Miss. Electric Power Association P. O. Box 1589 Hattiesburg, MS 39401 e

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