ML20087M704

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Monthly Operating Repts for Feb 1984
ML20087M704
Person / Time
Site: Saint Lucie, Hope Creek, Turkey Point, 05000000
Issue date: 03/15/1984
From: Grant N
FLORIDA POWER & LIGHT CO.
To:
Shared Package
ML20087M691 List:
References
NUDOCS 8403300185
Download: ML20087M704 (16)


Text

.

AVER AGE DAILY UNIT POWER LEVEL DOCKETNO. 50-250 UNIT Turkey Point #3 DATE 3-15 A4 COMPLETED BY N.W, Grant TELEPilONE (305) 552-3675 MONTH February, 1984 DAY AVER ACE DAILY POWER LEVEL DAY AVER AGE DAILY POWER !.EVEL (MWe Net)

-(MWe Net) 1 6RS 17 684 2

88 679 3

19 680 4

5 682 21 684 6

22 7

688 23 690 263 8

24 689 687 9

25 10 688 26 688 687 555 11 27 177 12 28 601 13 29 680 14 30 15 679 31 16 255 INSTRUCTIONS On this forinat.hst the average daily uinit power lesel in MWe Net for each day sit the reporting mont!. Compute to the nearest whole twgawart.

(9/77) h A

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OPER ATLNG DATA REPORT DOCKET NO. _5n 7sn DATE.t14 M COMPLETED BY 11.E Grant TELEPHONE (105) 552-3675 OPERATlh G STATUS 1' Unit N***

Turkey Point Unit #3 Notes

2. Reporting l en. d. February, 1984 Unit #3 operated at power except as indicated in o
3. Licensed Thermal Power (MWI):

?,200 the " Unit Shutdowns and Power

4. Nameplate tating (Gross MWe):

76n Reductions" Report.

S. Design Electrical Rating (Net MWe):

693

6. Maximum liependable Capacity (Gross MWe):

700 666

7. Maximum I ependable Capacity (Net MWe):
8. If Changes )ccur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasanc
9. Power Leul To Which Restricted,if Any (Net MWe):
10. Reasons For Restrictions,if Any:

This Month Yr..to-Date Cumulatise

11. Hours In Reporting Period 696 1.440 98.505.6
12. Number Of Hours Reactor Was Critical 446.1 1,049.2 67,355.4
13. Reactor Re.erve Shutdown Hours 0

0 844.4

14. Hours Gent rator On Line 417.R 076 7 66 RQR 6
15. Unit Resers e Shutdown flours 0

0 121.8

16. Gross Ther nal Energy Generated (MWil) 943.756 1.992.922 137;481.514
17. Gross Elect-ical Energy Generated (MWH) 306.200

, _, 600,816 41,513,833 640,265 43,850,830

18. Net Electri,al Energy Generated (MWH) 287,728
19. Unit Servie Factor 62.1 67.8 67.9
20. Unit Avails >ility Factor 67 1 67 R 6R.0
21. Unit Cage ty Factor (Using MDC Net) 62.1 62.6

@.1

22. Unit Capac ty Factor (Using DER Net) 59.7 60.2 60.8
23. Unit Force i Outage Rate 37.9 22.9 5.7 _
24. Shutdown > Scheduled Over Next 6 Months (Type. Date,and Duration of Each):
25. If Shut Do n At End Of Report Period. Estimated Date of Startup:

March 3,1984 (actual)

26. Units In Te st Status (Prior to Commercial Operation):

Forecast Achiaed i

INITIA L CRITICALITY INITIAL ELECTRICITY COMMERCIAL. OPERATION (9/771

UNITSilVTDOWNS AND POWER REDUCTIONS DOCKET NO.

50-250 UNIT NAME Turkey Point Unit #3 DATE 3-15-84 COMPLETED BY N 1J. Grant REPORT MONT1{

Fohrna ry, 1984 TELEPHONE (305) 552-3675 3

-f4 3E

}

hYk Licensee 5%

Cause & Currective Dale g

g jg5 Event p?

c?

Action to

$5 E

j5g Report a nC 0

H Preveni Recurrence 0

I

'98 840212 F

18.4 A

3 250-84-06 EB RELAYX Electrical relay malfunction caused loss of power supply to main feed pump which resulted in a reactor trip.

Unit was returned to service.

~09 840216 F

'195.2 A

3 250-84-07 EB RELAYX While preparing to make repairs to a breaker, a relay was jarred which caused -the loss of the power supplies.

to feed and consendate pumps. This resulted in a reactor trip. The unit remained out of service for a complete investigation.

10 840227 F

49.9 A

1 EB RELAYX The unit was removedfrom service to inspect, adjust and repair. auxillary power air, circuit breakers.

i.

'l 2

3 4

[

f: Forced Reason:

Method:

Exhibit C. instructions S Scheduled A Lyuipment Failure (Explain) 1 Manual for Preparation of Data B Maintenance of Test 2 Manual Scram.

Entry Sheets for Licensee C. Refueling 3 Automatic Scram.

Event Report (LER) File (NUREG-D Regulatory Restriction 9 OLher (Explain) 0161)

I! Operator Training & Ucense Examination F Adnumstrative p

5 C-Operational Erior (F splain) 4-. p a. 44ew.i..#

Exhibit i. Same Source 69/77).

Il Other (Explain)

SUMMARY

OF OPERATING EXPERIENCE 50-250 DOCKET NO.

Turkey Point Unit #3 DATE March 15.1984 COMPLETED BY N.W. Grant TEI,EPHONE (305) 552-3675 REPORT MONTH February,1984 Unit #3 operated at essentially full power except as indicated in the

" Unit Shutdowns and Power Reduction" Report.

Inspections and requirements of IE Bulletins and NUREG-0737 are continuing.

Florida Power & Light Company commitments for NUREG-0737 implementation are continuing. Refer to correspondence between FPL and NRC for additional in-formation.

AVERAGE DAIL) UNil POWER LEVEL DOCKET NO.

50-251 UNIT Turkey Point #4 DATE L18i Ra COMPLETED BY N.W. Grant TELEPilONE f7ngi sq9 1675 February, 1984 MONm DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL IMWe Net)

-(MWe-Net) 686 3

,7 2

688 18 3

684 19 681 4

20 S

6R1 23 6

685 22 689 7

23 8

689 24 598 9

690 685 25 685 684 no 26 685 532 33 p

264 12 28 88 13 29 14 674 30 675 15 3!

251 16 INSTRUCTIONS -

On this format.hst the average daily unit power leselin M Ve Sei for each day in the reporting month. Compute to the nearest whole twgawatt.

I (9/77)

OPERATING DA (A REPORT DOCKET NO.

50-251 DATE.3-15-84 COMPLETED BY fl.W. Grant TELEPHONE hnq i 487-3675 OPERATING STATUS Turkey Point Unit #4 Notes

1. Unit Nanm teoruary, 1964 Unit 4 operated at power ex-
2. Reporting Pen. d:

o cept as indicated in the "

3. Licensed Thermal Power (MWI):

2.200

" Unit Shutdowns and Power

4. Nameplate Rating (Gross MWe):

760

~

Reductions" Report.

693

5. Design Electrical Rating (Net MWe):
6. Maximum Dependable Capacity (Gross MWe):
7. Maxirnum Dependable Capacity (Net MWe):
8. If Changes Occur in Capacity Ratings (Items Number 3 Throup 7) Since I.ast Report.Give Reasons:
9. 'ower Level To which Restricted.lf Any (Net MWe):
10. Reasons For Restrictions,if Any:

This Month Yr to Date Cinnulatise

11. Hours in Reporting Period 646_

1; dan

_gg,733

12. Number Of Hours Reactor Was Critical 472.0 1.201.1 6s n39 7

~ I66.6

13. Reactor Reserve Shutdown Hours 0

0

14. Hours Generator On-Line 434.3 1,157.9 63,626.0 U
15. Unit Reserve Shutdown 1(ours

-0 31.2 1

4,bzz,918 134,269,659

16. Gross Thermal Energy Generated (MWii)
17. Gross Electrical Energy Generated (MWH) 303.040__,_.

821.410 42.742,719

18. Net Electrical Energy Generated (MWH) 283,309 777.469 40.dS1.528
19. Unit Service Factor 62.4 80.4 69.0 62 4 80.4 69.0
20. Unit Availability Factor
21. Unit Capacity Factor (Using MDC Net) 6111 R1 1 67,g
22. Unit Capacity Factor (Using DER het) 58.7 77.9 63_3
23. Unit Forced Outage Rate 37.6 19.6 4.7
24. Shutdowns Scheduled Oser Next 6 Months (Type. Date.and I uration of Each):
25. If Shut Down At End Of Report Period. Estimated Date of St.rtup.

April 30.1984

)

26. Units in Test Status (Prior to Commercial Operation):

Forecast Achiaed INITIA L CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPER ATION I

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DOCKET NO.50-251 UNITSilUTDOWNS AND POWER REDUCTIONS UNITNAME urkey Point Unit #4 T

DATE3-15-84 COMPLETED BY N.W. Grant REPORT MONTil February, 1984 TELEPHONE (305) 552-3675 a

1

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Licensec Eg Cause & Corrective No.

Date g *3=

i 2is Event g

p Action to g'

fE E

jgg Repor a mV H

P; event Recurrence l

6 I

02 840212 F

8.4 A

1 251-84-01 EB RELAYX Electrical relay malfunction caused loss of power supply to main feed I

o pump which resulted in a reactor trip.

l Unit was returned to service.

03 840212 F

19.4 A

3 251-84-02 EB RELAYX High steam flow signal and an actual steam generator low level resulted in a reactor trip. The malfunctioning transmitter was replaced. Unit was returned to service.

04 840216 F

182.7 A

3 251-84-03 EB RELAYX While preparing to make repairs to a breaker, a relay was jarred whith caused the loss of the power supplies-to feed and condensate pumps. This resulted in a reactor trip.- The unit remained out of service for a com-plete investigation.

.05 840227 F

51.2 A

1 EB RELAYX The unit was removed from service to inspect, adjust and repair auxillary power air circuit Dreaxers.

1 2

3 4

f: Forced Reason:

Method:

Ex.hibit C. Instructions S. Scheduled A Equipment Failure (Explain) 1-Manual for Preparation of Data B Maintenance or Test 2 Manual Scram.

Entry Sheets for Licensee C. Refueling 3 Automatic Scram.

Event Report (LER) File (NUREG.

D Regulatory Restriction c}-Other (Explain) 01611 E-Operator Training & License Examination F Administrative p

5 G-Operational Error (F splain) 4-. /.o e

4. cove y..cl Exhibii I. Same Si.uree (9/77)

Il Olher (Explain)

SUMMARY

OF OPERATING EXPERIENCE DOCKET NO.

50-25,1 UNIT Turkey Point Unit #4 DATE March 15, 1984 N.W. Grant COMPLETED BY TELEPHONE (305) 552-3675 REPORT MONTH Februa ry,1984 Unit 4 operated at essentially full power except as indicated in the " Unit Shutdowns and Power Reductions" Report.

Inspections and requirements of IE Bulletins and.NUREG-0737 are continuing.

Florida Power & Light Company commitments to NUREG-0737 implementation are continuing. Refer to correspondence between FPL and NRC for additional in-forma tion.

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AVERAGE DAILY UNIT POWER LEVEL 50-335 DOCKET NO.

UNIT St. Lucie Unit #1 DATE 3-15-84 COMPLETED BY Nu n,2n+

TELEPilONE (305) 552-3675 MONm __ February,1984 DAY AVE.l AGE DAILY POWER LEVEL DAY AVER AGE DAILY POWER LEVEL IMWe Net)

-(MWe-Net i 1

17 2

l8 3

19 4

20 S

21 6

22 7

23 8

9 25 10 26 Ii 27 12 28 13 29 14 30 15 31 16 INSTRUCTIGNS On this funna.! sr the average daily unit power leselin MWe Net for each day in the reporting nwnth. Compute to the nearest wi ole megawait.

(9/771

OPERATING DATA REPORT 50- 335 DOCKET NO.

DATE _ 3-15-84 COMPLETED IlY N W_ Grant TELEPHONE (3ng) 442-3675 OPERATING STATUS St. Lucie Unit #1 Notes I. Unit Name:

February, 1984

2. Reporting Pericd:

Unit #1 remained out of

3. Licensed Therma! Power (MWI):

2700 Service for refueling and

4. Nameplate Rating (Gross MWe):

890 scheduled maintenance.

830

5. Design Electrical Rating (Net MWe):
6. Maximum Dependable Capacity (Gross MWe):

ogy

7. Maximum Dependable Capacity (Net MWe):

R99

8. If Changes Occur in Capacity Ratings (items Number 3 Through 7) Since Last Report, Give Reasons:

i

9. Power Lesel To Which Restricted,If Any(Net MWe):
10. Reasons For Restrictions.If Any:

This Month Yr..to Date Cumulatise

11. Hours In Reporting Period 696 1440 63,048 0

0 44.466.I

12. Number Of Hours Reactor Was Critical
13. Reactor Reserve Shutdown Hours 0

0 205.3

14. Hours Generator On.Line 0

0 43,576.2

15. Unit Reserve Shutdown 1(ours 0

0 39.3

16. Gross Thermal Energy Generated (MWil) 0 0

108,667,938

17. Gross Electrical Energy Generated (MWH) n n

tg,171,n75

18. Net Electrical Energy Generated (MWH) 9 744 85 4Rfi 33.3?8.787
19. Unit Service Factor

~

0 0

69.1

20. Unit Availability Factor 0

0 69.2

21. Unit Capacity Factor (Using MDC Net) 0 0

67.0

22. Unit Capacity Factor (Using DER Net) 0 0

65 1

23. Unit Forced Outage Rate 0

0 4d_

24. Shutdowns Scheduled Oser Next 6 Months (Type. Date.and Duration of Each):
25. If Shut Down At End Of Report Period. Estimated Date of Startup:

Snring _ 1984 i

26. Units in Test Status (Prior to Commercial Operation):

Forecast Achiesed i

l lNITIA L CRITICALITY l

lNITIAL ELECTRICITY COMMERCIAL OPERATION (9/77) 1

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v UNITS!!UTDOWNS AND POWER REDUCTIONS DOCKET NO.

50-335 UNIT NAME St. Lucie Unit #1 DATE 3-15-84 COMPLETED BY N.W. Grant REPORT MONT11 Februarv,1984 TELEPHONE (305) 552-3675

  • 3 -a 3 E

~

=

e.

Licensee E,

$4 Cause & Corrective N...

Daie F-k

?y3 Event g

7

-7 gL g,j9, 52 U

6 y a:

g g3 y Report in v Prevent Recurrence o

x C

,3 830226 S

696.0 C

4 RC FUELXX Unit #1 remained out of service for refueling and scheduled maintenance.

l l

l 3

4 f:- Forced Reason:

Method:

Exhibit C - tastructions S. Scheduled A Equipment Failure (Explain) 1-Manual for Preparation of Data B Maintenance of Test 2-Manual Scram.

Entry Sheets for Licensee C Refueling 3 Automatic Scram.

Event ReporI (LER) Fde (NUREG-D Regulatory Restriction q-Other (Explain) 01611 li Operator Training & License Examination F Administrative Y~

O'****""#'

5 G-Operational lirrur (F splain)

4. j., ao ezzove,,,..e#

Exhibit I. Same Source l'8/77)

Il Other (Explain)

1 StTMMARY OF OPERATING EXPERIENCE DOCKET HO.

50-335 UNIT

.St. Lucie' Unit 1 DATE March 15, 1984

. Grant COMPLETED BY TELEPHONE (305) 552-3675 REPORT HONTH Februa ry,1984 St. Lucie Unit I remained out of service for a refueling and maintenance outage.

Inspections and requirements of IE Bulletins and NUREG-0737 are centinuing.

Florida Power & Light Company commitments for NUREG-0737 implementation are continuing. Refer to correspondence between FPL and NRC for additional in-formation.

In accordance with requirements of NUREG-0737 Item II.K.3.3, there were no challenges to PORV or safety valves during the report month.

See correspondence between FPL and NRC for information concerning the thermal shield.

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l AVERAGE Dally UNIT POWER LEVEL i

i DOCKET NO.

850-3gg UNIT St. Lucie Unit #2 3-15-84 DATE COMPLETED BY N.W. Grant TELEPHONE (305) 552->3675 f*brUBry, 1984 MONTH DAY AVER AGE DAILY POWER LEVEL DAY AVER AGE DAILY POWER LEVEL IMWe Net)

.(MWe-Net!

819 815 I

I, 816 816 2

18 818 815 3

19 81 8 814 4

20 5

817 21 814 809 813 6

22 766 816 7

23 819 816 g

24

=

352 Ol' 25 516 817 10 26 816 817 y,

817 817 12 28 819 818 33 29 818

,4 30 789 15 33 815 16 INSTRUCTIONS On this fonnat. Int the avenge daily unit power lesel in MWe-Nei for each day in the reporting nwnth. Compute to the nearest whole megawatt.

(9/771

OPERATLNG DATA REPORT DOCKET NO.

~50-389 DATE._3-15-84 COMPLETED BY _ N.W. Grant TELEPHONE.__.(305 ) 552-3675 OPERATING STATUS St. Lucie Unit #2 Notes I. Unit Name:

Unit #2 operated at

2. Reporting Period:

Fe brua ry. 1984 essentially full power except

3. Licensed Thermal Power (MWt):

2.500 as indicated in the " Unit 850

4. Nameplate Rating (Gross MWe):

Shutdown and Power Reductions 804

5. Design Electrical Rating (Net MWe):

Report.

6. Maximum Dependable Capacity (Gross MWe):
7. Maximum Dependable Capacity (Net MWe):

7R6

8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since last Report.Give Reason :
9. Power Lesel To which Restricted.lf Any (Net MWe):
10. Reasons For Restrictions,if Any:

This Month Yr to.Date Cmmilatise 696 1.440 4,945 II. Hours in Reporting Period I 'D *

12. Number Of Hours Reactor Was Critical
13. Reactor Reserve Shutdown Hours 0

0 0

14. Hours Generator On-Line 684.5 1,285.6 4,416.0
15. Unit Reserve Shutdown Qours 9

9

_g

16. Gross Thermal Energy Ger.erated (MWil)

(721 006 1,107,631 10 RRG,574-

17. Gross Electrical Energy Generated (MWH)

R7R,R10 1 ;n76 ;5 40 3;618;750

18. Net Electrical Energy Generated (MWH) 547.789 1.013.681 3.411.267
19. Unit Service Factor 98.3 89.3 89.3
20. Unit Availability Factor 98.3 89.3 89.3
21. Unit Capacity Factor (Using MDC Net) 100_1 no 6 R7 R
22. Unit Capacity Factor (Using DER Net) 07 4 R7_6

_85_8

23. Unit Forced Outage Rate 1.7 8.8 10.2
24. Shutdowns Scheduled Oser Next 6 Months (Type. Date.and Duration of Each):
25. If Shut Down At End Of Report Period. Estimated Date of Startup:
26. Units in Test Status (Prior o Commercial Operation):

Forecast Ai-hi sed INITIA L CRITICALITY INITIA L ELECTRICITY COMMERCIAL OPERATION (Y71

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i 50-389 UNIT Sl'UTDOWNS AND POWER REDUCTIONS DOCKET NO.

UNIT NAME St. Lucie Unit #2 DATE 3-15-84 I

COMPLETED BY N W. Grant REPORT MONT1{ Februa rv.1984 TELEPHONE (305) 552-3675 l

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254 Licensee e*L Cause & Currectise

=

s -. =

cv, g

i, 3=

j

,;; g 5 Event s?

No.

Date q'

Action to

$E E

j5y Report =

80 Prevent Recurrence c

o06 840209 F

11.5 A

3 389-84-04 HH PUMPXX Main feedwater pump tripped due to low suction pressure, resulting in reactor trip. A vent problem with the condensate pumps was the cause.

i The design is being changed to pre-vent recurrence.

07 840209 F

0.0 H

5 HH ZZZZZZ High steam generator chloride level caused power reduction.

I 2

3 4

l T: Forced Reason:

Method:

Exhibit G Instructions S Scheduled A Lyuipment Failure (Explain) l-Manual for Preparation of Data B-Maintenance of Test 2 Manual Scram.

Entry Sheets for Licensee

(*. Refueling 3 Automatic Scram.

Event Report (LER) File (NUREC-D Regulatory Restriction 9-Other (Explain) 01611 li4)perator Training & Licene Examination F Administrative 5

G. Operational Error (Fiplain) 4- _ 4. aa 44ouc;,..d Exhibit I Same Source t'8/77)

Il Other (Explain)

,_ = _

SUMMARY

OF C" EIMTING EXPERIENCE I

DOCKET NO.

50-389 IfMIT St. Lucie' Unit _(2

)) ATE March 15,1984 COMPLETED BY N.W. Grant (305) 552-3675 TELEPH )NE 4

i REPORT I40 NTH February,1984 Unit 2 operated at essentially full power except as indicated in the " Unit Shutdowns and Power Reductions" Report.

1 Inspections and requirements of IE Bulle tins and NUREG-0737 are continuing.

Florida Power & Light Company Commitments for NUREG-0737 implementation are continuing. Refer to correspondence between FPL and NRC for additonal in-formation.

In accordance with requirements of Technical Specification 6.9.1.6. there were no challenges to PORV or safety valves during the r'oport month.

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