ML20087M591

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Monthly Operating Rept for Feb 1984
ML20087M591
Person / Time
Site: Ginna Constellation icon.png
Issue date: 02/29/1984
From: Dodge R, Snow B
ROCHESTER GAS & ELECTRIC CORP.
To:
NRC OFFICE OF RESOURCE MANAGEMENT (ORM)
References
NUDOCS 8403300081
Download: ML20087M591 (6)


Text

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OPERATlHG DATA REPORT DOCKET NO.

50-244 DATE Marc,h 10, 1984 COMPLETED BYhm/u[N[h Robert E. Dodge TELEPilONE 1 (315) 524-4446 OPERATING STATUS Ext. 396 at.Ginna

1. Unit Name:

GINNA STATION. UNIT #1 Notes The reactor power level

2. Reporting Period: February, 1984 was maintained at 100% for the 1520 majority of the report month.
3. Licensed Thermal Power (Mit):

490

4. Nameplate Rating (Gross MWe):

Exceptions are detailed 470

5. Design Electrical Rating (Net MTe):

p 4,

490

6. Maximum Dependable Capacity (Gross MTe):
7. Maximum Dependable Capacity (Net MTe):

470

8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
9. Power Level to Thich Restricted, If Any (Net MTe):
10. Reasons For Restrictions, If Any:

This Month Yr.-t o-Da te Cumulative

11. Ilours In Reporting Period 696 144n 19; n16
12. Number of flours Reactor Tas Critical 696 1440 95.039.98 0

0 1.631.32

13. Reactor Reserve Shutdown flours 696 1440 92,951.63
14. Ilours Generator On-Line 0

0 8.5'

15. Unit Reserve Shutdown llours
16. Gross Thermal Energy Generated (MTil) 1.027.536 2,142,528 128 199;R97 341,611 712,460 41,876,830
17. Gross Electrical Energy Generated (MTil)
18. Net Electrical Energy Generated (MTil) 324,804 677;767 10 7na,n19 100%

100%

74.35%

19. Unit Service Factor 100%

100%

74.36%

20. Unit Availability Factor 99.29%

100.14%

69.35%

21. Unit Capacity Factor (Using MDC Net) 99.29%

100,14%

69.35%

22. Unit Capacity Factor (Using DER Net) 0.00%

0.00%

7.90%

23. Unit Forced Outage Rate
24. Shutdowns Scheduled Over Next 6 Months (Type, Date and Duration of Each):

?

March 3, 1984 - Annual Refueling and Maintenance - Approximately 65 days duration

25. If Shut Down At End Of Report. Period, Estimated Date of Startup:
26. Units in Test Status (Prior to Commercial Operation):

Forecast Achieved l

INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION 8403300001 840229 PDR ADOCK 05000244 R

PDR

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AVERAGE DAILY UNIT POWER LEVEL CCCELT 1.0.

50-244 UNIT

$1, Cinna Station DATE Marsh 10,_

1984 CCMPLLTLD BY / ), L / C /_#c4 y

%dbert L.

Loc @

TELEPHONL 1 (315) 524-4446 Ext. 396 at Ginna MONTH February, 1984 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (Mie-Ne t)

(Mbe-Net) 1.

477 17.

476 2.

478 18.

475 3.

479 19.

301 4.

479 20.

472 5.

479 21.

474 6.

479 22.

428 7.

478 23.

476 8.

478 24.-

464 9.

480 25.

465 10, 479 26.

'464 11.

478 27.

463 12.

478 28.

462-136 478 29.

460 14.

478 30.

15.

477 31.

16~.

476 INSTRUCTIONS

~

On this format, list.the average daily : unit power level 'in hbe-Net for-cach day'in the rcrorting: month.

Ccrapute to the nearest whole mcgawatt.

Yg

q DOCKET NO.

50-244 UNIT NAME #bGiina Station UNIT SHUTDOWN AND POWER REDUCTIONS nATE *I9? We N COMPLETED 11Y [llMC 47g,

'Rdbert E. Dodge r REPORT MONTH February TELEPIIONE 1 (315) 524-4446

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Ext. 396 at--G1nna n

IE Licensee a

Cause & Corrective Eq g

Event f,g Me.

De't.

g jg

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Action to F-dE

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R* Pert #

Au u

Prevent Reevrrence e

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O PR*

2-18-84 F

5.4 IIRS A

N/A N/A SF ACCUMU Power Reduction due to S.I. Accumulat 3r Low Pressure PR*

2-22-84 F-3.1 HRS, A N/A N/A IIB PIPEXX Power Reduction due to 2B Reheater Steam Leak PR*

2-24-84 S

N/A C

N/A N/A Coastdown Commenced PR*

2-24-84 F

2 HRS.

A N/A N/A 1111 XXXXX Power Reduction due to Loss of l

A and B lleater Drain Tank Pumps 1

2 3

4 F: Forced Reason:

  • Power Reduction Method:

Exhil;it G - Instructions S: Scheduled A-Equipment Failure (Explain) 1-Manual for Preparation of Data B-Maintenance or Test 2-Manual Scram.

Entry Sheets for Licensee C-Refueling 3-Automatic Scram.

Event Report (LER) File (NUREG-D-Regulatory Restriction 4-Other (Explain) 0161)

E-Operator Training ac License Examination F-Administrative 5

E G-Operational Error (Explain) as-se inav. um H-Other (Explain)

Exhibit 1 - Same Source L.

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NARRATIVE

SUMMARY

OF OPERATING EXPERIENCE LOCKET NO.

50-244 UNIT Cinna Staticn,Unital CATE I:p,.2;ch 10, 1984 CCl4PLETED BY p M / h Robert E. Eccg(

TELEFHCNE 1 (315) 524-4446 EXT. 396 at Ginna MONTH February, 1984 The reactor pcter level was niaintained at 1001 for the tajcrity of the report pericd, with the follcwing exceptions:

On 2/18, reactor pcker level reducticn was cenacnced to hot shutdekn as required by-Technien1 Specifications, due to S.I. Accumulator Low Pressure, the lcwest power achievcd was 30t.

The power level was

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restored-to 100% cn 2/19 after S.I. Accumulator Vent Valve was secured and capped, and S.I.

Accetulater Pressure increaccd above Technical Specification requircments.

On 2/22, the rcactor power level was reduced'to ~ 68% due to 2B Echeater steam leak.

The power level was restored to 100% after repair of steam leak at 2145 hours0.0248 days <br />0.596 hours <br />0.00355 weeks <br />8.161725e-4 months <br /> on 2/22.

~

On 2/24, at 0800 hours0.00926 days <br />0.222 hours <br />0.00132 weeks <br />3.044e-4 months <br /> ccnnonced coastdcun operation.

On 2/24, at approximately 0830 the reactor power level was reduced to 85% due to loss of "A" and "B" Header Drain Tank Pumps. The pcwcr level was restored at approximately 1030.cn 2/24.

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i Page 5 GINNA STATION Maintenance Ileport S umir,z.ry February, 1984 During the Ir.cnth of February, routine insl.cctions and n.ain-tent.nce were c cnil. l e t e d.

Also, preparations were underway for the shceduled 1984 Refueling Outage.

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4 ROCHESTER GAS AND ELECTRIC CORPORATION

  • 89 EAST AVENUE, ROCHESTER, N.Y.146 9 e

TELEPwoNE A.E 4 CODE 716 546 2700 GIhEA STATION March 10, 1964 Director, Office of Management Inforr;ation and Prograra Analysis U.S. NUCLLAR REGULA'IOhY COMMISSICN bashington, EC 20555

Subject:

Monthly Report for February, 1984 Operating Status Inforr.ation R.

E. Ginna.Euclear Power Plant Unit No. 1 Locket No. 50-244 Ecar Sir:

Pursuant to our Technical Specification 6.9.1, attached herewith is the conthly operating status report for Ginna Station for the n.onth of February, 1984 i f; e

Very truly yours, Br ce A. Snow Plant Superintendent

'EAS/clb Attachraents

_cc:

Dr. Thomas E. Murley.Nhc (1)

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