ML20087H306
| ML20087H306 | |
| Person / Time | |
|---|---|
| Site: | Davis Besse |
| Issue date: | 07/31/1995 |
| From: | Wolf G, Jeffery Wood TOLEDO EDISON CO. |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| KB-95-0121, KB-95-121, NUDOCS 9508180010 | |
| Download: ML20087H306 (5) | |
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TOLEDO EDISON A Centerior Energy Cornpany E
1 August 14, 1995 KB-95-0121 Docket No. 50-346 License No. NPF-3 U.S. Nuclear Regulatory Commission Document Control Desk Vashington, D.C.
20555 Gentlemen:
Monthly Operating Report, July, 1995 Davis-Besse Nuclear Power Station Unit 1 Enclosed are ten copies of the Monthly Operating Report for Davis-Besse Nuclear Power Station Unit No. 1 for the month of July, 1995.
If you have any questions, please contact G. M. Wolf at (419) 321-8114.
Very truly yours, John K. Wood i
Plant Manager Davis-Besse Nuclear Power Station GMW/dmc Enclosures cc:
L. L. Gundrum NRC Project Manager H. J. Hiller Region III Administrator f
S. Stasek
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NRC Senior Resident Inspector, Stop 4030 e
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AVERAGE DAILY UNIT POWER LEVEL
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DOCKET NO.
50-0346 UNIT Davis-Besse Unit 1 l
DATE August 2,1995 COMPLETED BY Gerald M. Wolf 7
TELEPHONE 419/321-8114
. MONTH July,1995 AVERAGE DAILY POWER LEVEL AVERAGE DAILY POWER LEVEL DAY (MWe-Net)
DAY (MWe-Net) l 1
878 17 871 2
881 18 863 3
879 19 875 4
872 20 873 5
868 21 874 3
6 870 22 872 7
876 23 872 8
880 24 873 9
844 25 873 10 876 26 872 11 875 27 871 12 874 28 867 13 865 29 870 l
14 863 30 873 15 863 31 871 16 869
OPERATING DATA REPORT 1
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- DOCKET NO 50-0346 DATE August 2,1995 COMPLETED BY Gerald M. Wolf TELEPHONE 419/321-8114 OPERATING STATUS
- 1. Unit Name: Davis-Besse Unit 1 Notes
- 2. Reporting Period July,1995
- 3. Licensed Thermal Power (MWt) 2772
- 4. Nameplate Rating (Gross MWe) 925
- 5. Design Electrical Rating (Net MWe) 906
- 6. Maximum Dependable Capacity (Gross MWe) 913
- 7. Maximum Dep_endable Capacity (Net MWe) 868
- 8. If Changes Occur in Capacity Ratings (items number 3 through 7) since last report, give reasons:
9.
Power Level To Which Restricted, if Any (Net MWe):
- 10. Reasons For Restrictions, if Any (Net MWe):
This Month Yr-to-Date Cumulative
- 11. Hours in Reporting Period 744.00 5,087.00 149,040.00
- 12. Number Of Hourt Reactor Was Critical 744.00 5,087.00 95,032.77
- 13. Reactor Reserve Shutdown Hours 0.00 0.00 5,532.00
- 14. Hours Generator On-Line 744.00 5,087.00 92,777.90
- 15. Unit Reserve Shutdown Hours 0.00 0.00 1,732.50
- 16. Gross Thermal Energy Generated (MWH) 2,058,376 13,995,650 _240,091,723
- 17. Gross Electrical Energy Generated (MWH) 681,329 4,682,633 77,754,122
- 18. Net Electrical Energy Generated (MWH) 648,101 4,455,161 73,366,530
- 19. Unit Service Factor 100.00 100.00 62.25
- 20. Unit Availability Factor 100.00 100.00 63.41
- 21. Unit Capacity Factor (Using MDC Net) 100.36 100.90 56.71
- 22. Unit Capacity Factor (Using DER Net) 96.15 96.67 54.33
- 23. Unit Forced Outage Rate 0.00 0.00 18.95
- 24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):
- 25. If Shut Down At End Of Report Period, Estimated Date of Startup:
- 26. Units in Test Status (Prior to Commercial Operation):
Forecast Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION l
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SUMMARY
July 1995 Reactor power was maintained at approximately 100 percent full power until 0000 hours0 days <br />0 hours <br />0 weeks <br />0 months <br /> on July 9,1995, when a manual power reduction was initiated to perform control valve testing. Power was manually reduced to approximately 94 percent full power by 0015 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br />, and the testing was conducted. At the completion of testing at 0035 hours4.050926e-4 days <br />0.00972 hours <br />5.787037e-5 weeks <br />1.33175e-5 months <br />, reactor power was j
reduced at the request of the load dispatcher. The power reduction was stopped at 0045 hours5.208333e-4 days <br />0.0125 hours <br />7.440476e-5 weeks <br />1.71225e-5 months <br /> with reactor power at approximately 90 percent full l
power. At 0830 hours0.00961 days <br />0.231 hours <br />0.00137 weeks <br />3.15815e-4 months <br />, reactor power was gradually increased to l
approximately 100 percent full power, which was achieved at 1000 hours0.0116 days <br />0.278 hours <br />0.00165 weeks <br />3.805e-4 months <br />.
Reactor power was maintained at approximately 100 percent full power until 0439 hours0.00508 days <br />0.122 hours <br />7.258598e-4 weeks <br />1.670395e-4 months <br /> on July 18, when a manual power reduction was initiated to perform maintenance on high pressure feedwater heater 1-4 normal j
drain valve. Power was manually reduced to approximately 93 percent full power by 0600 hours0.00694 days <br />0.167 hours <br />9.920635e-4 weeks <br />2.283e-4 months <br />, and the valve was isolated. At the completion of maintenance at 0818 hours0.00947 days <br />0.227 hours <br />0.00135 weeks <br />3.11249e-4 months <br />, reactor power was gradually increased to approximately 100 percent full power, which was achieved at 0924 hours0.0107 days <br />0.257 hours <br />0.00153 weeks <br />3.51582e-4 months <br />.
f Reactor power was maintained at approximately 100 percent full power for the rest of the month.
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