ML20086L188

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Forwards Sequoyah Nuclear Plant Unit 1,Cycle 5 Refuleing Outage Oct - Dec 1991, Per NRC 911119 Request.Rept Consists of Tubes Plugged in Each Sg,Results of SG Tubes in-service Insp & Results of Unit 1 Tube Degradation Investigations
ML20086L188
Person / Time
Site: Sequoyah 
Issue date: 12/09/1991
From: Joshua Wilson
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
Shared Package
ML20086L191 List:
References
NUDOCS 9112160087
Download: ML20086L188 (2)


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anAAA AAd, W mN e h x m r,aUrom k.o em J L W uon we nesent t %me taur ne December 9, 1991 U.S. Nuclear Regulatory Commission ATTN:

Docament Control Desk Washington,ED.C.

20555 3entlemen:

In the Mct:er of

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Docket No. 50-327 Tennessee Valley Authority

)

SEGUGYAH VUCLEAR PLANT (SQN) - UNIT 1 - SPECIAL REPORT ON STEAM GENERATGR (5/G) ACTIVIT!ES COMPLETED DURING THE UNIT l CYCLE 5 REFUELING QUTAGE

Reference:

IVA letter to NRC dated Jecember 2, ~1991 "Special Report on Steam Generator (SG) Tube Inspections That Fall Into Category C-3" In accordance with-the requirements of the SQN Unit 1 Technical

- Specification (TS) paragraphs 4.4.5.5(a), (b), and (c), and as requested by the NRC staff November 19, 1991, enclosed is a report including the number of tubes plugged in each S/G the results of the S/G tubes in-service inspection completed November 24.-1991, the results of investigations conducted to determine the cause of the SQN L' nit 1 S/G tube deg.adation, and corrective measures taken to prevent recurrence.

An in-service inspection was performed on approximately 30 percent'of the tubes in each S/G.

The in-service inspection results (defined in IS 4.4.5.2) were classified as Category C-2 for S/Gs 1, 2, and 3.

S/G 4 was classified as Category C-3 because of the detection of primary water stress corrosion cracking (PWSCC) at the explosively expanded top-of-tubesheet expansion. zone'of thi tubes. The TVA reference letter provided notification of the Category C-3.

Because of the detection of expansion zone PWSCC, rotating pancake coil examinations were completed on 100. percent of the tubes in all four S/Gs.

00113

-9112160007 911209 ADOCK 050 g 7 hf DR If /

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U.S. Nuclear Regulatory Commission

'Page 21 Dect.nber 9, 1991 To help prevent recurrence of expansion transition PWSCC in the SQN S/Gs, TVA took the conservative and proactive corrective action of the

-first-time implementation of shotpeening explosively expanded tubes b

during the Cycle 5 refuelin6 outage.

. Please direct questions-concerning this issue to D. V. Goodin at (615) 843-7734 Sincerely.

5 /N

)L. Wilson Enclosure cc (Enclosure):

Mr. D. : E. -LaBarge, Project Manager U.S. Nuclear Regulatory Commission One White Flint, North 11555 Rockville Pike Rockville, Maryland 10352 NRC Resident Inspectar i

LSequoyah Nuclear Plant

-2600 Igon Ferry Road Soddy Daisy. Tennessee 37379 7tr. B. A. Wilson.-Project Chief U.S. Nuclear Regulatory Commission Region II 101 Marietta Street, NW, Suite 2900 r

Atlanta.1 Georgia ~30323 L

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