ML20086G365
| ML20086G365 | |
| Person / Time | |
|---|---|
| Site: | Peach Bottom |
| Issue date: | 10/24/1975 |
| From: | Cooney M PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC |
| To: | Boyd R Office of Nuclear Reactor Regulation |
| References | |
| RO-75-23, NUDOCS 8401110268 | |
| Download: ML20086G365 (2) | |
Text
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PHILADELPHIA ELECTRIC COMPANY
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2301 M ARKET STREET PHILADELPHI A, PA.19101
)
1215) 841-dooo October 24, 1975 Mr. Roger S. Boyd, Acting Director Division of Reactor Licensing Of fice of Nuclear Reactor Regulations United States Mucicar Regulatory Commission Wa s hi ng ton, D.C.
20555
Dear Mr. Doyd:
Subicet: Envi ronmental Deviation The following deviation was reported to Mr. Walt Baunack, Office of Inspection and Enforcenent, Region 1, United States Nuclear Regulatory Conmission on October 15, 1975.
Reference:
License Number DPR-44/56 Envi ronmental Technica l Speci fications:
2.1 Report No.:
50-277/278-75-23 Report Date:
October 24, 1975 Deviation Date: October 15, 1975 Faci li ty:
Pcech Bottom Atomic Power Station Units 2 and 3 R.D. #1, Delta, Pennsylvania 17314 Identi fication of Deviation:
Removal of cooling tower for maintenance.
Condi tions Prior to Deviation:
Both units operating at a nominal 55% power.
The
'A' cooling tower was out of service because of a previous lif t pump bearing failure.
Description of Deviation:
Maintenance of the fire detection system piping on the
'C' cooling tower requi red removal of the tower f rom service for a period of approximately 14 hours1.62037e-4 days <br />0.00389 hours <br />2.314815e-5 weeks <br />5.327e-6 months <br /> on October 15, 1975.
Designation of Apparent Cause of Deviation:
Excessive ni trogen leakage from the fire detection system piping on the
'C' cooling tower was responsible for alarms approximately every 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />.
The tower was removed from service for approximately 14 hours1.62037e-4 days <br />0.00389 hours <br />2.314815e-5 weeks <br />5.327e-6 months <br /> on October 15, 1975 to accommodate maintenance work to reduce the 1"'
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alarm frequency.
i 8401110268 751024 PDR ADOCK 05000277 i
S PDR rnov MNT REGION '.a
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Mr. Roger S. Boyd 50-277/278-75-23 October 24, 1975 Page 2 Analysi s of Deviation:
Since river flows during the time interval were approximately C
28,000 CFS and no significant change in plant differential temperature was experienced, the removal of this tower from service had no signif-icant envi ronmenta l effect.
Corrective Action:
Inspection of the nitrogen piping associated ud th the fire detection system indicated numerous leaking connections. The access-able connections were repaired and resulted in reducing the frequency i
I of alarms due to low nitrogen pressure to once per day.
Failure Da ta:
There have been no previous maintenance outages required because of the fire detection system.
i i
~ Very truly yours, M. '
Cooney S erintendent Generation Div.-Nuclear i
Mr. James P. O'Rei lly, Di rector, Region 1 cc:
Office of Inspection and Enforcement United States Nuclear Regulatory Commission 631 Park Avenue i
King of Prussia, PA 19406 4
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