ML20086G313

From kanterella
Jump to navigation Jump to search
Environ RO 76-5:on 760114,settling Basin Effluent Ph Exceeded Environ Tech Spec Limit.Caused by Neutralizing Tank Discharged to Settling Basin W/O Being Neutralized Due to Improper Valving Lineup.Basin Isolated & Neutralized
ML20086G313
Person / Time
Site: Peach Bottom  Constellation icon.png
Issue date: 01/23/1976
From: Cooney M
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
References
RO-76-5, NUDOCS 8401110199
Download: ML20086G313 (2)


Text

_

y, .-- ,

rh

(') (v) 8 ;LE 7- COPT; i

PHILADELPHIA E'LECTRIC COMPANY 2301 MARKET STREET PHILADELPHIA, PA.19101 '

cy

-/D <0f s 2 si e414ooo

gpj{ g h ,;!d O 376 > -

January 23, 1976 { ,,,,,,mut ,,

77

/ NE.0I

/

Mr. J. P. O'Reilly ,

M Director, Region I s tu -

Office of Inspection and Enforcement U.S. Nuclear Regulatory Commission .

631 Park Avenue y King of Prussia, PA 19406  ;

. .t

Dear Mr. O'Reilly:

t  :

Subject:

Environmental Deviation j -

ThefollowingdeviationwasreportedtoMr..Jimhartlow, Office of Inspection and Enforcement, Region I, United States Nuclear Regulatory Conmission on January 15, 1976.

Reference:

License Number Dpr-44/56 Appendix B -

f y Environmental Technical Specifications: 2.2 3"  %

Report No.: 50-277/278-76-5 /

/

Report Date: January 23, 1976 [

Deviation Date: January 14, 1976 Facility: Peach Bottom Atomic Power Station (

Units 2 & 3 g R .D. 1, De l ta, Pennsylvania 17314

,\

Identification of Deviation:

Settling basin effluent pH in excess of Environmental Technical Specification limit.

Conditions Prior to Deviatio'n:

Unit 2 operating at approximately 99X power. Unit 3 shutdown for maintenance outage.

Description of Deviation:

Routine analysis of the settling basin effluent disclosed a a pH of 11 3 Dy ignation of Apparent Cause of Deviation:

.The neutralizing tank was discharged to the settling basin l ,

without being neutrali zed due to an improper volving li,ne-up564 -

l 8401110199 760123 PDR ADOCK 05000277 N S PDR

COPY SENT REGION

e t -

O O

. Mr. J. P. O'Reilly

  • 50-277/278-76-5 Januiry 23, 1976 ,

Page 2 Analisis of Deviation:

Because the settling basin flow is diluted by a factor of approximately 100,000 with circulating water flow, the pH of the circu-lating water was unaf fected. Therefore, the environmental impact was minimal.

Corrective Action:

The settling basin was immediately isolated and neutralized.

j The valve in the secondary flow path from the neutralizing tank to the i settling basin was locked closed. ' Correct operation was emphasized to the operators.

Failure Da a: ,

None. ,

4 Very truly yours, M. . Cooney Superintendent Generation Division - Nuclear cc: Mr. J. G. Davis, NRC ^

Mr . W. G . McDona l d, NR C i

g  %.

O e

i k

l l

ey , - . . r - - +