ML20086G136

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Environ RO 76-30:on 760707,pH for Settling Basin Effluent Exceeded Range Allowable by Ets.Cause Unknown.Memo Clearly Describing Proper Action During Clarifier Malfunction Sent to Operators & Supervisors
ML20086G136
Person / Time
Site: Peach Bottom  Constellation icon.png
Issue date: 07/16/1976
From: Cooney M
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To: Stello V
Office of Nuclear Reactor Regulation
References
RO-76-30, NUDOCS 8401100091
Download: ML20086G136 (2)


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PHILADELPHIA ELECTRIC COMPANY 2301 MARKET STREET PHILADELPHIA, PA.19101 (215)8414000

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Mr. Victor Stello, Jr.

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Director

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Division of Operating Reactors sf 3

Office of IIuclear Reactor Regulations y

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United States Nuclear Regulatory Commission Washington, D.C.

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Dear Mr. Stello:

Subject:

Environmental Deviation The following deviation was reported to Mr. Walt Baunack, Office of Inspection and Enforcement, Region 1, United States Nuclear Regulatory Cornmission on July 8,1976.

Reference:

License Number DPR-44/56 Environmental Technical Specifications:

2.2.2 Report No. :

50-277/278-76-30 Report Date:

July 16, 1976 Deviation Date:

July 7, 1976 Facility:

Peach Bottom Atomic Power Station Units 2 & 3 R.D.

1, Delta, PA 17314 Identification of Deviation:

The pH for the settling basin effluent exceeded the range allowable by the Environmental Technical Specifications.

Conditions Prior to Deviation:

Settling basin operating with maximum holdup.

Raw water surp in automatic code of operation.

0401100091 760716 PDR ADOCK 05000 S

74o0 COPY SEM REGION J' % _

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Mr. Victor Stello, Jr.

50-277/278-76-30 July 16, 1976 Page 2 Description of Deviation:

The pH of two grab samples taken from the settling basin measured 4.8 and 5.3.

A sample taken two hours latter measured 10.0.

The pH returned to the allowable range (6.0 to 9.0) within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> of the original sampling.

Designation of Apparent Cause of Deviation The initial low pH valve was due to a lack of soda ash addition to the clarifier during continuing alum feed.

This resulted in a low pH in the raw water sump which is pumped to the settling basin.

An investigation of the 10.0 pH did not reveal any apparent cause.

Analysis of Deviation:

Due to the short duration of the occurrence and because the settling basin flow is diluted by a factor of 100,000 with circulating water flow, the pH of the circulating water was unaffected.

Therefore, the environmental impact was minimal.

Corrective Action:

A memo which clearly describes proper action during clarifier malfunction is being sent to operators and supervision.

Failure Data:

Environmental Deviation Reports 50-277/278-76-20, 50-277/278-76-5 Very truly yours, 3

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M. J. Cooney Superintendent Generation Div.-Nuclear MJC:mam cc:

Mr. J. P. O'Reilly K3C Reg. Office i

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