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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20085N1451991-11-0505 November 1991 Revised Ro:Operability Date of 910830 for Electric Motor Driven Fire Water Pump P-4501 Not Met.Pump Not Actually Declared Operable Until 911025.Caused by Unforseen Matl & Testing Problems.Equivalent Pump Available ML20141D9651986-03-27027 March 1986 Ro:On 860314,compensatory Measures Implemented Due to Announcement of Bomb at Level 5 Reactor Door.Caused by Contract Employee,Unaware of Seriousness of Threat.No Bomb Found & No Threat to Security Existed ML20099C9631984-10-29029 October 1984 Ro:On 840911,moisture Discovered in Purified Helium Supply Line Wells During Installation of New Moisture Sensing Probes.Tests Indicate Leak Source Is Circulator Penetration A.Rate of Leak Approx .05 Gpm ML20098B3051984-09-0707 September 1984 Ro:On 840904,while Removing CRD & Orifice Assembly,Motor Overcurrent Condition on Auxiliary Transfer Cask Shutters Occurred,Preventing Full Closure.Caused by One Control Rod String Not Fully Retracted.Work Temporarily Discontinued ML20092N4741984-06-18018 June 1984 Ro:Re Failure of Masoneilan C-domotor Actuator During Steam Line Rupture Simulation Testing.Corrective Actions:Closed Shutoff Valves Installed Between Gauges & Taps.Gauges, W/Welded Stainless Steel Bourdon Tubes,Ordered ML20082A8431983-11-0707 November 1983 RO 83-43:on 831011,util Notified NRC of Various Nonconservative Errors Made in Original Analyses Which Constitute Basis of Tech Spec 4.1.9.GA Technologies Provided Interim Curves Which Corrected Deficiencies ML20069H1061983-03-17017 March 1983 RO 83-007:on 830215,instrument Power Inverter 1B Failed. Caused by Blown 150 Amp Fuse.Reactor Manually Scrammed, Instrument Bus re-energized & Blown Fuse Replaced ML20054F8461982-06-0909 June 1982 Ro:On 820605,one of Two Undervoltage Relays Which Monitor Reserve Auxiliary Transformer Tripped,Causing Load Shedding of Essential Busses 1 & 2.Caused by Procedural Inadequacy ML20054H2391982-05-0404 May 1982 Ro:On 820426,crack Found Extending Across Min cross-section Between Coolant Hole & One Face of Fuel Element 1-2415 Down Full Length of Block to Lower Exit.Caused by Mishandling. Damage Does Not Extend to Dowel Pin ML20064G7251978-12-0707 December 1978 Suppl Info to RO 50-267/78-05/03-X-1 on 781107:during Oper at 13% Thermal & 0 Elec Pwr,One of Three 1A Circulator Speed Indication Channels Was at 0,due to Bridge Unbalance.Similar Problem Occurred 7 Times Since 780425 ML20064G5661978-12-0505 December 1978 on 781129 at 4:00 Pm,Due to Problem in Heluim Circulatory Sys,There Was a Minute Release of Radioactivity in Reactor Bldg.No Hazard to Public ML20085L6121976-09-30030 September 1976 RO 50-267/75/05B:on 750323,helium Circulators 1A & 1B Tripped & Buffer Differential Pressure Indication of Helium Circulators 1C & 1D Dropped.Caused by Increased Pressure in Surge Tanks Due to Water Inflow.Procedures Revised ML20085M6621975-12-18018 December 1975 RO 50-267/75/17A:on 750912,orifice Valve Assembly Associated W/Control Rod Drive Observed Falling Vertically from Normally Installed Position.Caused by Improper Final Assembly of Control Rod Drive Unit ML20085M5851975-12-15015 December 1975 RO 50-267/75/18A:on 750924,while Removing Boron Carbide Balls from Reserve Shutdown Assembly of Control Rod Drive, Serial Number 28,core Region 13,light Deposit of White Crystal Noted on Surface of Several Balls ML20085M5141975-11-18018 November 1975 RO 50-267/75/20:on 751024,reactor Plant Supply Fan 1B Developed Fault,Causing Reactor Plant MCC 3 Essential Bus to Be Out of Svc During Repair of Fan 1A.Caused by Loose Electrical Connection.Bus & Motor Meggered & Verified ML20085M5381975-10-17017 October 1975 RO 50-267/75/16:on 751009,apparent Failure of Control Sys for Circulator High Pressure Separator C Resulted in Flooding of High Pressure Separator.Low Selector Removed, Disassembled,Inspected & Cleaned ML20085M6141975-10-17017 October 1975 RO 50-267/75/19:on 750926,spare Control & Orifice Assembly Modified by Addition of New Seals to Reduce Helium Bypass Flow.Caused by Seal Ring Larger in Outside Diameter than Inside Diameter at Refueling Penetration ML20085M6021975-10-13013 October 1975 RO 50-267/75/13A:on 750911,fan Start Relay for 480-volt Transformer 1B Failed.Caused by Component Failure & Design Flaw.Relays Replaced W/Better Application & Relay Logic Circuitry Reversed to Require Deenergized Relay ML20085M6071975-10-0909 October 1975 RO 50-267/75/13:on 750911,fan Start Relay for 480-volt Tansformer 1B Failed.Caused by Component Failure & Design Flaw.Relays Replaced W/Better Application & Relay Logic Circuitry Reversed Requiring Deenergized Relay ML20085M5521975-10-0202 October 1975 RO 50-267/75/17:on 750912,orifice Valve Assembly Associated W/Control Rod Drive Observed to Have Fallen Vertically Downward from Installed Position.Caused by Improper Final Assembly of Control Rod Drive Unit ML20085M5941975-09-30030 September 1975 RO 50-267/75/18:on 750924,during Removal of Boron Carbide Balls from Reserve Shutdown Hopper Assembly of Control Rod Drive,Serial Number 28,core Region 13,light Deposit of White Crystal Noted on Surface of Several Balls ML20081J5621975-09-29029 September 1975 RO 50-267/75/14:on 750829,480-volt Bus Tie Breaker Between Bus 2 & 3 Opened Removing Power from 280-volt Bus 2.Caused by Opening of Bus Tie Breaker.Tie Breaker Trip Settings Adjusted ML20085L6381975-07-21021 July 1975 RO 50-275/75/8:on 750428,insp Revealed That Adequate Fire Stops in Vertical Cableways Between Floors in Reactor Bldg, in Horizontal Cable Trays & in Vertical Cable Ducts Not Installed Per FSAR Commitment.Cause Not Stated ML20085L5981975-06-18018 June 1975 RO 50-267/75/10:on 750428,analysis of Pcrv Cooling Tube Outlet Temps Revealed Four Tubes W/Temp of 24 F.Caused by Differential Pressure Driving Control Rods Into Annulus. Drive Housings Will Be Modified ML20085M7461975-06-17017 June 1975 RO 50-267/75/2A:on 750115,both Secondary Coolant Loops Appeared Isolated Simultaneously by PPS Action.Caused by Design Error.Capacitors Added Across Collector Load of Output Buffer Transistors ML20085L6341975-05-29029 May 1975 RO 50-267/75/12:on 750516,engine B Failed to Start Due to Fuel Sys Airlock.Caused by Fuel Being Shut Off W/O Engine Being Removed from Svc.Procedure Will Be Revised ML20085L6221975-05-0707 May 1975 RO 50-267/75/7:on 750428,temporary Cables from Auxiliary Electrical Equipment Cabinets Not Segregated from Permanent Cables.Cause Not Stated.Work Authorization Issued to Correct Color Coding ML20085L6391975-04-30030 April 1975 RO 50-267/75/6:on 750402,bearing Water Makeup Pump P-2105 Handswitch Insp Revealed Discrepancies in Maintaining Bus Segregation Requirements.Cause Not Stated.Field Change Notice Issued to Correct Discrepancies ML20085L6981975-04-18018 April 1975 RO 50-267/75/5:on 750323,circulators a & B Tripped Off & Buffer Indications on Circulators C & D Dropped.Caused by Increased Pressure in Surge Tanks Due to Water Inflow Displacing Helium & Increasing Suction Pressure ML20085L6521975-03-14014 March 1975 RO 50-267/75/4:on 750213,control Rod & Orifice Position Indicators Operated Erratically Due to High Moisture Levels in Primary Coolant Circuit.Caused by Shutdown of Purification Sys.Potentiometer Test Developed ML20085L7251975-03-0404 March 1975 RO 50-267/75/3:on 750203,drop in Loop 2 Instrument Bus Voltage Caused Loop 1 Helium Circulator to Trip.Cause Not Stated ML20085L7791975-03-0404 March 1975 RO 50-267/75-1-A:on 750117,insp Revealed Discrepancies in Maintaining Loop & Bus Segregation Requirements.Caused by Error in Installation.Wires,Switches & Relays Not Meeting Segregation Requirements Separated ML20085L7831975-01-31031 January 1975 RO 50-267/75/1:on 750117,insp Revealed Discrepancies in Maintaining Loop & Bus Segregation.Caused by Error in Installation.Wires,Switches & Relays Separated ML20085L7971975-01-14014 January 1975 RO 50-267/75/2:insp of Steam/Water Dump Valves Revealed That Portions of Electrical Conduit Runs to Valves Violated Loop & Bus Segregation Criteria.Caused by Improper Installation. Cables,Switches,Solenoids & Junction Boxes to Be Modified ML20086E2261974-11-0606 November 1974 RO 50-267/74/1:on 741106,during Review,Short That Could Potentially Lead to Loss of Both Power Supplies on Circulatory Auxiliary Control Panel I-29 Discovered.Caused by Design Error.Three Wires Removed ML20086E2091974-01-14014 January 1974 Ro:On 740112,during Insp of Permanent Half Size Top Reflector,Seven Elements Failed to Meet Specs for Chips & Gauges.Spare Reflectors Replaced Failed Elements.Great Lakes Carbon,Supplier of Elements,Contacted ML20086E1951974-01-14014 January 1974 Ro:On 740114,during Insp of Metal Clad Keyed Top Reflector Elements,Burrs Found on Drilled Holes in Bottom of Distribution Plate.Seven Elements Installed Will Be Removed. Procedure from Ga Co Awaited ML20086B1431971-10-29029 October 1971 Ro:On 710514,0819 & 0924,reactor Trip Breakers Failed to Open When Trip Signal Applied.After Investigation, Westinghouse Determined Undervoltage Device Latch Spring Pressure Improperly Set.Devices Adjusted 1991-11-05
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20196G6731997-07-0101 July 1997 Informs Commission That Decommissioning Process Has Been Completed at PSC of Colorado Fsvngs,Unit 1 Located in Town of Platteville in Weld County,Co ML20141K9961997-05-0505 May 1997 Safety Evaluation Supporting Amend 89 to License DPR-34 ML20140E1121997-04-10010 April 1997 Confirmatory Survey of Group Effluent Discharge Pathway Areas for Fsv Nuclear Station,Platteville,Co ML20134D1661997-01-30030 January 1997 Rev 1,Vol 6 to Final Survey Rept,Final Survey of Group E (Book 2A of 2) ML20137S6111996-12-31031 December 1996 Annual Rept Pursuant to Section 13 or 15(d) of Securities Exchange Act 1934, for Fy Ended Dec 1996 ML20134G6401996-10-29029 October 1996 Rev 0,Volume 6,Books 1 & 2 of 2 to Final Survey of Group E ML20134G6171996-10-29029 October 1996 Rev 2,Volume 1,Books 1 & 2 of 2 to Final Survey Description & Results ML20134G7271996-10-29029 October 1996 Rev 0,Volume 11,Book 1 of 1 to Final Survey of Group J ML20134G6861996-10-29029 October 1996 Rev 0,Volume 8,Books 1 & 2 of 2 to, Final Survey of Group G ML20134G6321996-10-26026 October 1996 Rev 1,Volume 5,Books 2 & 3 of 3 to Final Survey of Group D ML20133D7831996-10-22022 October 1996 Preliminary Rept - Orise Support of NRC License Insp at Fsv on 960930-1003 ML20116A4661996-07-19019 July 1996 Fsv Final Survey Exposure Rate Measurements ML20112J6861996-05-31031 May 1996 June 1996 Quarterly 10CFR50.59 Rept of Changes,Tests & Experiments for Fsv Decommissioning.Rept Covers Period of 960216-0531 ML20112C1531996-05-17017 May 1996 Fsv Final Survey Exposure Rate Measurements ML20101G5521996-03-21021 March 1996 Confirmatory Survey Activities for Fsv Nuclear Station PSC Platteville,Co, Final Rept ML20097E3201996-01-31031 January 1996 Nonproprietary Fort St Vrain Technical Basis Documents for Piping Survey Instrumentation ML20095K4131995-12-26026 December 1995 Rev 3 to Decommissioning Plan ML20095H7211995-12-20020 December 1995 Revs to Fort St Vrain Decommissioning Fire Protection Plan Update ML20095K9751995-12-15015 December 1995 Fort St Vrain Project Update Presentation to NRC, on 951207 & 15 ML20096C1671995-12-13013 December 1995 Rev 4 to Decommissioning Fire Protection Plan ML20094M1651995-11-30030 November 1995 Nonproprietary Fsv Technical Basis Documents for Piping Survey Implementation ML20092F3461995-09-14014 September 1995 Quarterly 10CFR50.59 Rept of Changes,Tests & Experiments for Fsv Decommissioning, Covering Period of 950516-0815.W/ ML20137H3531994-12-31031 December 1994 Partially Withheld, Rept of Independent Counsel Investigation Concerning Issues at Fort St Vrain Nuclear Generating Station Decommissioning Project, App D,Comments by Mkf & Westinghouse Team & Responses ML20137S2331994-12-31031 December 1994 Rept of Independent Counsel Investigation Concerning Issues at Fort St Vrain Nuclear Generating Station Decommissioning Project, Dec 1994 ML20029C6031993-12-31031 December 1993 1993 Annual Rept Public Svc Co of Colorado. W/940405 Ltr ML20058Q3791993-12-21021 December 1993 Rev 1 to Decommissioning Plan for Fort St Vrain Nuclear Generating Station ML20045B3641993-06-30030 June 1993 June 1993 Quarterly 10CFR50.59 Rept of Changes,Tests & Experiments for Fsv Decommissioning. ML20045A4291993-06-0303 June 1993 LER 93-003-00:on 930505,new Source of Natural Gas Introduced within 0.5 Miles of ISFSI & Reactor Bldg W/O Prior NRC Approval.Caused by Field Routing of Natural Gas Pipe.Well Isolated by Well operator.W/930603 Ltr ML20077D1631993-05-10010 May 1993 Enforcement Conference, in Arlington,Tx ML20125C7161992-12-0707 December 1992 Part 21 Rept Re Possibility for Malfunction of Declutching Mechanisms in SMB/SB-000 & SMB/SB/SBD-00 Actuators. Malfunction Only Occurs During Seismic Event.Balanced Levers May Be Purchased from Vendor.List of Affected Utils Encl ML20128D7191992-12-0101 December 1992 Safety Evaluation Approving Exemption from Requirement of 10CFR50.54(q) to Change to Biennial Emergency Plan Exercise Rather than Annual Following Completion of Next Scheduled Exercise at Plant ML20127P5861992-11-23023 November 1992 Followup to 921005 Part 21 Rept Re Potential Defect in SB/SBD-1 Housing Cover Screws.Procedure Re Replacement of SBD-1 Spring Cover Bolts Encl.All Fasteners Should Be Loosened & Removed.List of Affected Utils Encl ML20127F5691992-11-0303 November 1992 Informs Commission of Intent to Issue Order Approving Plant Decommissioning Plan & Corresponding Amend to License DPR-34 ML20101E5761992-05-31031 May 1992 Monthly Defueling Operations Rept for May 1992 for Fort St Vrain ML20096E8221992-04-30030 April 1992 Monthly Operating Rept for Apr 1992 for Fort St Vrain.W/ ML20095E9601992-04-17017 April 1992 Rev to Fort St Vrain Proposed Decommissioning Plan ML20100R7431992-03-31031 March 1992 Monthly Operating Rept for Mar 1992 for Fort St Vrain.W/ ML20090L0621992-02-29029 February 1992 Monthly Operating Rept for Feb 1992 for Fort St Vrain Unit 1 ML20092D0081992-01-31031 January 1992 Monthly Operating Rept for Jan 1992 for Fort St Vrain Nuclear Generating Station ML20102B2241992-01-22022 January 1992 Fort St Vrain Station Annual Rept of Changes,Tests & Experiments Not Requiring Prior Commission Approval Per 10CFR50.59, for Period 910123-920122 ML20094N6701991-12-31031 December 1991 Public Svc Co Annual Financial Rept for 1991 ML20091J6251991-12-31031 December 1991 Monthly Operating Rept for Dec 1991 for Fort St Vrain.W/ ML20094D6711991-11-30030 November 1991 Monthly Operating Rept for Nov 1991 for Fort St Vrain Unit 1 ML20090M1871991-11-20020 November 1991 FOSAVEX-91 Scenario for 1991 Plant Exercise of Defueling Emergency Response Plan ML20086D6891991-11-15015 November 1991 Proposed Decommissioning Plan for Fort St Vrain Nuclear Generating Station ML20085N1451991-11-0505 November 1991 Revised Ro:Operability Date of 910830 for Electric Motor Driven Fire Water Pump P-4501 Not Met.Pump Not Actually Declared Operable Until 911025.Caused by Unforseen Matl & Testing Problems.Equivalent Pump Available ML20086C5451991-10-31031 October 1991 Monthly Operating Rept for Oct 1991 for Fort St Vrain.W/ ML20085H6611991-10-10010 October 1991 Assessment of Mgt Modes for Graphite from Reactor Decommissioning ML20091D7671991-10-0101 October 1991 Rev B to Engineering Evaluation of Prestressed Concrete Reactor Vessel & Core Support Floor Structures for Proposed Sys 46 Temp Change ML20085D9861991-09-30030 September 1991 Monthly Operating Rept for Sept 1991 for Fort St Vrain.W/ 1997-07-01
[Table view] |
Text
.
i O O P. O. Box 361, Platteville, Colorado 80651 October 2, 1975 -
i
,A ,.s Mr. E. !! orris Howard, Director '
/- 4:
02[.g Nuclear Regulatory Commission -
Region IV Office of Inspection and Enforec=ent '
~
Suite 1000 .
nuington, Texas 76012 -
P.EF: Facility Operating License ,
. Nn. DFR-34 Docket No. 50-267 ,
Dear Mr. Howard:
Enclosed please find a copy of Unusual Event Report. No. 50-267/75/17, Preliminary, submitted pcr the requirements of the Technical Specifi-Cations.
Very truly'yours,
,Frederic E. Svart Superintendent, Nuclear. Production
~rort St. Vrain Nuclear -
Generating Station FES/alk Mr. Roger S. Boyd '/
i
. A, l -
f
.(
8311080628 751002 PDR ADDCK 05000267 '
S PDR
-64 o
e
_ 9
- Events and Abnormal Unusual Operating Monthly occurrence Occurrence ^ Cost Reports R epor *.s Report s Letter _
Addressee San Francisco Operations Office
Oakland, California 94612 2 2 2 -
Atta: Manager * * ~ 4 Pinance & Budget 1 1 - -
Calif. Patent Group Division of Reactor Research and Development ERDA - -
Washington, D. C. 20545 ,
1 1 1, ~
Atta: Director ~ ~
Asst. Dir. for UEBR Programs 2 2 2 -
Asst. Dir. for Gas Cooled teactor Project 1 - 1 1 -
Asst. Dir. for Engrg. and Technology 1 1 1 -
Asst. Dir. for Reactor Safety
- 1 1 1 1
ERDA -SCRPO-SD .
P. O. Box 81325 .
San Diego, California 92138 .
1 1 W. Soule', Project Engr.
ERDA -SCRPO .
P. O. Box 1446 Canoga Park', California _91304 1 1 1
bttr
- ERDA -SCRPO t2 ++ P. O. Box 1446 .
+* Canoga Park, California 91304 .
3 3 Technical Information Center
.ERDA P. O. Box 62 .. .
Oak Ridge, Tennessee 37830 10 10 , 2 John R. Zanot, Project Manager (FFLC)'
P. O. Box 81608 San Diego, California 92138 I"#E f,
Por Monthly Letter only: B1ick Bob Clark 1 P. O. Box 426 Platteville, CO 80651 R. Walker 1 'l 1 1 1 P. Svart 1 'l L. Brey **
D. Rodgers' 1 E. Eill 1 P. Mathie 1 1 'l
- J. Cahm D. Alexander 1 J. Liebelt 1-K. Stannard 1 (Room 526) 1 NRC, Director of Regulations, k'ashington,D.C. 20545 d NCoPy of Howard letter & xe ** g r8of
R. Boyd
= 1 1 1 (Chairman.NFSC) Oscar Lee i Control Room D. Warembourg i 1 1 (letter) copy of letter to Boyd E. Novard i P. Bronson 1
- M..J. Cooney 1 Philadelphia Electric Company 1 1 2301 Market St. PORC Committee Philadelphia, Pa.18101
O o REPORT DATE:
October 2, 1975 UNUSUAL EVENT 75/17 Page 1 of 5 OCCURRENCE DATE:
September 12, 1975 FORT ST. VRAIN NUCLEAR GENERATING STATION .
PUBLIC SERVICE COMPANY OF COLORADO P. O. BOX 361 PLAITEVILLE, COLORADO 80651 REPORT No. 50-267/75/17 Preliminary IDENTIFICATION OF .
OCCURRENCE:
At approximately 1030, September 12, 1975, the orifice valve assembly associated with control rod drive serial nomber 010 was observed to have fallen vertically
~
downward from its nor=al, install'ed position on the control rod drive unit while it was positioned in a special work stand located over an equipment storage well on the refueling floor. This control . rod drive unit was in position in the work stand
- for approximately two days and ha'd not been moved prior to the orifice valve becoming disengaged.
This has been identified as an unusual event per AC 7.6', Non1 Routine' Reports, Section C.2 of the' Fort St. Vrain Technic,a1' Specifications.
CONDITIONS PRIOR Routine Shutdown TO OCCURRENCE:
Steady State Power
- ' Routine Load Change Hot Shutdown X
Cold Shutdown Other (specify)
Reft $eling Shutdown Routine Startup The major plant parameters at the time of the event were as follows:
RTR ~* Wth Power E E'CT
- psig Secondary Coolant Temperature * 'F Flow
Pressure
- psig Primary Coolant Temperature *- *P Core Inlet-
~ '
O o IMUSUAL EVENT 75/17 Page 2 of 5 CONDITIONS PRIOR
- TO OCCURRENCE (continued):
Temperature
- 'F Core Outlet Primary Coolant (continued) F16w
- No bearing on this event.
DESCRIPTION OF OCCURRENCE:
Vrain are in the process of modifica-All of the control rod drives at Fort St.
tion to eliminate internal gas flow leakage paths (CWP-51). Control rod. drive serial number 010 had been removed from region five of the PCRV and placed in a special work stand on the refueling floor for implementation of the necessary modifications. All operations and handling associated with this control rod drive were routine and normal.
~
a functional Upon completing the prescribed approved modifications to this unit,All tests resulted.
operating test was performed using established procedures.Just prior to preparing in normal response from the control rod drive unit.
this unit for return to the PCRV, the orifice valve was observed to have fallen from its normal position at the lower end of the control . rod drive unit.
The dust cover (6) which protects the bolted support assembly for the orifice -
All of the parts were re-valve and actuator shaft was removed for inspection.
covered in tact: 1 self-locking. nut (42), 6 belleville washers (41),.1 bearing w:asher (49), and 1 stop plate (15) (see drawing SLR D1201-400G attached). The
control rod drive unit was then further disassembled as required to allow addi-tional internal inspection of the orifice drive mechanism.
APPARENT CAUSE Design Unusual Service Cond.
OF OCCURRENCE: Including Environ.
Manufacture Component Failure.
Installation /Const. X Other (specify)
Operator Improper final assembly of the Procedure . control rod drive unit at time _
of manufacture.
~
The apparent cause of this occurrence is failure to fully eng ge the lock nut with the threaded portion of the support shaf t'. The locking action of _ the
~
lock nut requires full engage.ient so that this improper assembly allowed the lock nut to disengage from the shaft.
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O o UNUSUAL EVENT 75/17 Page 4 of 5 ANALYSIS OF
All of the bolted support parts (12, 42, 49, 41, and 15) (SLR-D1201-400) were No' abnormal indi-removed from the control rod drive and closely inspected.
cations of any kind could be found. The orifice valve support shaf t and ac-tuator were removed from the control rod drive unit and carefully inspected, with considerable emphasis being given. to the threaded end of the stiaft to which the bolted support is attached. All threads looked normal; no signs of distress or abnormality could be seen. All of the parts were then reassembled This was done to determine that the physical mating of all parts was normal. Further, tihe self-satisfactorily and 'all parts fit properly and smoothly.
locking nut (42) threaded down to its proper position and tightenedThis snugly, is nor-was in fact locked such that a wrench was required to remove it. .
' mal and proper. .
' The only conclusion which can be drawn in view of the observed facts is that -
the self-locking nut had never been tightened down properly during initial assembly of the unit. Because the nut was not properly tightened, vibrations and pulsing of the nearby orifice drive motor could have caused the nut to back off sufficiently to release the orifice valve. This threaded support is essentially unstressed during normal installation and operation of.the control rod drive which would allow the nut free movement if it were,not preperly tightened. ,
CORRECTIVE ACTION: <
Seven spare control rod drives plus the 25 units still to be removed from the PCRV will be inspected to verify that the orifice valve support bolt is properly assembled, and that the retaining nut is tightened to the proper It is felt that this unusual event is an position on the isolated case. mating threads.If any additional discrepancies are found, the additional units, presently installed in the PCRV, will be removed for inspection.
FAILURE DATA /SIMILAR REPORTED OCCURRENCES:
- None PROGRAMfATIC IMPACT:
None .
,0DE IMPACT:
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UNUSUAL EVENT 75/17 Page 5 of 5 Submitted By: kav C. # a _/'n- -
Harvey W. Hillyard, Jr/
Technical Services Supervisor ,
l-Reviewed By: .
Frank M. Mathie Superintendent Maintenance f?
Approved By: / e ' .
I pederic E. Swart Superintendent, Nuclear Production 9
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