ML20085L725

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RO 50-267/75/3:on 750203,drop in Loop 2 Instrument Bus Voltage Caused Loop 1 Helium Circulator to Trip.Cause Not Stated
ML20085L725
Person / Time
Site: Fort Saint Vrain 
Issue date: 03/04/1975
From: Brey H
PUBLIC SERVICE CO. OF COLORADO
To: Howard E
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML20085L723 List:
References
RO-50-267-75-3, NUDOCS 8311020383
Download: ML20085L725 (4)


Text

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' O C) public service company oe ochmea P. O. Box 361, Platteville, Colorado 80651 March 4, 1975 q,-( M %

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p n U jf';' " C r-Mr. E. Morris Howard, Director I

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Region IV Office of Inspection & Enforcement

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611 Ryan Plaza Drive Suite 1000

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Arlington, Texas 76012

Dear Mr. Iloward:

REF:

Facility Operating License No. DPR-34 Docket No. 50-267 Enclosed please find a copy of Unusual Event Report No. 50-267/75/3, submitted per the requirements of the Technical Specifications.

Very truly yours, Y

My ($9

11. Larry Brey Superintendent-Operations Fort St. Vrair. Nucicar Cencrating Station llLB:11 cc:

Mr. Angelo Ciambusso 0

8311020383 770630 28 PDR ADOCK 05000 S

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i REIMT DATE : rebrunry 22,,,__1975 UNUSUAL EVENT 0CCUlutE?:CE DATE February 3, 1975_

1 FORT ST. VRAIN NUCLEAR CENFPATING' STATION

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.g ej REPORT 1;0. 50-267/75/3 l.

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Preliminary

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IDENTIFICATION OF OCCURRENCE:

OnFebruary3,1975,bidr in the Loop 2 instrunent bus volta:;c caused a Loop 1 llelium Circulator to trip This is identified as' an Unusual Event per Technical Specification definition AC 7.6.C.3.

CONDITIONS PRIOR TO OCCURRENCE:

Steady State Power Routine Shutdown Hot Shutdown Routine Load Change Cole :.diardv.a Other (specity)

Refueling Shutdown Routine Startup The major plant parameters at the time of the event were as follows:

Power

PTR, MWth

. ELECT, MWe Secondary Coolant Pressure psig Temperature 140*h'MainSteam 500'F Rcheat-Flow f /hr. -

Primary Coolant Pressure jsig Temperaturc

'F Core Inlet' l

'F Core Outlet

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  • A, B, D, Helium Circulators self turbining between 300-500 rpm i

C llelium Circulator,at 2000 rpm 1

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j Page 2 DESCRIPTION OF OCCUPJ:ENCE:

At 1445 hours0.0167 days <br />0.401 hours <br />0.00239 weeks <br />5.498225e-4 months <br /> en February 3,1975, a construction electrician accidently grounded the Loop 62 instrument bus.

Helium Circulators B, C and D Tripped of f primarily due to a buf fer/mid-buffer upset.

A fault on the Loop Inst rument Bus should not have af fected a Loop 1 liclium Circulator ("B" Helius Circulator).

APPARENT CAUSE OF OCCUERECE:

Design Unusual Service Cond.

Including Environ.

Manufacture Component railure Installation /

Const.

X Othcr (Specify)

Operator The cause of this occurrence in Procedure presentiv unknown.

ANALYSIS OF OCCUnnFNCE:

The upset in the buffer system caused by the instrument bus voltage dip some how reflected from Loop 2 into Loop 1.

This incident along with a Helium Circulator upset uhich occurred on January 15, 1975, wher. firing of a Loop 2 bearing water accumulator to meet a Technical Specification Surveillance Test requirerent caused an upset in the buffer systea which could be seen on the Loop 1 Helium Circulators was presented to the Plant Operations Review Committee.

The Committec-revitued both incidents and determined them to be " Safety Significant",

The NTSC was appraised of the situatlon and has recommended that the system vendor be notified cf the problems and that the risc-to-power testing program be delayed until the problems are satisf actorily resolved.

CORRECTIVE ACTION:

The Corrective Action has not, as yet, been determined.

This will be transmitted with the " Final" Unusual Event correspondence for Unusual Event No. 50-267/75/1.

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  • i FAILUn_E DATA /SIMILAR REPORTED OCCUllRENCES:

None PROGPR fATIC IMPACT:

Unknown CODE IMPACT:

None RECO.TIENDED :

APPROVED:

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~_urri. J H. L. Brey, puperintendent, Operations

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rederic C. Swart, Superintendent, Production Fort St. Vrain Nuclear Station Vrain Nuclear Station l

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DATE:

DATE:

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