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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20085N1451991-11-0505 November 1991 Revised Ro:Operability Date of 910830 for Electric Motor Driven Fire Water Pump P-4501 Not Met.Pump Not Actually Declared Operable Until 911025.Caused by Unforseen Matl & Testing Problems.Equivalent Pump Available ML20141D9651986-03-27027 March 1986 Ro:On 860314,compensatory Measures Implemented Due to Announcement of Bomb at Level 5 Reactor Door.Caused by Contract Employee,Unaware of Seriousness of Threat.No Bomb Found & No Threat to Security Existed ML20099C9631984-10-29029 October 1984 Ro:On 840911,moisture Discovered in Purified Helium Supply Line Wells During Installation of New Moisture Sensing Probes.Tests Indicate Leak Source Is Circulator Penetration A.Rate of Leak Approx .05 Gpm ML20098B3051984-09-0707 September 1984 Ro:On 840904,while Removing CRD & Orifice Assembly,Motor Overcurrent Condition on Auxiliary Transfer Cask Shutters Occurred,Preventing Full Closure.Caused by One Control Rod String Not Fully Retracted.Work Temporarily Discontinued ML20092N4741984-06-18018 June 1984 Ro:Re Failure of Masoneilan C-domotor Actuator During Steam Line Rupture Simulation Testing.Corrective Actions:Closed Shutoff Valves Installed Between Gauges & Taps.Gauges, W/Welded Stainless Steel Bourdon Tubes,Ordered ML20082A8431983-11-0707 November 1983 RO 83-43:on 831011,util Notified NRC of Various Nonconservative Errors Made in Original Analyses Which Constitute Basis of Tech Spec 4.1.9.GA Technologies Provided Interim Curves Which Corrected Deficiencies ML20069H1061983-03-17017 March 1983 RO 83-007:on 830215,instrument Power Inverter 1B Failed. Caused by Blown 150 Amp Fuse.Reactor Manually Scrammed, Instrument Bus re-energized & Blown Fuse Replaced ML20054F8461982-06-0909 June 1982 Ro:On 820605,one of Two Undervoltage Relays Which Monitor Reserve Auxiliary Transformer Tripped,Causing Load Shedding of Essential Busses 1 & 2.Caused by Procedural Inadequacy ML20054H2391982-05-0404 May 1982 Ro:On 820426,crack Found Extending Across Min cross-section Between Coolant Hole & One Face of Fuel Element 1-2415 Down Full Length of Block to Lower Exit.Caused by Mishandling. Damage Does Not Extend to Dowel Pin ML20064G7251978-12-0707 December 1978 Suppl Info to RO 50-267/78-05/03-X-1 on 781107:during Oper at 13% Thermal & 0 Elec Pwr,One of Three 1A Circulator Speed Indication Channels Was at 0,due to Bridge Unbalance.Similar Problem Occurred 7 Times Since 780425 ML20064G5661978-12-0505 December 1978 on 781129 at 4:00 Pm,Due to Problem in Heluim Circulatory Sys,There Was a Minute Release of Radioactivity in Reactor Bldg.No Hazard to Public ML20085L6121976-09-30030 September 1976 RO 50-267/75/05B:on 750323,helium Circulators 1A & 1B Tripped & Buffer Differential Pressure Indication of Helium Circulators 1C & 1D Dropped.Caused by Increased Pressure in Surge Tanks Due to Water Inflow.Procedures Revised ML20085M6621975-12-18018 December 1975 RO 50-267/75/17A:on 750912,orifice Valve Assembly Associated W/Control Rod Drive Observed Falling Vertically from Normally Installed Position.Caused by Improper Final Assembly of Control Rod Drive Unit ML20085M5851975-12-15015 December 1975 RO 50-267/75/18A:on 750924,while Removing Boron Carbide Balls from Reserve Shutdown Assembly of Control Rod Drive, Serial Number 28,core Region 13,light Deposit of White Crystal Noted on Surface of Several Balls ML20085M5141975-11-18018 November 1975 RO 50-267/75/20:on 751024,reactor Plant Supply Fan 1B Developed Fault,Causing Reactor Plant MCC 3 Essential Bus to Be Out of Svc During Repair of Fan 1A.Caused by Loose Electrical Connection.Bus & Motor Meggered & Verified ML20085M5381975-10-17017 October 1975 RO 50-267/75/16:on 751009,apparent Failure of Control Sys for Circulator High Pressure Separator C Resulted in Flooding of High Pressure Separator.Low Selector Removed, Disassembled,Inspected & Cleaned ML20085M6141975-10-17017 October 1975 RO 50-267/75/19:on 750926,spare Control & Orifice Assembly Modified by Addition of New Seals to Reduce Helium Bypass Flow.Caused by Seal Ring Larger in Outside Diameter than Inside Diameter at Refueling Penetration ML20085M6021975-10-13013 October 1975 RO 50-267/75/13A:on 750911,fan Start Relay for 480-volt Transformer 1B Failed.Caused by Component Failure & Design Flaw.Relays Replaced W/Better Application & Relay Logic Circuitry Reversed to Require Deenergized Relay ML20085M6071975-10-0909 October 1975 RO 50-267/75/13:on 750911,fan Start Relay for 480-volt Tansformer 1B Failed.Caused by Component Failure & Design Flaw.Relays Replaced W/Better Application & Relay Logic Circuitry Reversed Requiring Deenergized Relay ML20085M5521975-10-0202 October 1975 RO 50-267/75/17:on 750912,orifice Valve Assembly Associated W/Control Rod Drive Observed to Have Fallen Vertically Downward from Installed Position.Caused by Improper Final Assembly of Control Rod Drive Unit ML20085M5941975-09-30030 September 1975 RO 50-267/75/18:on 750924,during Removal of Boron Carbide Balls from Reserve Shutdown Hopper Assembly of Control Rod Drive,Serial Number 28,core Region 13,light Deposit of White Crystal Noted on Surface of Several Balls ML20081J5621975-09-29029 September 1975 RO 50-267/75/14:on 750829,480-volt Bus Tie Breaker Between Bus 2 & 3 Opened Removing Power from 280-volt Bus 2.Caused by Opening of Bus Tie Breaker.Tie Breaker Trip Settings Adjusted ML20085L6381975-07-21021 July 1975 RO 50-275/75/8:on 750428,insp Revealed That Adequate Fire Stops in Vertical Cableways Between Floors in Reactor Bldg, in Horizontal Cable Trays & in Vertical Cable Ducts Not Installed Per FSAR Commitment.Cause Not Stated ML20085L5981975-06-18018 June 1975 RO 50-267/75/10:on 750428,analysis of Pcrv Cooling Tube Outlet Temps Revealed Four Tubes W/Temp of 24 F.Caused by Differential Pressure Driving Control Rods Into Annulus. Drive Housings Will Be Modified ML20085M7461975-06-17017 June 1975 RO 50-267/75/2A:on 750115,both Secondary Coolant Loops Appeared Isolated Simultaneously by PPS Action.Caused by Design Error.Capacitors Added Across Collector Load of Output Buffer Transistors ML20085L6341975-05-29029 May 1975 RO 50-267/75/12:on 750516,engine B Failed to Start Due to Fuel Sys Airlock.Caused by Fuel Being Shut Off W/O Engine Being Removed from Svc.Procedure Will Be Revised ML20085L6221975-05-0707 May 1975 RO 50-267/75/7:on 750428,temporary Cables from Auxiliary Electrical Equipment Cabinets Not Segregated from Permanent Cables.Cause Not Stated.Work Authorization Issued to Correct Color Coding ML20085L6391975-04-30030 April 1975 RO 50-267/75/6:on 750402,bearing Water Makeup Pump P-2105 Handswitch Insp Revealed Discrepancies in Maintaining Bus Segregation Requirements.Cause Not Stated.Field Change Notice Issued to Correct Discrepancies ML20085L6981975-04-18018 April 1975 RO 50-267/75/5:on 750323,circulators a & B Tripped Off & Buffer Indications on Circulators C & D Dropped.Caused by Increased Pressure in Surge Tanks Due to Water Inflow Displacing Helium & Increasing Suction Pressure ML20085L6521975-03-14014 March 1975 RO 50-267/75/4:on 750213,control Rod & Orifice Position Indicators Operated Erratically Due to High Moisture Levels in Primary Coolant Circuit.Caused by Shutdown of Purification Sys.Potentiometer Test Developed ML20085L7251975-03-0404 March 1975 RO 50-267/75/3:on 750203,drop in Loop 2 Instrument Bus Voltage Caused Loop 1 Helium Circulator to Trip.Cause Not Stated ML20085L7791975-03-0404 March 1975 RO 50-267/75-1-A:on 750117,insp Revealed Discrepancies in Maintaining Loop & Bus Segregation Requirements.Caused by Error in Installation.Wires,Switches & Relays Not Meeting Segregation Requirements Separated ML20085L7831975-01-31031 January 1975 RO 50-267/75/1:on 750117,insp Revealed Discrepancies in Maintaining Loop & Bus Segregation.Caused by Error in Installation.Wires,Switches & Relays Separated ML20085L7971975-01-14014 January 1975 RO 50-267/75/2:insp of Steam/Water Dump Valves Revealed That Portions of Electrical Conduit Runs to Valves Violated Loop & Bus Segregation Criteria.Caused by Improper Installation. Cables,Switches,Solenoids & Junction Boxes to Be Modified ML20086E2261974-11-0606 November 1974 RO 50-267/74/1:on 741106,during Review,Short That Could Potentially Lead to Loss of Both Power Supplies on Circulatory Auxiliary Control Panel I-29 Discovered.Caused by Design Error.Three Wires Removed ML20086E2091974-01-14014 January 1974 Ro:On 740112,during Insp of Permanent Half Size Top Reflector,Seven Elements Failed to Meet Specs for Chips & Gauges.Spare Reflectors Replaced Failed Elements.Great Lakes Carbon,Supplier of Elements,Contacted ML20086E1951974-01-14014 January 1974 Ro:On 740114,during Insp of Metal Clad Keyed Top Reflector Elements,Burrs Found on Drilled Holes in Bottom of Distribution Plate.Seven Elements Installed Will Be Removed. Procedure from Ga Co Awaited ML20086B1431971-10-29029 October 1971 Ro:On 710514,0819 & 0924,reactor Trip Breakers Failed to Open When Trip Signal Applied.After Investigation, Westinghouse Determined Undervoltage Device Latch Spring Pressure Improperly Set.Devices Adjusted 1991-11-05
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20196G6731997-07-0101 July 1997 Informs Commission That Decommissioning Process Has Been Completed at PSC of Colorado Fsvngs,Unit 1 Located in Town of Platteville in Weld County,Co ML20141K9961997-05-0505 May 1997 Safety Evaluation Supporting Amend 89 to License DPR-34 ML20140E1121997-04-10010 April 1997 Confirmatory Survey of Group Effluent Discharge Pathway Areas for Fsv Nuclear Station,Platteville,Co ML20134D1661997-01-30030 January 1997 Rev 1,Vol 6 to Final Survey Rept,Final Survey of Group E (Book 2A of 2) ML20137S6111996-12-31031 December 1996 Annual Rept Pursuant to Section 13 or 15(d) of Securities Exchange Act 1934, for Fy Ended Dec 1996 ML20134G6401996-10-29029 October 1996 Rev 0,Volume 6,Books 1 & 2 of 2 to Final Survey of Group E ML20134G6171996-10-29029 October 1996 Rev 2,Volume 1,Books 1 & 2 of 2 to Final Survey Description & Results ML20134G7271996-10-29029 October 1996 Rev 0,Volume 11,Book 1 of 1 to Final Survey of Group J ML20134G6861996-10-29029 October 1996 Rev 0,Volume 8,Books 1 & 2 of 2 to, Final Survey of Group G ML20134G6321996-10-26026 October 1996 Rev 1,Volume 5,Books 2 & 3 of 3 to Final Survey of Group D ML20133D7831996-10-22022 October 1996 Preliminary Rept - Orise Support of NRC License Insp at Fsv on 960930-1003 ML20116A4661996-07-19019 July 1996 Fsv Final Survey Exposure Rate Measurements ML20112J6861996-05-31031 May 1996 June 1996 Quarterly 10CFR50.59 Rept of Changes,Tests & Experiments for Fsv Decommissioning.Rept Covers Period of 960216-0531 ML20112C1531996-05-17017 May 1996 Fsv Final Survey Exposure Rate Measurements ML20101G5521996-03-21021 March 1996 Confirmatory Survey Activities for Fsv Nuclear Station PSC Platteville,Co, Final Rept ML20097E3201996-01-31031 January 1996 Nonproprietary Fort St Vrain Technical Basis Documents for Piping Survey Instrumentation ML20095K4131995-12-26026 December 1995 Rev 3 to Decommissioning Plan ML20095H7211995-12-20020 December 1995 Revs to Fort St Vrain Decommissioning Fire Protection Plan Update ML20095K9751995-12-15015 December 1995 Fort St Vrain Project Update Presentation to NRC, on 951207 & 15 ML20096C1671995-12-13013 December 1995 Rev 4 to Decommissioning Fire Protection Plan ML20094M1651995-11-30030 November 1995 Nonproprietary Fsv Technical Basis Documents for Piping Survey Implementation ML20092F3461995-09-14014 September 1995 Quarterly 10CFR50.59 Rept of Changes,Tests & Experiments for Fsv Decommissioning, Covering Period of 950516-0815.W/ ML20137H3531994-12-31031 December 1994 Partially Withheld, Rept of Independent Counsel Investigation Concerning Issues at Fort St Vrain Nuclear Generating Station Decommissioning Project, App D,Comments by Mkf & Westinghouse Team & Responses ML20137S2331994-12-31031 December 1994 Rept of Independent Counsel Investigation Concerning Issues at Fort St Vrain Nuclear Generating Station Decommissioning Project, Dec 1994 ML20029C6031993-12-31031 December 1993 1993 Annual Rept Public Svc Co of Colorado. W/940405 Ltr ML20058Q3791993-12-21021 December 1993 Rev 1 to Decommissioning Plan for Fort St Vrain Nuclear Generating Station ML20045B3641993-06-30030 June 1993 June 1993 Quarterly 10CFR50.59 Rept of Changes,Tests & Experiments for Fsv Decommissioning. ML20045A4291993-06-0303 June 1993 LER 93-003-00:on 930505,new Source of Natural Gas Introduced within 0.5 Miles of ISFSI & Reactor Bldg W/O Prior NRC Approval.Caused by Field Routing of Natural Gas Pipe.Well Isolated by Well operator.W/930603 Ltr ML20077D1631993-05-10010 May 1993 Enforcement Conference, in Arlington,Tx ML20125C7161992-12-0707 December 1992 Part 21 Rept Re Possibility for Malfunction of Declutching Mechanisms in SMB/SB-000 & SMB/SB/SBD-00 Actuators. Malfunction Only Occurs During Seismic Event.Balanced Levers May Be Purchased from Vendor.List of Affected Utils Encl ML20128D7191992-12-0101 December 1992 Safety Evaluation Approving Exemption from Requirement of 10CFR50.54(q) to Change to Biennial Emergency Plan Exercise Rather than Annual Following Completion of Next Scheduled Exercise at Plant ML20127P5861992-11-23023 November 1992 Followup to 921005 Part 21 Rept Re Potential Defect in SB/SBD-1 Housing Cover Screws.Procedure Re Replacement of SBD-1 Spring Cover Bolts Encl.All Fasteners Should Be Loosened & Removed.List of Affected Utils Encl ML20127F5691992-11-0303 November 1992 Informs Commission of Intent to Issue Order Approving Plant Decommissioning Plan & Corresponding Amend to License DPR-34 ML20101E5761992-05-31031 May 1992 Monthly Defueling Operations Rept for May 1992 for Fort St Vrain ML20096E8221992-04-30030 April 1992 Monthly Operating Rept for Apr 1992 for Fort St Vrain.W/ ML20095E9601992-04-17017 April 1992 Rev to Fort St Vrain Proposed Decommissioning Plan ML20100R7431992-03-31031 March 1992 Monthly Operating Rept for Mar 1992 for Fort St Vrain.W/ ML20090L0621992-02-29029 February 1992 Monthly Operating Rept for Feb 1992 for Fort St Vrain Unit 1 ML20092D0081992-01-31031 January 1992 Monthly Operating Rept for Jan 1992 for Fort St Vrain Nuclear Generating Station ML20102B2241992-01-22022 January 1992 Fort St Vrain Station Annual Rept of Changes,Tests & Experiments Not Requiring Prior Commission Approval Per 10CFR50.59, for Period 910123-920122 ML20094N6701991-12-31031 December 1991 Public Svc Co Annual Financial Rept for 1991 ML20091J6251991-12-31031 December 1991 Monthly Operating Rept for Dec 1991 for Fort St Vrain.W/ ML20094D6711991-11-30030 November 1991 Monthly Operating Rept for Nov 1991 for Fort St Vrain Unit 1 ML20090M1871991-11-20020 November 1991 FOSAVEX-91 Scenario for 1991 Plant Exercise of Defueling Emergency Response Plan ML20086D6891991-11-15015 November 1991 Proposed Decommissioning Plan for Fort St Vrain Nuclear Generating Station ML20085N1451991-11-0505 November 1991 Revised Ro:Operability Date of 910830 for Electric Motor Driven Fire Water Pump P-4501 Not Met.Pump Not Actually Declared Operable Until 911025.Caused by Unforseen Matl & Testing Problems.Equivalent Pump Available ML20086C5451991-10-31031 October 1991 Monthly Operating Rept for Oct 1991 for Fort St Vrain.W/ ML20085H6611991-10-10010 October 1991 Assessment of Mgt Modes for Graphite from Reactor Decommissioning ML20091D7671991-10-0101 October 1991 Rev B to Engineering Evaluation of Prestressed Concrete Reactor Vessel & Core Support Floor Structures for Proposed Sys 46 Temp Change ML20085D9861991-09-30030 September 1991 Monthly Operating Rept for Sept 1991 for Fort St Vrain.W/ 1997-07-01
[Table view] |
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Ep Unit No. 1 P-76222 .
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i G Mr. E. Morris Howard, Director.
Nuclear Regulatory Commission Region IV Office of Inspection and Enforcement Suite 1000 Arlington, Texas 76012 REF: Facility Operating License No. DPR-34 Docket No. 50-267
Dear Mr. Howard:
Enclosed Final Supplement, please find a copy of Unusual Event Report No.
50-267/75/05B ,
fications. submitted per the requiraments of the Technical Speci-Also please find enclosed one copy of the Licensee Event Report for Unusual Event Report No. 50-267/75/05B.
Very truly yours,
./ .2 n %%%0 Frederic E. Swart l Superintendent, Nuclear Production l Fort St. Vrain Nuclear Generating Station .
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- . O O REPORT DATE: September 30, 1976 UNUSUAL EVENT 75/05B Page 1 of 4 OCCURRENCE DATE: March 23, 1975 FORT ST. VRAIN NUCLEAR GENERATING STATION PUBLIC SERVICE COMPANY OF COLORADO P.O. BOX 361 PLATTEVILLE, COLORADO 80651 REPORT No. 50-267/75/05B Supplement Final .
IDENTIFICATION OF OCCURRENCE:
A situation occurred while testing the helium circulator backup bearing water
~
system which resulted in helium circulators 1A and 1B automatically tripping off and the buffer differential pressure indication of helium circulators 1C and ID to drop, resulting in operator action to set the brake and seal.
This is identified as an Unusual Event, per Technical Specification definition AC 7.6c, paragraph 3.
00NDITIONS PRIOR TO OCCURRENCE: Steady State Power Routine Shutdown Hot Shutdown Routine Load Change X _ Cold Shutdown Other (specify)
Refueling Shutdown Routine Startup The major plant parameters at the time of the event were as follows:
I Power RTR 0 Wth ELECT 0 We Secondary Coolant Pressure N/A psig Tempera ture N/A 'F Flow N/A #/hr.
Primary Coolant Pressure 85 psig Temperature s200 *F Core Inlet N200 *F Core Outlet Flow Helium circulator self- #/hr.
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i DESCRIPTION OF i
OCCURRENCE:
The emergency feedwater. header had been isolated via V-21453 in order to repair the pressure control for valve PV-21105. Upon completion of this repair, pressurization of the emergency feedwater header was initiated by slowly opening the isolation valve V,-21453. The following events then occurred: :
- 1. Helium circulators lA and 1B tripped on negative buffer-mid- ,
buffer differential pressure. !
- 2. HV-2366-1 and HV-2366-2 changed the supply of makeup buffer gas to the helium circulators from the purified helium header to the helium storage system. At a PCRV pressure of 85 psig helium -
density is barely sufficient to place the purified helium com-pressors in service. Loss o' f a major helium user such as circu-lator 1A and 1B buffer, caused the purified helium compressor to trip and the automatic controls to switch to the high pressure helium storage system.
- 3. The bearing water surge tank pressure in both loops increased to 140 psi, causing the buffer return flows to drop to 0 on the remaining circulators. Circulator 1C buffer differential pressure decreased to 10" negative but did not trip. Circulator ID buffer differential pressure dropped but did not go negative. The operator set the brake and seal on both of these circulators be-cause the return flow was so low. The Rix recovery compressors were then set up to vent to atmosphere in order to get the bearing water surge tank pressure down. When surge rank pressure equalled ,
reactor vessel pressure,1C and ID helium circulators were 1 restarted.
APPARENT CAUSE OP OCCURRENCE: X Design Unusual Service Cond.
Including Environment
_iManufacture Component Failure Installation /Const. Other-(specify)
Operator Procedure The increased pressure in the surge tanks due to the water inflow displaced helium from these tanks, thereby . increasing the buffer helium recirculation suction pressure. This reduced the buffer return flow from the helium circu-lators causing them to trip on buffer-mid-buffer.
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UNUSUAL EVENT 75/05B Page 3 of 4 ANALYSIS OF OCCURRENCE:
i' It appears that PV-21105 failed to control as did PDV-2191 and PDV-2192. With !
these valves not operating while V-21453 was being opened, there was no con- !
trol of the backup bearing water flow. The large amount of flow into the bearing water surge tanks caused a displacement of the helium from the surge tanks (due to a level increase). This helium flowed backward through the equalization line to the suction of the buffer helium recirculators, which caused reverse flow of the buffer return from the helium circulators. . The ,
reverse flow of buffer return caused a buffer-mid-buffer differential suffici-ently negative to initiate the automatic circulator trips. l l
Ihe level increase would not have occurred under normal operating conditions l because with the normal bearing water pumps tripped and bearing water supplied i from the backup bearing water system, a feed forward signal from the control !
system would have opened the surge tank drain valves. Under these conditions, !
the possibility of high rate of change in the surge tank level and the reversal of return flow from the circulators, is eliminated. I I
l CORRECTIVE ACTION: .
A test of the backup bearing water system was completed. This test, RT-356, was i performed to verify that backup bearing water will function correctly and re-lated transients are repeatable. This test was performed at (1) pressures simulating the most adverse requirements for backup bearing water, and (2) at the pressure which also causes the most adverse helium buffer-mid-buffer inter-actions.
This test of (1) was performed five (5) times by simultaneously transferring all
, four circulators to backup bearing water. The results of the test show that on the most severe transient there was a margin of 25 psid between the transient and the circulator trip point. All other' test results show a larger.
margin.
The test of (2) was performed and the results show that the most severe' differ-ential pressure transient on the buffer-mid-buffer decreased but remained positive. The trip point is -9" water differential pressure. The results of test RT-356 verify the operability of the backup bearing water system and con-ciudes this report.
Rev. A procedure to establish backup bearing water without tripping operating B circulators, has been added to the appropriate System Operating Procedure.
No further corrective action is planned or' required.
PAILURE DATA /
SIMILAR REPORTED OCCURRENCES:
Unusual Occurrence No. 50-267/75/02 reports a. failure of PV-21105-1 in the backup.
bearing water system which occurred on April 10,- 1975.
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UNUSUAL EVENT 75/05B Page 4 of 4 PROGRAMMATIC IMPACT: ;
None CODE IMPACT:
. i None Submitted by: . . f ; .
H.W. Hillyard,/Jr. / '
Technical Services Supervisor Reviewed by:
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H. Larry Brey \ \
Superintendent, Operations .
. Y Approved by: e !m
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Fr eric E. Swart
[ q M .7, Su rintendent . Nuclear Production-t i
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P. O. Box 361, Platteville, Colorado 80651 I 1
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- B y -[g n August 9, 1976 g#' -
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' Fort St. Vrain M Unit No. 1 Y %r' P-76179
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atT 0 Mr. E. Morris lloward, Director Nuclear Regulatory Commission Region IV Office of Inspection and Enforcement Suite 1000 Arlington, Texas 76012 .
REF: Facility Operating License No. DPR-34 Docket No. 50-267
Dear Mr. Iloward :
Enclosed please find a copy of Unusual Event Report No. 50- 267/ 75 /07A, Final Supplement, submitted per the requirements of the Technical Speci-fications.
Also please find enclosed one copy of the Licensee Event Report for Unusual Event Report No. 50-267/75/07A.
Very truly yours, .
&E-Frederic E. Swart Superintendent, Nuclear Production FES/alk cc: Mr. Roger S.-Boyd
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- August 9, 1976 UNUSUAL EVENT 75/07A REPORT DATE:
, , Page 1 of 3 OCCURRENCE DATE: April 28, 1975 FORT ST. VRAIN NUCLEAR CENERATING STATION PUBLIC SERVICE COMPANY OF COLORADO P. O. BOX 361 PLATTEVILLE, COLORADO 80651 REPORT No. 50-267/ 75/07A FINAL SUPPLEMENT IDENTIFICATION OF JD_CCURRENCE :
Temporary cables from the auxiliary c1ccerical equipment cabinets to the temporary instrumentation and test equipment were not segregated from the permanent cables accocding to specification 1-N-2. Color coding on the temporary cables was not consistent with the scheme used in the permanent ins tallation.
CONDITIONS PRIOR TO OCCURRENCE: Steady State Power Routine Shutdown.
Hot Shutdown Routine Load Change -
4 Cold Shutdown Other (specify)
Refueling Shutdown X' Routine Startup The major plant parameters at the time of the event were an follows:
Power RTR - 116 . 4 7 HWth /
2 ELECT 0.0 HRe Secondary Coolant Pressure 1,216 psig -j
. .Temperatnre 30 6 'F Flow 1. 209 ~ x 100 #/hr.
. Primary ~ Coolant Pressure 411- ps ig' -
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[ Temperature _ 270- *
'F Co'reJoutlet.
350 I
Flow -0.31 x 108 f/hr.1
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. , UNUSUAL EVENT 75/07A Page 2 of 3 l DESCRIPTION OF l OCCURRENCE.
l Inspection revealed that some of the temporary cables to the temporary in-strumentation and test equipment in the auxiliary electrical equipment room were not segregated from the permanent cables above the auxiliary electri-cal equipment cabinets, either by physical separation or by fire resistant zipper tubing according to Specification 1-N-2.
APPARENT CAUSE OF OCCURRENCE: Design Unusual Servica Cond.
Including Environment Manufacture Component Failure X Installation /Const. Other (specify)
Operator Procedure ANALYSIS OF OCCURRENCE:
Adequate separation and segregation should exist between the temporary -
and permanent cables ~, according to Specification 1-N-2. l CORRECTIVE ACTION:
Cencral Atomic Work Authorization No. 99F1849 has been issued to correct !
color coding on 'the temporary cables and to zipper tube cables that do not meet segregation criteria according to Specification 1-N-2. The work ,
will be inspected af ter the work authorization h. s been completed. **
An extensive modification to correct violations of separation and segre -
gation has been completed. This was followed by an audit to verify that A separation and segregation criteria were met. .The results of this work are documented in Public. Service Company letter P-76105,. dated May 11, 19 76, from R. F. Walker to R. P. Denise. .!
l No further corrective action is anticipated or required.
PROGRAMMATIC IMPACT:
13 Months-CODE IMPACT: .
None f
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.. O .O UNUSUAL ~ EVENT 75/07A
. . . Page 3 of 3 i
Submitted by: ~ , .
H. W. Hillyagd, Jr. d' '
Technical Services Supervisor i
Reviewed by: Nk d 6 4 1 [r M. blcBride /
Resident Engineer Approved by: _ A.e uu W M F)Eederic E. Swart .
Superintendent, Nuclear Production 4
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