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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20149G9861994-11-0404 November 1994 Special Rept:On 941006,Unit 1 Fuel Storage Pool Conductivity Exceeded 10 Micro/Mho/Cm TS Limit & Returned to within TS on 941010.Caused by Decomposition of Biological micro-organisms in Fuel Storage Pool.Temporary Demineralizer Restarted ML20069E5351983-03-15015 March 1983 RO 83-014:on 830219,contaminated Demineralized Water Released Into Condenser,Allowing 0.7 Mci to Steam Out of Vent.Caused by Personnel Error.Operator Opened Valve MO-3-1301-10 Instead of Valve MO-3-4399-74 ML20069A3561983-03-0909 March 1983 RO 83-016:on 830207,contaminated Water from Drain & Refill of 2/3A Heating Boiler Inadvertently Released to Storm Sewer Sys.Caused by Operator Not Realizing Floor Drain Led to Storm Sewer Sys,Not Radwaste Sys.Tech Specs Not Violated ML20054F7971982-06-0909 June 1982 RO 82-027:on 820511,excessive Radioactive Contamination Identified in Two Areas of Offsite Dump.Caused by Inadequate Control of Dump Access & Failure to Survey Large Loads of Matl Thoroughly.Area Cleaned Up & Procedure 12-5 Revised ML20084R9011977-03-23023 March 1977 Telecopy Ro:On 770322,while Completing Operability Surveillance Following Maint on Sys Air Compressors,Diesel Generator Field Failed to Flash & Diesel Generator 2/3 Failed to Start on First Attempt.Cause Unknown ML20084A0611976-12-20020 December 1976 Telecopy Message of Ro:On 761220,empty Spent Fuel Cask Areas Found W/Removable Contamination ML20084L7821976-12-15015 December 1976 RO 50-237/1974-27A update.Three-yr Study of Use of phosphorus-bronze in Place of Teflon as Bushing Matl in torus-to-drywell Vacuum Breakers Provides No Justification for Replacement of Teflon Bushings ML20084A0991976-12-15015 December 1976 Telecopy Message of Ro:On 761215,4% Reduction Made in Allowable Maplhgr.Caused by Error in GE ECCS Analysis ML20084A2151976-12-13013 December 1976 RO 50-237/76-66:on 761113,HPCI Sys Injection Valve 2-2301-8 Failed.Valve Repairs to Be Completed at Next Outage ML20084A1391976-12-0606 December 1976 Telecopy Message of Ro:Empty Spent Fuel Shipping Cask Received W/Areas of Removable Surface Contamination ML20084A1811976-12-0202 December 1976 Telecopy Message of Ro:On 761202,empty Spent Fuel Shipping Cask Received W/Areas of Removable Surface Contamination ML20084R9111976-11-19019 November 1976 Telecopy Ro:On 761119,potential HPCI Design Error Discovered Which Could Cause Failure of HPCI Valve MO3-2301-8 During Certain Postulated Conditions.Caused by Design Wiring Problem.Valve Placed out-of-svc in Open Position ML20084R9181976-09-20020 September 1976 Telecopy Ro:On 760914,during Reactor Power Operation, Primary Containment Oxygen Content Found Greater than 4%. Caused by Terminated Unit Shutdown After Sys Min Load Problems Developed ML20084R5841976-06-15015 June 1976 Suppl Rept to ROs 50-249/75-10A,11A & 33A:motors Replaced on Valves 3-1402-4A & 3-1501-5A & Original Motors Sent to Manufacturer for Evaluation.Valve Trips Occurred Due to Undersized Overload Heaters.Mods Initiated ML20090E3751976-03-25025 March 1976 Telecopy Ro:On 760325,through-wall Crack Indication Found on HPCI Steam Supply Line safe-end.Cause Not Stated ML20084S0111976-03-0303 March 1976 Telecopy Ro:On 760303,emergency Electrical Feed to 2/3 Standby Gas Treatment Sys B Unavailable While Sys a out-of- Svc for Filter Replacement.Caused by Diesel Generator out- of-svc Due to Loose Connection in Manual Control Circuit ML20084R9381976-02-18018 February 1976 Follow-up RO 50-249/74-29A:on 740924,through-wall Crack Discovered on Torus/Drywell Purge Line.Probably Caused by Slight Preloading,Resulting in Strain on Piping.Pipe Examined for Other Cracks & Repair Program Initiated ML20084N6301975-12-0808 December 1975 Telecopy Ro:On 751208,Bergen-Patterson Piping Restraint on Cleanup Sys 8-inch Supply Line Inside Drywell Failed Due to Loss of Hydraulic Fluid.Caused by Faulty Zirc Fitting.Zirc Fitting Replaced ML20084N6411975-12-0404 December 1975 Telecopy Ro:On 751204,intermediate Range Monitor 12 Instrument Setpoint Drifted Above Tech Spec Limit.Setpoint Corrected ML20084N6641975-12-0202 December 1975 Telecopy Ro:On 751201,offgas Activities Increased During Steady State Operations.Probably Caused by Fuel Degradation. Testing in Progress ML20090E4351975-11-17017 November 1975 Telecopy Ro:On 751116,quarterly Closure Time of IC MSIV Found Below Tech Spec Limit.Valve Repaired ML20090E4381975-11-0303 November 1975 Telecopy Ro:On 751103,torus Level Exceeded Tech Spec Limits. Caused by Water Being Pumped from Storage Tank to Torus During HPCI Surveillance Check ML20084N6691975-10-17017 October 1975 Ro:On 751008,portable Fuel Loading Chamber Containing 2 G SNM Declared Lost.Caused by Lack of Proper Storage.Rev of Nuclear Procedures Will Be Initiated ML20084N6791975-09-29029 September 1975 Telecopy Ro:On 750928,leak Discovered in Feedwater Heater 3D3 Normal Drain Line at Weld Attachment to 4 Inch Pipe Support.Caused by Undercut Weld During Original Installation ML20090E4521975-09-29029 September 1975 Telecopy Ro:On 750929,HPCI Turbine Failed to Shut Down. Caused by Damaged Trip Solenoid Coil ML20090E4551975-09-29029 September 1975 Telecopy Ro:On 750929,pressurizing 21-2 D/W Went to 3 Psig. Caused by Excess Nitrogen Added Through Normally Closed Manual Bypass Valve ML20090E4721975-09-11011 September 1975 Telecopy Ro:On 750911,diesel Generator Cooling Water Pump Breaker on Bus 28-3 Tripped ML20084N7031975-09-0808 September 1975 Telecopy Ro:On 750908,five of Eight Intermediate Range Monitoring Instrument Channels Failed to Respond During Reactor Startup.Caused by Open Cables Due to Personnel Contact ML20090E4951975-09-0202 September 1975 Telecopy Ro:On 750830,diesel Generator Tripped,Following Generator Cooling Water Pump Failure.Investigation Continuing ML20084N8531975-08-28028 August 1975 Telecopy Ro:On 750826,isolation Condenser Pressure Switches PS3-263-53A,53B & 53C Setpoints Above Tech Spec Limit. Probably Caused by Setpoint Drift Due to Inactivity During Refuel Outage ML20084N7411975-08-28028 August 1975 Telecopy Ro:On 750828,reactor Pressure Scram Bypass Switches PS3-263-51A & 51B Drifted Above Tech Spec Limit.Caused by Inactivity of Switches During Refueling Outage ML20084N8611975-08-28028 August 1975 Telecopy Ro:On 750826,pressure Switches PS3-263-53A,53B & 53C Drifted Above Tech Spec Limit.Probably Caused by Inactivity Due to Refueling Outage ML20084N8591975-08-28028 August 1975 Telecopy Ro:On 750828,scram Bypass Switches PS3-263-51A & 51B Showed Instrument Drift Above Allowable Limit.Probably Caused by Inactivity Due to Refueling Outage ML20084N9011975-08-27027 August 1975 RO 50-249/75-33:on 750728,suction Valve for LPCI Pump MO-3-1501-5A Tripped Twice on Thermal Overload.Caused by Defective Motor.Motor Replaced ML20084N8021975-08-25025 August 1975 Telecopy Ro:On 750824,during Instrument Surveillance,Scram Switches PS3-263-55A,B & C Found to Have Drifted.Apparently Caused by Inactivity ML20084N8741975-08-21021 August 1975 Telecopy Ro:On 750821,main Feed Breaker to Bus 34-1 Failed to Trip During Trip Testing.Cause Not Stated.Investigation Underway ML20084N8901975-08-0808 August 1975 Telecopy Ro:On 750808,isolation Condenser Condensate High Flow Switches 3-1349A & 3-1349B Failed to Trip within Tech Spec Limit.Apparently Caused by Instrument Setpoint Drift. Switches Reset ML20084N9111975-07-22022 July 1975 Telecopy Ro:On 750722,location of Broken Tack Welds on Jet Pump Restrainer Clamp Bolt Keepers Determined During Tv Exam of Jet Pumps 6 & 17.Cause Not Stated.Tack Welds Will Be Rewelded Under Water ML20084N9471975-06-27027 June 1975 Telecopy Ro:On 750627,during Overhaul Operations,Cracks Found on Collet Housing Portion of Control Rod Drive Housing Outer Tube.Cause Not Stated.Control Rod Drive Manufacturer Contacted to Determine Extent of Problems ML20084N9841975-06-0505 June 1975 Telecopy Ro:On 750605,actuation of Standby Liquid Control Sys Pump Discharge Release Valve Below Tech Spec Limit. Caused by Procedural Inadequacy ML20084P8051975-06-0202 June 1975 Telecopy of Ro:On 750330,during Refueling Outage Surveillance,Excessive Leakage Through Primary Containment Feedwater Isolation Check Valves 3-220-58B & 3-220-62B Observed.Caused by Failed Valve Disc Seal ML20084D3501975-05-16016 May 1975 Telecopy Ro:From 750421-23,personnel Were within Line of Sight of Core During Rod Withdrawal.Caused by Personnel Error.Operation Terminated When Violation Became Known ML20084D3921975-05-0808 May 1975 Ro:On 750507,control Rod Drive Return Line Check Valve Failed to Pass Local Leak Rate Test.Valve to Be Repaired Prior to Startup ML20084R4041975-04-29029 April 1975 Telecopy Ro:On 750429,HPCI High Temp Isolation Switches Drifted During Operations Exceeding Tech Spec Limit.Caused by Drift of 12 Sensors Found During Refueling Outage.Sensors Will Be Replaced W/Capillary Type Switches ML20084R4061975-04-28028 April 1975 Telecopy Ro:On 750428,HPCI High Temp Isolation Switches Drifted During Operations,Exceeding Tech Spec Limit.Caused by Drift of 12 Sensors Found During Refueling Outage. Switches Will Be Replaced W/Capillary Type Switches ML20084Q6141975-04-25025 April 1975 Telecopy Ro:On 750425,during Refuel Outage Local Leak Rate Testing,Excessive Leakage Discovered Through Torus to Drywell Vacuum Breaker 3-1601-32B.Cause Not Stated.Valve Will Be Inspected & Repaired During Outage ML20085J9881975-04-23023 April 1975 Telecopy Ro:On 750423,during Refuel Outage Surveillance, Feedwater Check Valves 3-220-58A & 62A & Feedwater Line 3A Failed to Pass Leak Rate Test.Cause Not Stated ML20084Q6831975-04-23023 April 1975 Telecopy Ro:On 750423,during Refuel Outage Surveillance, Feedwater Check Valves 3-220-58A & 62A & Feedwater Line 3A Failed to Pass Local Leak Rate Test.Cause Not Stated.Valves Will Be Inspected & Repaired ML20084R4431975-04-17017 April 1975 Telecopy Ro:On 750417,main Steam Line D Drywell Penetration X105D Failed to Pass Containment Local Leak Rate Tests. Caused by Broken Testline Which Penetrates Bellows Type Penetration Between Primary & Secondary Bellows ML20084T0331975-04-0404 April 1975 RO 50-249/75-18:on 750324,during Surveillance Testing,Core Spray Valve 3-1402-4A Failed to Close Electrically.Caused by Fault in Motor Operator.Valve Closed Manually 1994-11-04
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20249C8491999-09-30030 September 1999 1999 Third Quarter Rept of Completed Changes,Tests & Experiments Evaluated,Per 10CFR50.59(b)(2), for Dresden Nuclear Power Station. with ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20210R6081999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Dresden Nuclear Power,Units 1,2 & 3.With ML20209E1291999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20210D3071999-06-30030 June 1999 Corrected Page 8 to MOR for June 1999 for DNPS Unit 3 ML20209J3481999-06-30030 June 1999 1999 Second Quarter Rept of Completed Changes,Tests & Experiments, Per 10CFR50.59.With ML20195G6381999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations ML20206N2821999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20205N7491999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20206B1901999-03-31031 March 1999 First Quarter Rept of Completed Changes,Tests & Experiments Per 10CFR50.59 for Dresden Nuclear Power Station. with ML20207M6921999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20207E9311999-02-26026 February 1999 Part 21 Rept Re Sprague Model TE1302 Aluminum Electrolytic Capacitors with Date Code of 9322H.Caused by Aluminum Electrolytic Capacitors.Affected Capacitors Replaced ML20199M0891999-01-22022 January 1999 Part 21 Rept Re Failure of Square Root Converters.Caused by Failed Aluminum Electrolytic Capacitory Spargue Electric Co (Model Number TE1302 with Mfg Date Code 9322H).Sent Square Root Converters Back to Mfg,Barker Microfarads,Inc ML20199D3261998-12-31031 December 1998 10CFR50.59 SER for 1998-04 Quarter, of Changes,Tests & Experiments.With ML20199C8951998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Dnps,Units 1,2 & 3 ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with ML20197G8591998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Dresden Nuclear Power Station.With ML20196J0061998-11-19019 November 1998 Rev 66 to Topical Rept CE-1-A, QA Program ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB ML20195D2861998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Dresden Nuclear Power Station.With ML20154N4131998-09-30030 September 1998 1998 Third Quarter 10CFR50.59 Rept, for Dresden Nuclear Power Station of Completed Changes,Tests & Experiments ML20154L3681998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20153C5061998-09-21021 September 1998 SER Accepting Qualified Unit 1 Supervisor Initial & Continuing Training Program for Dresden Nuclear Power Station,Unit 1 ML20151Y2711998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20237A1341998-08-0707 August 1998 Safety Evaluation Supporting Amend 163 to License DPR-25 ML20237A7161998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20236M6041998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20236F8131998-06-30030 June 1998 Rev 0 to Defueled SAR Dresden Nuclear Power Station Unit 1 Commonwealth Edison Co ML20236T8331998-06-30030 June 1998 COLR for Dresden Station Unit 3,Cycle 15 ML20236T8391998-06-30030 June 1998 Rev 1 to EMF-96-141, Dresden Unit 3 Cycle 15 Reload Analysis Rept ML20236Q5851998-06-30030 June 1998 1998 Second Quarter 10CFR50.59 Rept, for Dresden Nuclear Power Station of Completed Changes,Tests & Experiments ML20248M3021998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted ML20247F3391998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20217D0281998-04-22022 April 1998 Part 21 Rept Re Additive Constants Used in MCPR Determination for Siemens ATRIUM-9B Fuel by Core Monitoring Sys Were Found to Be non-conservative.SPC Personnel Notified All Customers w/ATRIUM-9B Lead Test Assemblies ML20216C9651998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20216D4411998-03-31031 March 1998 First Quarter Rept of Completed Changes,Tests & Experiments for 10CFR5059 ML20216E2531998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Dresden Nuclear Power Station ML20203K5201998-02-25025 February 1998 Safety Evaluation Supporting Amends 165 & 160 to Licenses DPR-19 & DPR-25,respectively ML20203H2441998-02-25025 February 1998 Safety Evaluation Supporting Amends 166 & 161 to Licenses DPR-19 & DPR-25,respectively ML20202F7831998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Dresden Nuclear Power Station ML20199K1651998-01-23023 January 1998 Rev 65h to Topical Rept CE-1-A, Comm Ed QA Tr ML20202E2971998-01-0505 January 1998 Safety Evaluation Supporting Amends 164,159,179 & 177 to Licenses DPR-19,DPR-25,DPR-29 & DPR-30,respectively ML20198P5321997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Dresden Nuclear Power Station ML20198P7021997-12-31031 December 1997 Fourth Quarter Rept of Completed Changes,Tests & Experiments Per 10CFR50.59 ML20216D3611997-12-31031 December 1997 Unicom Corp 1997 Summary Annual Rept ML20203F8781997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Dresden Nuclear Power Station ML20199B0701997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Dresden Nuclear Power Station 1999-09-30
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PMS MR J y aRv DMECTOR DIRECTORI ATE OF LICENSING US ATOMIC ENERGY COMMISSION WUX WASHDC 20545 SUBJECT DPR-25 DRESDEN NUCLEAR POWER STATION UNIT 3 THIS WILL CONFIRM A CONVERSATION WITH MR MAURA OF YOUR OFFICE AT 1500 HOURS THIS DATE CONCERNING FAILURE OF MO-3-1201-2 TO ISOLATE ON LOW REACTOR LEVEL A80VE Wil NOVEMBER 27, 197:a OTHER VALVES IN THE SYTEM CLOSED PROPERLY.
INITI ATING SIGNAL WAS RESULT OF FEED WATER CONTROL SYSTEM PROBLEM AND NOT ASSOCI ATED WITH CLEAN UP PIPING LEAKS ELECTRICI AN FOUND PRO 8LEM WITH AUXILI ARY CONTACT ON BREAKER COIL AND C,0RRECTED SAM E.
VALVE WAS SATISFACTORILY CYCLED PRIOR TO REACTOR START UP W P WORDEN, SUPERINTENDANT DRESDEN NUCLEAR POWER STATION f,,
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Q, ATOMIC ENERGY COMMISSION J
o DIRECTORATE OF REGULATORY OPER ATIONS jg REGION lli
%rts o' "p 799 ROOSEVELT ROAD mag GLEN ELLYN. ILLINOIS 60137 (312) 858-2660 November 27, 1973 Comonwealth Edison Co:npany Dockets No. 50-10 ATTN Mr. Byron Lee, Jr.
.30-23Z 50-2497 (50-254 Vice President P. O. Box 767 Chica'go, Illincis 60690 50-265 Centiment The enclosed Directorato of Regulatory Operations Bulletin No. 73-6,
" Inadvertent Criticality in a Loiling Water Reactor," io sent to you to provide you with infor: nation that was reported
' Yankee Nucicar Power Corporation concerning an inadvertent criticality incident that was experienced in the Vermont Yankee facility. This information my have direct applicability to your facilitics. Action requested on your part is identified in Sc'ction A of the enclosed bulletin.
Very truly yours, James G. Koppler Regional Director
- a Enclosures RD Bulletin No. 73-6 bec: RO Files DR Central Files PDR Local PDR l
- Ltr dtd 11-8-73 to' Directorate of Regulatory Operations, Region I, I
King of Prucaia, Pa.
- Ltr dtd 11-14-73 to Directorate of Licensing, USAEC, Washington, D.C.
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~J November 27, 1973 Directorate of Regulatory Operations Bulletin No. 73-6 INADVERTENT CRITICALITY IN A BOILING WATER REACTOR We recently received an abnormal occurrence report from the Vermont Yankee Nuclear Power Corporation relating to an inadvertent criticality incident that was experienced at their Vermont Yankee facility. A copy of this report is being sent to you under separate cover to provide you with pertinent details of this event.
At the time of the inadvertent criticality incident, the reactor vessel and primary containment heads were removed, the refueling cavity above the reactor vessel was flooded, control rod friction tests were in progress, the rod worth minimizer was bypassed, and core verification had been in progress. As a result of the incident, no measurable radioactivity was released, no fuel damage resulted and no personnel exposures were experienced. The incident is currently under review l
and evaluation by the Regulutory Staff.
i Action requested by this bulletin is contained in Section A.
A.
Action Requested by Licensees
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In light of this occurrence you are requested to take the following actions. Upon completion of these actions you are requested to i
inform this office in writing, within 45 days of the date of this letter, of the status of each item identified in each paragraph and subparagraph listed below:
1 1.
Procedural Review a.
Control Rod Drive Operating and Testing Procedures (1) Conduct a review of your control rod drive operating and testing procedures to determine that approved l
procedures exist for all operations and tests.
l (2) Verify that appropriate prerequisites are included in the procedures to require testing of associated inter-i locking and protection features before control rod testing is permitted.
l (3) Assure that prerequisites and detailed instructions are provided that dedonstrate compliance with technical specification requirements and design bases.
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Bypass Installation Procedures (Jumpers or Lifting of Leads) i Assure that existing bypass installation procedures have been conservatively reviewed for technical adequacy and for adminis-j strative controls.
c.
Radiation Protection Procedures Assure that procedures for access control and personnel f
accountability in areas subject to accidents are current.
d.
Shift Transition Procedure (Turnover)
Assure that complete and detailed procedures are in effect that provide instructions for a proper and conservative turnover of shift responsibilities. Such procedures must include requirements for communicating the status of all safety related equipment and conditions.
2.
Management controls l
Assure that your management controls that are in effect provide for qualified technical and administrative reviews and approvals of i
temporary circuitry changes and temporary off-normal plant conditions.
This review should assure that the responsibilities and requirements associated with the review and approval, installation, verification, j
removal, and subsequent testing of temporary circuitry changes and temporary off-normal plant conditions are clearly delineated in station procedures, are understood by the station staff, and arc being properly implemented.
3.
Licensed Operator Performance Assure that management provides the necessary opportunities and time so that operators are adequately trained to carry out their
'i assigned responsibilities.
In particular, confirm that shift crew members are provided special training for safety related activities that are infrequent, complex, or have unusual safety significance.
If you have any questions concerning this request, please contact this office.
Enclosure:
AO No. 7331 - Ltr dtd 11/14/73 (separate cover) b s
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UNITED STATES ATOMIC ENERGY COMMISSION j ]
I DIVISION OF COMPLIANCc REGION lli f,
si,,,, p 799 ROOSEVELT ROAD TELEPHONC GLEN ELLYN, ILLINOIS 60137 (sta) ess.2eso NOV 2 7 1973
' LOCAL PUBLIC DOCUMENT ROOMS
- Enclosed are copies of documents listed below relating to Commonwealth Edison Company '
, Docket No(s).
50-10, 50-237, t 50-249 :
Letter to Commonwealth Edison Compary from James G. Keppler dated November 27, 1973.
3 This correspondence is submitted pursuant to arrangements made by the Public Proceedings Branch, Office of the Secretary, for use by 3
the public.
1 Where possible, these materials should be punched and filed in a folder labeled as follows:
a CORRESPONDENCE TO AND FROM APPLICANT OR' LICENSEE q
(Excluding Envirdnmental and Antitrust) 5 :*. ' ja f t i c j c...u e
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' James G. Keppler Regional Director
Enclosures:
As noted above t
ec: Washington " Ulic Document Room, w/enci Central Mali & Files Unit, Document Room Clerk, w/o enc 1 I\\
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