ML20084C578

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AO 251-74-2:on 740812,counting of Daily Composite Steam Generator Secondary Sys Water Sample Revealed Significant Increase in Radiation Level.Cause Unknown.Steam Generator a Will Be Examined by Reactor Vendor to Identify Source
ML20084C578
Person / Time
Site: Turkey Point NextEra Energy icon.png
Issue date: 08/22/1974
From: Schmidt A
FLORIDA POWER & LIGHT CO.
To: Oleary J
US ATOMIC ENERGY COMMISSION (AEC)
References
AO-251-74-2, NUDOCS 8304080109
Download: ML20084C578 (2)


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FLORIDA POWER & LIGHT CONWsw August 22, 1974

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Mr. John F. O' Leary, Director

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Dear Mr. O' Leary:

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ABNORMAL OCCURRENCE NO. 251-74-2 AUGUST 22, 1974 OCCURRENCE DATE:

AUGUST 12, 1974 TURKEY POINT UNIT NO. 4 PRIMARY TO SECONDARY LEAK A.

CONDITION PRIOR TO OCCURRENCE The reactor was in routine operation at 99% power.

B.

DESCRIPTION OF OCCURRENCE At 11:15 a.m. on August 12, 1974, counting of the daily compo-site steam generator secondary system water sample revealed a significant increase in radiation level.

The com tration was 2.1x10- pCi/ml as coripared to <1x10 posite concen-pCi/ml on the previous day.

This increase in concentration was con-sidered to be evidence of a primary to secondary leak.

After the primary to secondary leak was discovered, the steam generators were sampled individually to identify which steam generator contained the leak.

From the gross activity level of each steam generator, it was apparent that the leak was in the "A"

steam generator.

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CAUSE OF OCCURRENCE The specific mechanism of the primary to secondary leakage has i

not been determined.

However, as stated in the corrective action, the reactor was shut down to continue the investigation into the cause.

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ANALYSIS OF THE OCCURRENCE-Upon detection of the increased activity in the steam generator, the primary coolant leak rate was immediately calculated.

The calculation showed a leakage of 0.116 gl m which is considered i

normal.

Subsequent calculations have shown-leakages of this same magnitude, indicating that the primary to. secondary leak was.not increasing.

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Mr. John F. O' Leary, Director Page 2 August 22, 1974 Failure of the 4-R-19 radiation detector (AO-251-74-3) to detect the increase in activity resulted in steam generator blowdown being discharged to.the cooling canals for a maximum of 27.4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />.

Calculations show that the maximum activity which could have been discharged to the cooling canals was 10.4 mci.

This represents s.2% of the quarterly limit allowed by the Technical Specifications.

After this discharge, the accumulated activity of the total plant discharge to the cooling canals _ for the month was <.3% of the quarterly limit.

An extensive program of process sampling, radiation monitoring and Icak rate calculation was initiated and continued until reactor shutdown.

Sampling revealed that there was no detect-abic airborne activity at the generating station boundary.

Thus, no established limits were exceeded, and neither reactor safety nor the health and safety of the public were jeopardized by this occurrence.

E.

CORRECTIVE ACTION The immediate corrective action consisted of:

1)' Terminating the steam generator blowdown to minimize the radioactive liquid effluent releases, and 2) Monitoring the secondary system in accordance with the Technical Specifications.

A reactor shutdown was initiated on August 18, 1974.

During the shutdown, the reactor vendor will examine the "A" steam genera-tor to identify the source of the leakage and make appropriate repairs.

As part of the permanent corrective action, Florida' Power G Light Company and the NSSS Vendor are evaluating alternate methods of steam generator water treatment.

F.

FAILURE DATA i

This occurrence represents the first primary to secondary leak the Turkey Point Nuclear Units.

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Very truly yours,

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  1. 3t' D Schmidt p

i liregt'or of power Resources DWR/cpc cc:

Mr.' Norman.C. Moscicy Jack R. Newman, Esquire.

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