ML20082S021

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Monthly Operating Rept for Aug 1991 for Jm Farley Nuclear Plant Unit 2
ML20082S021
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 08/31/1991
From: Dennis Morey, Woodard J
ALABAMA POWER CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9109160342
Download: ML20082S021 (5)


Text

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J. D. Woodard /\\l{}flillll()lk)W(T if, ['"" Septanber 12, 1991 Docket No. 50-364 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D. C. 20555 Joseph M. Farley Nuclear Plant Unit 2 Monthly Operatina Data Report Attached is the August 1991 Monthly Operating Report for Joseph M. Farley Nuclear Plant Unit 2, as required by Section 6.9.1.10 of the Technical Specifications. If you have any questions, please advise. Respectfully submitted, C J a"rd N. AEJ:edb3014 Attachments cc: Mr. S. D. Ebneter Mr. S. T. Hoffman Mr. G. F. Maxwell J'(kf 9109160342 910831 ADOCK 0500g-{$/ 4 ,4 DR

JOSEPil M. FARLEY NUCLEAR PLANT UNIT 2 NARRA11VE SLM MRY Of OPERATIONS August 1991 There was one reactor trip during the month of August. At 1704 on August 6, while operating at approximately 100 percent power, a reactor trip occurred. Apparently, a lightning induced transient in the rod conirol system caused some of the control rods to drop which resulted in a negative flux rate reactor trip. Testing and inspection of the rod control system revealed no damage. All power susply voltages were normal and the surge suspressor on the rod control power ca)inets backup power supplies was found to se functioning properly. All control rods were exercised several times and the operability of the rod control system was verified per FNP-2-STP-5.0 (full Length Control Rod Operability Test) and TNP-0-ETP-3643 (Verification of Rod Control System Operability). The following major safety-related maintenance was performed during the month: 1. 2E Service Water Pump and Motor was replaced on 8-15-91 and returned to service on 8-22-91. 2. 2B Service Water Pump was replaced on 8-27-91 and returned to service on 8-28-91. 3. Miscellaneous corrective and preventive maintenance was performed on the diesel generators. 1 l l File:mm/licens/nrc-mont

t l i i OPERATING 1&TA REP 0KF j DOCKET No. 50-364 t*' lit ~5eptember 5, 119T COMP 1271lD BY D. H. Morey TELEPHONa'T203T897 5136 I OPERATING S1h1US ~ Notes l

1. Unit Name:

Joseph M. rarley - Unit 2

1) Cumulative data since
2. Reporting Period:

August 1991 7-30-81, date of

3. Licensed %ermal Power (twt):

2,652 cormercial operation.

4. Nameplate Rating (Gross PHe):

560

5. Design Electrical Rating-(Net ~lNe): -829 l
6. Maximim Dependable Capacity (Gross twe):

864.2 i

7. Maximum Dependable Capacity (Net IWe):

824.0.

8. If Changes Occur in Capacity _ Ratings (Items Number 3 2 rough 7) Since Last Report, l

Give Reasons: N/A j

9. Power Level To Which Restricted, If Any (Net IWe):

N/A

10. Reasons For Restrictions, If Any N/A y

l Wis Month Yr-to-Date Cummilative i

11. Hours In Reporting Period 744 5,831.

88,440_

12. Number Of Hours Reactor Was Critical 724.2 5,551.1 75,935.3
13. Reactor Reserve Shutdown Hours 0.0 0.0 135.0
14. Hours Generator On-Line 716.3 5,448.3 T4,999.5

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15. Unit Reserve Shutdown Hours 0.0 0.0 0.0

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16. Gross hermal Energy Generated (tWH) 1,874,009

'T4~123,923 131,327,872 ' ' ~

17. Gross Electrical Energy Generated (!HH) 604,202 4,588,354

'52,794 3T6"~ ~

18. 'Not Electrical Energy Generated (IMH) 574,302 4,357,382

~5F,5~51,300-j

19. Unit Service Factor 96.3 93.4 84.8
30. Unit Availability Factor 9W 93R 84.8
21. Unit Capacity Factor (Using MDC Net) 93.7 90 91.3
23. Unit Capacity Factor (Using DER Net) 93.1 90.'l

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33. Unit Forced Outage Rate 3.7 4.4 43

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24. Shutdowns Scheduled over Next 6 Months (Type, Date, and Duiration of Each):

N/A r

25. If Shut Down At End Of Report Period, Estimated Date of Startup: N/A I
26. Units In Test Status-(Prior to Commercial Operation) -

Forecast Achieved l ~ INITIAL CRITICALITY 05/06/81 05/08 03 f INITIAL ELEC1RICITY 05/24/81 U5' I~ 00fMERCIAI. OPERATION DB/01/B1 07/30/81 [ l rorm 2/30 i i

l 1 f DOCKET No. 50-364 f UNIT 2 i DATE September 5, 1991 ~ f COMPLETED BY D. N. Morey { TELEN10NE (205)S99-5156 HONTH August DAY AVERAGE DAILY POVER LEVEL DAY AVERAGE DAILY POVER LEVEL-(MVe-Het) (MVe-Net) [ i -1 81 7 17 816 i ~ t 2-815 18 81_4 r i 3 814 19 815 4 811 20 820 5 811 21 824 6 570 22 824 7 0 23 820 8 527 24 817 9 811 25 817 10 812 26 817-11 816 27 814 12

_816, 28 813 13-817 29 814 14 818 30 815-

-15 821- '31 816 16 819 INSTRUCTIONS On.this format, list the-average daily unit power level in MVe-Net for each day in the reporting month. Compute _to the nearest whole megavatt. ~

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OWIT SEUTDDaWS AND POWER REDUCTIONS DOC 72T 50. 50-364 ERRIT EARE 3 P. FAR127 - YMrIT 2 ORTE Sottoeber 5,1991 COMF12TED BY D. W. Y93EPET REPORT N3NTE AUGUST TE1.EF90WE (2951899-$1Y* l l l l l l METWOO OF l LICENSEE l l l CAESE & CORRECTITE l l l l l DURATION l SEUTTING l ETENT l SYSTEM l COMPOEN3rT l ACTIDW TO

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I onTE I TTFr* i ta= RS) 5 I REreRT e i C=E' l CooE l rRETEnr RE( - l l 037 j 910806 l F l 27.7 l B l 3 l 91485 l IS l RCO lA ligestning imdweed transient in the red centrol l l l l l l l l l l l system caused some of the control rods to drop l l l l l l l l l l lwhich resulted in a megatioe flum rete reacter l 1 1 I i i l I i i lerie-1 1 1 1 1 I t I i i i I l l l l l l l l l l Testing med inepecties of the red centrol systee l l l l l l l l l lreeenled me damage. All power supply eeltages l l l l l l l l l lwere aermal and the serve suppressor em the red l l l l l l l l l l l control power cabioets backey power supplies was l l l l l l l l l l jfound t. %e tenetioning properly. All control reds l l l l l l l l l l lwere esercised seeeral times and the o erability ofl v l l l l l l l l l lthe red control system was eerified per l 1 I I I i i i I I trw -a-sTr-5

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I I l l l I I I I I I I l l l l l l l l l lAn engineering stedr has boom initiated to l 1 1 I I I I I I I I *ter=i== See to pr - e foremer lige.tmi.g l l l i I i i i i i lind=ced re-ter tries. I i 1 1 I I I I I I I I i I I I i i i l i i I F: Forced Reason: Method: Exhibit 4-Zestructices S: Scheduled A-Equipment Failure (Esplain) 1-Manual for Preparaties of Data B-Maintenance or Test 2-Manual Scram. Entry Sheets for Licensee C-Refueling 3-Antematic Scram. Eowet Report (12R) File (NUREG-D-Regulatory Restraction 4-other (Emplaial 9161) E--Operator Training & License Esamination F-Administratioe Exhibit I -Sese Searco G-operational Error (Explaimp H 4 her (Emplain) Page 1 M Rxm M __}}