ML20078K633
| ML20078K633 | |
| Person / Time | |
|---|---|
| Site: | Davis Besse |
| Issue date: | 09/08/1983 |
| From: | Sarsour B TOLEDO EDISON CO. |
| To: | |
| Shared Package | |
| ML20078K615 | List: |
| References | |
| NUDOCS 8310190170 | |
| Download: ML20078K633 (2) | |
Text
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REVISION 1 OPERATING DATA REPORT DOCKET NO.
50-346 DATE Seotember 8, 1983 COMPLETED BY Bilal Sarsour TELEPHONE 419-259-5000, Ext. 384 OPERATING STATUS
- 1. Unit Name:
Davis-Besse Unit 1 Notes
. 2. Reporting Per".t:
July, 1983
- 3. Licensed Thermal Power (MWt):
2772
- 4. Nameplate Rating (Gross MWe):
925
- 5. Design Electrical Rating (Net MWe):
ons
- 6. Maximum Dependable Capacity (Gross MWe):
918
- 7. Maximum Dependable Capacity (Net MWe):
874
- 8. If Changes Occur in Capacity Ratings (Items Nuraber 3 Through 7) Since Last Report. Give Reasons:
- 9. Power Level To which Restricted. If Any (Net MWe):
- 10. Reasons For Restrictions.If Ar.y:
This Month Yr to-Date Cumulative
- 11. Hours In Reporting Period 744.0 5,087.0 43,848.0 12.- Number Of Hours Reactor Was Critical 588.4 4,591.2 25,486.7
- 13. Reactor Reserve Shutdown Hours 155.6 469.5 3,833.6
- 14. Hours Generator On.Line 588.4 4,538.8 24,298.4
- 15. Unit Reserve Shutdown Hours 0.0 0.0 1.732.5
- 16. Gross Thermal Energy Generated (MWH) 1.202.826 11.534.142 56.906,903
- 17. Gross Electrical Energy Generated (MWH) 394.838...
3.841.150 18,946,804
- 18. Net Electrical Energy Generated (MWH) 366.862 3,631,352 17,746,792
- 19. Unit Service Factor 79.1 89.2 55.4
- 20. Unit Availability Factor 79.1 89.2 59.4
- 21. Unit Capacity Factor (Using MDC Net) 56.4 81.7 46.3
- 22. Unit Capacity Factor (Using DER Net) 54.4 78.8 44.7 l 1l
- 23. Unit Forced Outage Rate 12.4 9.5 18.7 i
- 24. Shutdowns Scheduled Over Next 6 Months (Type. Date,and Duration of Each):
i
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
September 20, 1983
- 26. Units in Test Status (Prior to Commercial Operation):
Forecast Achiesed INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIA L OPER ATION (9/771 8310190170 830908 PDR ADOCK 05000346 R
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REVISION 1 50-346 UNIT SHUTDOWNS AND POW:dt REDUCliONS DOCKET NO.
UNIT NAME Davis-Besse Unit 1 DATE September 82,1983 COMPLETED ilY Bilal Sarsour REPORT MONTil July 1983 TELErilONE (419) 259-5000. Ext. 384 "E
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3 h.!f k Licensee
,E*
Cause & Corrective No.
Date k
3g
.g jg5 Event 3,7 Attion to 8-
$5 jigg Repor y
Prevent Recurrence 8r mu i
6 t
1l 7
83 07 25 F
83.6 A
3 The reactor tripped due to Steam and Feedwater Rupture Control System (SFRCS) actuation.
1 8
83 07 29 s
72.0 C
9 A unit outage was initiated to per-e form scheduled maintenance and refueling work, i
Sce Operational Summary for further details.
t t
I 2
3 4
l F: Forced Reason:
Method:
Exhibit G. instructions S: Schedu!cd A Equipment Failure (Explain) 1-Manual for Preparation of Data 1
B-Maintenance of Test 2 Manual Scrarri.
Entry Sheets for Licensee C Refueling 3-Automatic Scram.
Event Report (l.ER) File (NUREG-D-Regulatory Restriction 4-Continuation from Previous Month 0161)
E. Operator Training & License Examination l 5-Load Reduction j
F Administrative 9-Other (Explain)
S G Operaniunal Eirur (lixplain)
Exliibit i Same Saurce (9/77) ll-Other (E xplain)