ML20078K246

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Monthly Operating Rept for Aug 1983
ML20078K246
Person / Time
Site: Beaver Valley
Issue date: 09/07/1983
From: Carey J, Holtz J
DUQUESNE LIGHT CO.
To:
NRC
References
NUDOCS 8310190019
Download: ML20078K246 (5)


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OPERATING DATA REPORT DOCKET NO. 50-334 DATE 9-7-83 COMPLETED BY _J.

L. Foltz TELEPHONE. 4' ' 441 I369 OPERATING STATUS

1. Unit Name: Beaver Valley Power Station. Unit #1 Notes
2. Reporting Period:

August, 1983

3. Licensed Thermal Power (MWt):

M

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4. Nameplate Rating (Gross MWe):

923

5. Design Electrical Rating (Net MWe):

835

6. Maximum Dependable Capacity (Gross MWe):

860

7. Maximum Dependable Capacity (Net MWe):

810

8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since last Report, Give Reasons:
9. Power Level To Which Restricted.If Any (Net MWe):

None

10. Reasons For Restrictions,If Any:

N/A This Month Yr to.Date

" Cumulative II. Hours !n Reporting Period 744 5,831 64,295

12. Number Of Houn Reactor Was Critical 0

3,718.9 28,536.4

13. Reactor Reserve Shutdown Hours 0

0 4,482.8

14. Hours Generator On.Line 0

3,708.2 27,508.4

15. Unit Reserve Shutdown Hours 0

0 0

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16. Gross Thermal Energy Generated (MWH) 0 9,476,64'3.8 61,986.830.2
17. Cross Electrical Energy Generated (MWH) 0 3,091,400 19,604,040
18. Net Electrical Energy Generated (MWH)

-2,848 2,941,317 13,153,434

19. Unit Service Factor 0

63.6 44.7

20. Unit Availability Fictor 0

63.6 44.7

21. Unit Capacity Factor (Using MDC Net) 0 62.3 38.2 j
22. Unit Capacity Factor (Using DER Net) 0 60.4 37.1
23. Unit Forced Curage Rate 0

4.0 32.Q

24. Shutdowns Scheduled Over Next 6 Months ! Type. Date.and Duration of Each):

The station was shutdown for the 3rd refueling on June 10, 1983.

Scheduled startup is Seotember 22, 1983,

25. If Shut Down At End Of Report Period. Estimated Date of Startup: September 22, 1983
26. Units in Test Status (Prior to Commercial Operation):

Forecast Achieved INITIAL CRITICALITY N/A N/A l

INITIAL ELECTRICITY N/A N/A l

COMMERCIA L OPERATION N/A N/A 8310190019 830907 PDR ADOCK 05000334 i

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UNITSifUTDOWNS AND POWER REDUCTIONS DOCKET NO.

50-334 UNIT NAME BVPS Unit #1 DATE 9-7-83 REPORT MONiil August COMPLETED BY J.

L. Ifoltz 1ELEril0NE _412-643-1369

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8 g.=5 Licemce j't, No.

Date Cause & Conective o;

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,g5 Event r3 y0" Action to P

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EO Preveni Recurrence S

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06/10/83 S

1968.6 C

1 N/A ZZ ZZZZZZ Shutdown for 3rd refueling and major modifications outage.

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F: Fosced Reason:

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S Scheduled A.Eiguipment Failure (Explain)

Exhibit G-Insenscilons liethod:

1-Manual B. Maintenance of Test for PsepasJIion of Data 2-Manual scram C RcIncling Ento Sheets for 1.icensee 3-Automatic Scram D-Regulatos) Restriction Eveni Rep.us a1.I'R t I'de INURI'G 4-Continued From Previous Month 01611 l

l' Operatos Training & lAense l'xamination F. Administrative 5-Reduction i

9-Other 5

G-Operaliunal 1:nos ll xplain) 19/77)

Il Olher (lisplain t 1:zhibit I. Same, Source r

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of NARRATIVE

SUMMARY

OF MONTHLY OPERATING EXPERIENCE - AUGUST, 1983 August 1 The station was in operational mode 6 except that no fuel through was in the reactor vessel. The replacement of the control rod August 6 guide tube split pins was in progress. All fuel was in the spent fuel pool and all reactor coolant loops were isolated and drained. All steam generators were drained on both primary and secondary sides. The spent fuel pool cooling and purification system was controlling decay heat.

August 7 The split pin replacement wa-completed on the 7th. On the 9th, through the secondary side of the IB Steam Generator was hydro tested August 13 following the completion of tube plugging' On the 10th, the lA Reactor Coolant Loop was filled and v,ented, as was the 1B Loop on the 12th.

Both loops were returned to service.

Fuel loading began at 0204 hours0.00236 days <br />0.0567 hours <br />3.373016e-4 weeks <br />7.7622e-5 months <br /> on the 13th.

August 14 The station was in operational mode 6 with fuel loading in progress when a cable broke on the fuel upender at 0945 hours0.0109 days <br />0.263 hours <br />0.00156 weeks <br />3.595725e-4 months <br />. The fuel transfer canal was isolated and drained to allow the upender cable to be replaced.

August 15 Following repairs to the fuel upender, the fuel transfer canal was unisolated then reflooded, and fuel loading resumed at 0615 hours0.00712 days <br />0.171 hours <br />0.00102 weeks <br />2.340075e-4 months <br />.

August 16 Fuel loading was completed at 0141 hours0.00163 days <br />0.0392 hours <br />2.331349e-4 weeks <br />5.36505e-5 months <br />.

August 17 Work began on installing the upper internals in the reactor vessel.

through It was discovered that a fuel assembly, K-2, had been damaged August 25 while reloading the core. At 1949 hours0.0226 days <br />0.541 hours <br />0.00322 weeks <br />7.415945e-4 months <br /> on the 25th, movement of 67 fuel assemblies frca the reactor vessel to the spent fuel pool was begun in order to inspect the damaged assembly.

The 1C Reactor Coolant Loop was filled and vented on the 24th.

August 26 The station was in operational mode 6, refueling. At 2315 hours0.0268 days <br />0.643 hours <br />0.00383 weeks <br />8.808575e-4 months <br /> the movement of fuel was completed. The damaged assembly, K-2, was the last one removed from the reactor vessel.

August 27 The station was in operational mode 6 with RCS temperature and through pressure at ambient conditions.

Fuel reloading was started at August 31 0720 hours0.00833 days <br />0.2 hours <br />0.00119 weeks <br />2.7396e-4 months <br /> on the 31st.

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,, a MAJOR SAFETY-RELATED MAINTENANCE - AUGUST, 1983 1.

The control rod guide tube split pin replacement was completed on August 7.

2.

The replacement of the seals in the Bergen-Patterson snubbers is in progress.

3.

The 1A Reactor Coolant Pump motor was repaired and the thrust bearings were inspected.

1 4.

A sample eddy current inspection was done on the 1B and 1C Steam Generators.

5.

Secondary side inspection of the 1A, 1B, and 1C Steam Generators.

6.

The seals were replaced in the 1B Main Feedwater Pump.

7.

All three containment air recirculation fan motors were overhauled.

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'At3 Telephone (412) 39%000 Nuclear Division P.O. Box 4 Shippinoport. PA 15077-0004 September 7, 1983 Beaver Valley Power Station, Unit No. 1 Docket No. 50-334, License No. DPR-66 Monthly Operating Report United States Nuclear Regulatory Commission Director, Office of Management Information & Program Control Uashington, D.C.

20555 Ge'Itlemen:

In accordance with Appendix A, Technical Specifications, the Monthly Operating Report is submitted for the month of August, 1983.

Very truly yours, J. J. Carey

" ice President Nucle.ar Division Enclosures cc: NRC Regional Of fice, King of Prussia, PA

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