ML20076D440

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Responds to NRC Re Violations Noted in IE Insp Repts 50-321/83-15 & 50-366/83-15.Corrective Actions:Seal Water Shutoff Valve Locked & Valve Handwheels Painted Bright Orange
ML20076D440
Person / Time
Site: Hatch  Southern Nuclear icon.png
Issue date: 07/12/1983
From: Gucwa L
GEORGIA POWER CO.
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20076D433 List:
References
NED-83-387, NUDOCS 8308230398
Download: ML20076D440 (3)


Text

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Georgia Power Corrpany 333 Piedmont Avenue Attanta, Georg:a 30308 Telephone 404 526-6526 USNRC 'F G N.:

p 7&T7lx5343 AU CA.

dORGIA T

A!!anta, Georg:a 30302 83 Jill 20 All : 42 Geogia Power L T. Gucwa tw soumern elsmc sy tem Chief Nuclear Engineer Power Generat:on Department NED-83-387 July 12, 1983 U. S. Nuclear Regulatory Conmission utzt;xt;rCE:

Office of Inspection and Enforcement RII: JPO Region II - Suite 2900 50-321/50-366 101 Marietta Street, IM I&E Inspection Atlanta, Georgia 30303 Report 83-15 ATIENTION: Mr. Jamcc P. O'Reilly GENIIDEN:

Georgia Power Conpany (GPC) submits the following information in response to I &'E Inspection Report 50-321/83-15 and 50-366/83-15 concerning the routine safety inspection conducted by Mr. R. V. Crlenjak of your office at Plant Hatch.

Violation Technical Specification 6.8.1 requires that procedures controlling the operation of safety-related systems be implemented.

Plant procedure HNP-1-lll7, RHR Service Water, Data Package 1, requires that the seal water shutoff valve for RHR service water pump "D" be locked open. Also plant procedure HNP-1-3358 requires that the isolation valve for cable spreading room sprinkler multimatic valve be locked open.

Contrary to the above, on May 5,1983, tr,. seal water shutoff valve for RHR service water pump "D", Unit 1 was found unlocked.

The chain was locked through the handwheel but not such to prevent valve operation.

On May 29, 1983, the isolation valve for the cable spreading room sprinkler system was found unlocked.

We chain was through the handwheel but not locked.

This is a repeat violation.

See Inspection Report Nos. 50-321/82-12, 50-321/82-20 and 50-321/83-07.

This is a Severity Level IV Violation (Supplement I).

Response

Admission or denial of alleged violation: We violation occurred.

Reason for violation:

Personnel did not follow established controls as specified in plant procedures.

8308230398 830804 PDR ADOCK 05000321 G

PDR

Georgia Power d U. S. Nuclear Regulatory Comnission Office of Inspection and Enforcement

-101 Marietta Street, W Atlanta, Georgia 30303 July 12, 1983 Page 'No Corrective steps which have been taken and the results achieved:

1.

'Ihe subject valves were promptly locked to prevent unauthorized valve position changes.

2.

Valve handwheels at the intake structure which are required to be locked have been painted bright orange. This will aid Operations personnel in identifying valves which are required to be locked at the intake structure.

3.

Access into the intake structure has been restricted.

Operations personnel will monitor work at the intake structure to ensure that valves are locked properly.

Corrective steps that will be taken to avoid further violations:

Because of the recurrent nature of this event, we have determined that the need exists for increased administrative controls.

A program is now being developed which will strengthen the controls for logging and tracking changes in locked valve positions.

This program will require independent verification of the locked position of safety related valves.

Fire protection and instrument valves will be placed under a similar administrative controls program.

To assure compliance, the new program will require closer management overview of its implementation.

Periodic audits will assure compliance with the newly established controls.

This enhanced administrative program will be fully implemented no later than August 31, 1983.

Accessible locked valves will be verified properly locked (under this new program) no later than September 30, 1983.

Date when full compliance will be achieved:

Full compliance was achieved on May 29, 1983, when the isolation valve for the cable spreadire room sprinkler system was properly locked.

On May 5, 1983, the seal water shutoff valve was properly locked.

If you have any further questions, please contact this office.

Very Truly Yours, f.r. q m L. T. Gucwa MJB 700775

1 Georgia Power A U. S. Nuclear Regulatory Comnission Office of Inspection and Enforcement 101 Marietta Street, W Atlanta, Georgia 30303 July 12, 1983

_ Page 'Ihree xc: Mr. J. T. Beckham, Jr.

Mr. H. C. Nix, Jr.

Plant Hatch Senior Resident Inspector 4

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i 700775