ML20076A822
ML20076A822 | |
Person / Time | |
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Site: | LaSalle |
Issue date: | 08/08/1983 |
From: | Schroeder C COMMONWEALTH EDISON CO. |
To: | James Keppler NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
References | |
10CFR-050.55E, 10CFR-50.55E, 7106N, 83-01, 83-1, NUDOCS 8308180346 | |
Download: ML20076A822 (1) | |
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Category:DEFICIENCY REPORTS (PER 10CFR50.55E & PART 21)
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[Table view]SER Input Authorizing Licensee Proposed Request to Modify Definition of Core Alteration in Section 1.0 of TS & Update Sections 3/4.1,3.4.3 & 3/4.9 to Reflect Proposed Definition Change 05000373/LER-1999-003-04, :on 990902,reactor Scram on Low Reactor Water Level,Was Received.Caused by Personnel Error.Appropriate Disciplinary Action Taken with non-licensed Operator1999-10-0404 October 1999
1999-09-30 |
Text
['O Commonwealth Edison
^ ) one First National Plata. Chictgo, Illinois t
"J Address Reply to: Post Office Box 767 (j Chicago, Illinois 60690 August 8, 1983 Mr. James G. Keppler, Director - Region III U.S. Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL 60137
Subject:
LaSalle County Station Unit 2 10CFR50.55(e) Notification 83-01 Correction to Final Report, Riley Temperature Indicating Switches NRC Docket No. 50-374 Reference (a):
C.W.
Schroeder letter to J.G. Keppler dated March 16, 1983.
(b):
C.W. Schroeder letter to J.G. Keppler dated May 3, 1983.
(c):
C.W. Schroeder letter to J.G. Keppler dated June 3, 1983.
Dear Mr. Keppler:
The purpose of this letter is to correct a statement made in 4
Reference (c).
The Unit 2 Riley temperature switches have not yet been recalibrated to the modified calibration procedure suggested by Riley, i
~ 0nly the Unit 1 temperature switches have been recalibrated at this time.
We will complete the calibration on Unit 2, using the same calibration procedure as Unit 1, prior to fuel load.
If there are any questions in this matter, please contact this office.
Very truly yours, k
C.W. Schroeder l
Nuclear Licensing Administrator 1m cc:
Region III Inspector - LSCS Director of Enforcement & Inspection 8308190346 830808 PDR ADOCK 05000374
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