ML20073T142
ML20073T142 | |
Person / Time | |
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Site: | LaSalle |
Issue date: | 05/03/1983 |
From: | Schroeder C COMMONWEALTH EDISON CO. |
To: | James Keppler NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
References | |
10CFR-050.55E, 10CFR-50.55E, 6504N, 83-01, 83-1, NUDOCS 8305100352 | |
Download: ML20073T142 (1) | |
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Category:DEFICIENCY REPORTS (PER 10CFR50.55E & PART 21)
MONTHYEARML20217A1691999-09-22022 September 1999
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Commonwzith Edison T- ' one First National Plaza. Chicago, Illinois O Address Reply to: Post Office Box 767 '
Chicago, lilinois 60690 May 3, 1983 Mr. James G. Keppler, Director Directorate of Inspection and Enforcement - Region III U.S. Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL 60137 i
Subject:
LaSalle County Station Unit 2 10CFR50.55(e) Notification 83-01 Updated Interim Report, Riley Temperature Indicating Switches NRC Docket No. 50-374 Reference (a): C. W. Schroeder letter to J. G.
Keppler dated March 16, 1983.
4
Dear Mr. Keppler:
l Commonwealth Edison filed a 30 day report to your office by Reference (a) concerning the status of the problems we experienced with the Riley temperature switches installed in the leak detection system at LaSalle.
In that report it was indicated that the calibration procedure for these devices would be modified to solve the temperature off-set p;oblem. This effort has been completed and presently the switch units have been recalibrated utilizing the revised procedure and are accurately indicating the proper temperature.
At the time of the 30 day report, we anticipated final resolution of the temperature module problem (hardware modification) by the end of April. Presently, General Electric and Riley are still in the process of finalizing the solution. Meetings are planned in San Jose the week of May 2nd to accomplish this task. Final resolution is currently expected by 6/1/83. A final report will be 1ssued at that time.
If you or your staff have any questions concerning this activity, please contact this office.
Very truly yours, N u" .s j y} o, j i C. W. Schroeder Nuclear Licensing Administrator RAB/CWS/bmb/lm cc: Director of Inspection and Enforcement, Washington, D.C.
Region III Inspector _- LSCS (flh
/ /