ML20072R589

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Monthly Operating Rept for Aug 1994 for Vogtle Electric Generating Plant
ML20072R589
Person / Time
Site: Vogtle  Southern Nuclear icon.png
Issue date: 08/31/1994
From: Hooper G, Mccoy C
GEORGIA POWER CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LCV-0360-E, LCV-360-E, NUDOCS 9409130248
Download: ML20072R589 (12)


Text

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oeorgia Power Company 40 inverness Center Parkway i

Post O'Sce Dox 1295 a

8monghamf Alabama 3520t

' Tetepnor*; 205 877 7122

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m Georgia Power -

C. K. McCoy vce Prewer.t Nuciew

'h" S*'** "CI'C SVstem VOTic Pr%ect

$ p g y g, }994 LCV-0360-E

. Docket Nos. 50-424 50-425 U. S. Nuclear Regulatory Commission i

ATTN: Document Control Desk Washington, D. C. 20555 i

Gentlemen:

VOGTLE ELECTRIC GENERATING PLANT MONTHLY ~ OPERATING REPORT i

Enclosed are the August 1994, monthly operating reports for Vogtle Electric Generating Plant (VEGP) Units 1 and 2. These reports are submitted in accordance with Technical Specification 6.8.1.5.

Sincerely, C. K. McCoy CKM/JLL Enclosures f

cc: _Cgprgia Power Company Mr. J. B. Beasley, Jr.

Mr. M. Sheibani l

NORMS u

U. S. Nuclear Reculatory Commis. sign Mr. S. D. Ebneter, Regional Administrator Mr. D. S. Hood, Licensing Project Manager, NRR Mr. B. R. Bonser, Senior Resident Inspector, Vogtle

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3 ENCLOSURE 1

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VOGTLE ELECTRIC GENERATING PLANT - UNIT 1 MONTHLY OPERATING REPORT FOR AUGUST 1994 l

TABI.E OF CONTENTS

.I NARRATIVE REPORT Page V1-1.

l OPERATING DATA REPORT Page VI-2 AVERAGE DAILY POWER LEVEL Page VI-3 UNIT SHUTDOWNS AND POWER REDUCTIONS

Page VI-4 n

l

,~

NARRATIVE REPORT DOCKET NO, 50-424 UNIT 1 DATE:

SEPTEMBER 1,1994 COMPLETED BY: G. L. HOOPER TELEPHONE:

(706) 826-4104 AUGUST 01 00:00 UNIT 1 AT 100% POWER WITH NO OPERATIONAL PROBLEMS.

AUGUST 12 13:30 UNIT 1 BEGAN COASTDOWN FOR REFUELING OUTAGE.

AUGUST 31 23:59 UNIT 1 AT 78% POWER WITH COASTDOWN IN PROGRESS.

i V1-1

~

OPERATING DATA REPORT DOCKET NO. 50-424 DATE:

SEPTEMBER 1,1994 COMPLETED BY: G. L. HOOPER TELEPHONE:

(706) 826-4104 OPERATING STATUS

1. UNIT NAME:

VEGP UNIT 1

2. REPORT PERIOD:

AUGUST 1994

3. LICENSED THERMAL POWER (MWt):

3565

4. NAMEPLATE RATING (GROSS MWe):

1215

5. DESIGN ELECTRICAL RATING (NET MWe):

1169

6. MAXIMUM DEPENDABLE CAPACITY (GROSS MWe):

1223

7. MAXIMUM DEPENDABLE CAPACITY (NET MWe):

1169

8. IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS 3 THROUGH 7) SINCE LAST REPORT, GIVE REASONS:

NA

9. POWER LEVEL TO WHICH RESTRICTED, IF ANY (NET MWe):

NO RESTRICTIONS

10. REASONS FOR RESTRICTION, IF ANY:

NA THIS MONTH YR. TO DATE CUMULATIVE

11. HOURS IN REPORTING PERIOD:

744 5831 63576

12. NUMBER OF HOURS REACTOR WAS CRITICAL:

744.0 5791.6 55666.7 l

13. REACTOR RESERVE SHUTDOWN HOURS:

0.0 0.0 0.0

14. HOURS GENERATOR ON-LINE:

744.0 5782.0 54654.9

15. UNIT RESERVE SHUTDOWN HOURS:

0.0 0.0 0.0 i

16. GROSS THERMAL ENERGY GENERATED (MWH):

2448946 20146358 183867556

17. GROSS ELEC. ENERGY GENERATED (MWH):

827249 6885338 61868300

18. NET ELEC. ENERGY GENERATED (MWH):

787859 6579458 58820750

19. REACTOR SERVICE FACTOR 100.0 %

99.3 %

87.6 %

20. REACTOR AVAILABILITY FACTOR 100.0 %

99.3 %

87.6 %

21. UNIT SERVICE FACTOR:

100.0 %

99.2 %

86.0 %

22. UNIT AVAILABILITY FACTOR:

100.0 %

99.2 %

86.0 %

23. UNIT CAPACITY FACTOR (USING MDC NET):

90.6%

96.6 %

83.8 %

24. UNIT CAPACITY FACTOR (USING DER NET):

90.6 %

- 96.5 %

83.2 %

25. UNIT FORCED OUTAGE RATE:

0.0%

0.8%

5.1%

26. SHUTDOWNS SCHEDULED OVER THE NEXT 6 MONTHS (TYPE, DATE, AND DURATION OF EACH):

REFUELING, SEPTEMBER 11,1994,29 DAYS

27. IF SHUTDOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP:

NA i

V1-2

4' UNIT 1 AVERAGE DAILY DOCKET NO. 50-424 POWER LEVEL DATE:

SEPTEMBER 1,1994 COMPLETED BY: G. L. HOOPER TELEPHONE:

(706) 826-4104 DAY Net MW 1..

1152 2..

1152 3.

1148 4..

1152 5.

1149 6..

1159 7.

1160 8.

1163 9.

1162 10...

1159 11.

1155 12.,

1147 13.

1126 14.

1109 15..

1096 16.

1081-17.

1064 18..

1058 19.

1044 20.

1019

21..

1010 22.

994-23...

981 24...

971 25...

956 26.

946 27.

928 28..

916 29.

900 30.

893 31.

878 V1-3

UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50-424 DATE:

SEPTEMBER 1,1994

]

UNIT NAME:

VEGP UNIT 1 COMPLETED BY: G. L. HOOPER TELEPHONE:

(706) 826-4104 REPORT MONTH AUGUST 1994 R

M S

E E

Y T

A T

LICENSEE SC Y

S H

EVENT TO COMPONENT CAUSE & CORRECTIVE I

P DURATION O

O REPORT ED CODE ACTION TO NO.

DATE E

(HOURS)

N D

NUMBER ME (SUBCODE)

PREVENT RECURRENCE NA NA NA NA NA NA NA NA NA NA i

F: FORCED REASON:

METHOD:

EVENTS REPORTED INVOLV S: SCHEDULED A-EQUIPMENT FAILURE (EXPLAIN) 1 - MANUAL A GREATER THAN 20%

B-MAINTENANCE OR TEST 2 - MANUAL SCRAM REDUCTION l'-

VEAGE C-REFUELING 3 - AUTO. SCRAM DAILY POWER L= ELFOR D-REGULATORY RESTRICTION 4 - CONTINUATIONS THE PRECEDING 24 HOURS.

E-OPERATOR TRAINING & LICENSE 5 - LOAD REDUCTION F-ADMINISTRATIVE 9 - OTHER (EXPLAIN)

G-OPERATIONAL ERROR (EXPLAIN)

H-OTHER (EXPLAIN)

V1-4

1 L

l ENCLOSURE 2 I

VOGTLE ELECTRIC GENERATING PLANT - UNIT 2.

MONTHLY OPERATING REPORT FOR AUGUST 1994 I

TABLE OF CONTENTS NARRATIVE REPORT Page V2-1 j

OPERATING DATA REPORT Page V2-2 AVERAGE DAILY POWER LEVEL Page V2-3 UNIT SHUTDOWNS AND POWER REDUCTIONS Page V2-4 i

f 9

9 W-4 9

I' NARRATIVE REPORT DOCKET NO. 50-425

)

UNIT 2 DATE:

SEPTEMBER 1,1994 -

COMPLETED BY: G. L. HOOPER TELEPHONE:

(706) 826-4104 1

AUGUST 01 00:00 UNIT 2 IN MODE 5, RHR PUMP REPAIRS IN PROGRESS.

AUGUST 02 14:15 UNIT 2 ENTERED MODE 4.

AUGUST 02 20:57 RHR PUMP REPAIRS COMPLETE.

AUGUST 03 03:30 UNIT 2 ENTERED MODE 3.

AUGUST 03 22:58 UNIT 2 ENTERED MODE 2.

AUGUST 03 23:54 UNIT 2 REACTOR CRITICAL.

AUGUST 04. 04:47 UNIT 2 ENTERED MODE 1.

AUGUST 04 08:02 UNIT 2 GENERATOR TIED TO GRID.

AUGUST 05 23:59 UNIT 2 RETURNED TO 100% POWER.

AUGUST 31 23:59 UNIT 2 AT 100% POWER WITH NO OPERATIONAL PROBLEMS.

I t

k V2-1

OPERATING DATA REPORT DOCKET NO. 50-425 DATE:

SEPTEMBER 1,1994 COMPLETED BY: G. L. HOOPER TELEPHONE:

(706) 826-4104 OPERATING STATUS

1. UNIT N AME:

VEGP UNIT 2

2. REPORT PERIOD:

AUGUST 1994

3. LICENSED THERMAL POWER (MWt):

3565

4. NAMEPLATE RATING (GROSS MWe):

1215

5. DESIGN ELECTRICAL RATING (NET MWe):

1169

6. MAXIMUM DEPENDABLE CAPACITY (GROSS MWe):

1223

7. MAXIMUM DEPENDABLE CAPACITY (NET MWe):

1169 i

8. IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS 3 THROUGH 7) SINCE LAST REPORT, GIVE REASONS:

NA

9. POWER LEVEL TO WHICH RESTRICTED, IF ANY (NET MWe):

NO RESTRICTIONS

10. REASONS FOR RESTRICTION, IF ANY:

NA THIS MONTH YR. TO DATE CUMULATIVE

11. HOURS IN REPORTING PERIOD:

744 5831 46320

12. NUMBER OF HOURS REACTOR WAS CRITICAL:

672.1 5174.2 41214.6

13. REACTOR RESERVE SHUTDOWN HOURS:

0.0 0.0 0.0

14. HOURS GENERATOR ON-LINE:

664.0 5134.8 40661.2

15. UNIT RESERVE SHUTDOWN HOURS:

0.0 0.0 0.0

16. GROSS THERMAL ENERGY GENERATED (MWH):

2341001 18047537 135127035

17. GROSS ELEC. ENERGY GENERATED (MWH):

794825 6177295 45859332

18. NET ELEC. ENERGY GENERATED (MWH):

757825 5891965 43639442

19. REACTOR SERVICE FACTOR 90.3 %

88.8 %

89.0 %

j

20. REACTOR AVAILABILITY FAC TOR 90.3 %

88.8 %.

89.0%

21 UNIT SERVICE FACTOR:

89.2 %

88.1 %

87.8 %

22. UNIT AVAILABILITY FACTOR:

89.2 %

88.1 %

87.8 %

23. UNIT CAPACITY FACTOR (USING MDC NET):

87.1 %

86.5 %

84.4 %

)

24. UNIT CAPACITY FACTOR (USING DER NET):

87.1 %

86.4 %

84.4 %

)

25. UNIT FORCED OUTAGE RATE:

10.8 %

'7.4%

2.3%

26. SHUTDOWNS SCHEDULED OVER THE NEXT 6 MONTHS (TYPE, DATE, AND DURATION OF EACH):

REFUELING, FEBRUARY 17,1995,31 DAYS

27. IF SHUTDOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP :

NA 1

l V2-2 i

UNIT 2 AVERAGE DAILY DOCKET NO. 50-425 POWER LEVEL DATE:

SEPTEMBER 1,1994

)

COMPLETED BY: G. L. HOOPER i

TELEPHONE:

(706) 826-4104 l

DAY Net MW

~i 1.

0 2..

0 3.

0 4.

406 5.

1136 6.

1156 j

7.

1159 1

8.

1165 9.

1165 10.

1161 11.

1159 12.

1156 13.

1155 14.

1156 15.

1160 l

16.

1155 17.

1155 j

18.

1159 19.

1160 20.

1155 21.

1156 22..

1162 23.

1162 24.

1165 25.

1166 26.

1166 27...

1163 28.

1159 29.

1154 i

l 30.

1154 i

31.

1153 I

i I

l V2-3

UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50-425 DATE:

SEPTEMBER 1,1994 UNIT NAME:

VEGP UNIT 2 COMPLETED BY: G. L. HOOPER TELEPHONE:

(706) 826-4104 REPORT MONTH AUGUST 1994 R

M S

E E

Y T

A T

LICENSEE SC Y

S H

EVENT TO COMPONENT CAUSE & CORRECTIVE P

DURATION O

O REPORT ED CODE ACTION TO NO.

DATE E

(HOURS)

N D

NUMBER ME (SUBCODE)

PREVENT RECURRENCE 94-6 7/23 F

80.0 8

4 2-92-05 AB V

SEE BELOW F: FORCED REASON:

~

METHOD:

EVENTS REPORTED INVOLV S: SCHEDULED A-EQUIPMENT FAILURE (EXPLAIN) 1 - MANUAL A GREATER THAN 20%

B-MAINTENANCE OR TEST 2 - MANUAL SCRAM REDUCTION IN AVERAGE C-REFUELING 3 - AUTO. SCRAM DAILY POWER LEVEL FOR D-REGULATORY RESTRICTION 4 - CONTINUATIONS THE PRECEDING 24 HOURS.

E-OPERATOR TRAINING & LICENSE 5 - LOAD REDUCTION F-ADMINISTRATIVE 9 - OTHER (EXPLAIN)

G-OPERATIONAL ERROR (EXPLAIN)

H-OTHER (EXPLAIN)

EVENT 94-6 CAUSE: CONTINUATION OF UNIT 2 CONTROLLED SHUTDOWN TO REPAlR LEAK ON THE RCS LOOP 3 INTERMEDIATE LEG DRAIN LINE ISOLATION VALVE.

CORRECTIVE ACTION: RHR PUMP REPAIRS WERE COMPLETED AND THE PLANT WAS RETURNED TO 100%

POWER.

V2-4

l

~

ENCLOSURE 3 VOGTLE ELECTRIC GENERATING PLANT-UNITS 1 AND 2 CHALLENGES TO PORV OR SAFETY VALVES s

DOCKET NOS. 50-424,50-425 DATE:

SEPTEMBER 1,1994 COMPLETED BY: G. L. HOOPER TELEPHONE:

(706) 826 4 104 EVENT DATE TAG NO.

TYPE DESCRIPTION NA NA NA NA L

c.