ML20072C535
| ML20072C535 | |
| Person / Time | |
|---|---|
| Site: | Monticello |
| Issue date: | 01/05/1983 |
| From: | Myrabo A NORTHERN STATES POWER CO. |
| To: | |
| Shared Package | |
| ML20072C521 | List: |
| References | |
| NUDOCS 8303080469 | |
| Download: ML20072C535 (4) | |
Text
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OPERATING DATA REPORT DOCKET NO.
50-263______
DATE 1-5_83____
COMPLETED BY A. L. Myrabo TELEPHONE 612/295-5151 OPERATING STATUS INotes
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________________________Monticello l
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- 1. Uni t Name :
- 2. Reporting period: ____'_______________ DECEMBER I
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- 3. Licensed Therma L Power (MWt): ______.._____1670 l
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- 4. Namep la te Ra t i ng (Gross NWe): _____________569 I
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- 5. Design Electrica l Ra t ing (Net MWe):
_____545.4 l
1
- 6. Maximum Dependab Le Capacity (Gross MWe): __553 l
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- 7. Maximum Dependable Capacity (Net MWe): ____525 l__________________________I
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
__N/A_____________________________________________
- 9. Power Level To Which Restricted, If Any (Net MWe):
___N/A___________________
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- 10. Reasons For Restrictions, If Any: __N/A_____________________________________
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_______________m________________________________________________________
This Month
'Yr._to-Date Cumulative
- 11. Hours I,h Repor t ing Period
_____744
__ _ _ _8 76 0'
____10084'9
- 12. Number Of Hours Reactor Was Critical
___288.6
___5697.8
__ 80633.4
- 13. Reactor Reserve Shutdown Hours
_____0.0
______0.0
_____940.7
- 14. Hours Generator On_Line
___213.9
___5545.5
__ 78755.2
- 15. Unit Reserve Shutdown Hours
_____0.0
______0.0
_______0.0
- 16. Gross Thermal Energy Generated (MWH)
_ 183058
_ 767789C
_127360240
- 17. Gross Electrical Energy Generated (MWH) __ 59522
__2550516
__40555893
- 18. Net Electrical Energy Generated (MWH)
__ 53988
__2420020
__38764039
- 19. Unit Service Factor
__ 28.8%
___ 63.3%
____ 78.1%
- 20. Unif Availab i li ty Factor
__ L8.8%
___ 63.3%
____ 78.1%
- 21. Uni t Capaci ty Factor (Using MDC Net)
__ 13.8%
___ 52.6%
____ 73.2%
- 22. Unit Capacity Factor'(Using DER Net)
__ 13.6%
___ 51.7%
____ 72.0%
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- 23. Unit Forced Outage Rate 0.0%
1.7%
5.8%
- 24. Shutdowns Scheduled Over Next 12 Months (Type, Date, and Duration of Each)
__0ctober 8, 1983 - Refueling Outage -
98 days _________________________
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____________________a_____-_____________________________________________
- 25. If Shut Down At End Of Report.Poriod, Estimated Date Of Startup:___ i-8-83_
- 26. Uni ts In Test Status (Prior to~ Commercia l Opera t ion): N/A Forecast Achieved l
l INITIAL CRITICALITY
~~~~~~~~ ~~~~~~~~
INITIAL ELECTRICITY COMMERCIAL OPERATION
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AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.
50-263______
UNIT MonticelLo__
DATE i-5-83____
COMPLETED BY A. L. Myrabo TELEPHONE 612/295-5151 e
i MONTH ______ DECEMBER _______
DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) -
(MWe-Net) 1
-3____________
17 4____________
2
-3___'_________
18
-5____________
3
-4____________
19
-5____________
4
-4____________
20
-5____________
5
-4_
21 3____________
6
-5____________
22 214____________
7
-4____________
23 368____________
8
-4____________
24 292____________
9
-5____________
25 302____ ______
iO
_5_________
n6 n55____________
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_6____________.
n.7 5_ __________
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_11________~____
n8
_4__
13 54____________
29
-4____________
14 257____________
30
-4____________
'f 1,5 288____________
31
-4_
16 295____________
INSTRUCTIONS On this format, List the average daily unit power level in MWe-Net'for each day in the reporting month.
Compute to the nearest whole megawatt.'
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NARRATIVE
SUMMARY
OF OPERATING EXPER ENCE DOCKET NO.
50-263____,_
DATE 1-5-83__,,-,
3 COMPLETED BY A. L. Myrabo TELEPHONE 612/295-5151
/
MONTH ______ DECEMBER _______
12-1-82 to Continuation of 1982 refueling outage.
12-8-82 12-9-82 Startup physics testing in progress.
12-10-82 Startup delayed waiting for NRC approvat.on recirc riser weld overlay repair.
12-11-82 Power operation.
Turbine overspeed test completed.
to Power Limited to 60% due to reactor feed pump 12-16-82 seal probtems..
12-17-82 Reactor shutdown for repair and adjustment of tur-to bine bearings.
12-20-82 12-21-82 Power operation.
Power limited to 60% due'to closure to of one high pressure feedwater black valve.
12-25-82 12-26-82 Reactor shutdown for repair and adjustment of tur-to bine bearings.
12-31-82 v'
Note: Power operation defined as essentially 100% of
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rated power except for weekend load drops for specified surveillance testing.
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DOCKETNO. 50-263 UNIT SilOTDOW S AND POWER REDUCTIONS UNITNAME micello DATE I-5-53 REPORT 510NTil December COMPLETED BY A. Mrrabo g
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TEt.EPHONE 612/295-515I E
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j Yj Licensee 5v, h
Cause A Correctise l
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Auion to j
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,j i j Repint =
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Prevens Recurrence.
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1 i
10 12-1-82 S
294.9 C
2 N/A ZZZZ ZZZZZZ Continuation of 1982 Rafteling outage 11 12-13-82 S.
1.2 B
4 N/A HA TURBIN Turbine overspeed test 12 12-17-82 S
112.2 B
2 N/A IIA
'IURBIN Turbine Bearing repair and alignment 13 12-26-82 S
121.6 B
2 N/A flA.
TURBIN Turbine bearing repair, and alignment 4
I 2
3 4
F: Forced Re'ason.
Method:
Exhibit C-Instructions L
5: SchedulcJ
\\ Equipment failureIExplaint -
I Manual foi Preparation oi Data B.Staintenance of Test 2-Manual Scram.
Entry Sheets for Licensee h
C Refueling 3 Automatic Scram.
Event Report (LERI File (NUREG-P D Regulator) Restriction 4-Other (Explain) 0161)
E Operstor Training & License Examination F AJministrati.e 5
G Operanional Es ror ([splaini Eshibit I;Same Source f
l'8/77)
II 0:her IEylaini
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