ML20071L266
| ML20071L266 | |
| Person / Time | |
|---|---|
| Site: | Hatch |
| Issue date: | 03/28/1983 |
| From: | Head G GEORGIA POWER CO. |
| To: | James O'Reilly NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| Shared Package | |
| ML20071L202 | List: |
| References | |
| NED-83-215, NUDOCS 8305270508 | |
| Download: ML20071L266 (2) | |
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>m U. S. Nuclear Regulatory Commission
REFERENCE:
Office of Inspection and Enforcement RII: HCD Region II - Suite 2900 50-366 l
101 Marietta Street, NW Inspection Report Atlanta, Georgia 30303 83-02 ATTENTION:
Mr. James P. O'Reilly GENTLEMEN:
Georgia Power Company (GPC) herein suomits the follo,ving information in response to 1&E Inspection Report 50-366/83-02 concerning the findings cf Mr. R. V. Crlenjak during tne period of Decemtier 20, 1982 to January 21, l
1983.
This report was ir, regard to the failure to submit a special report t
as required by Technical Specification 3.7.6.1.
One violation wcs identified and considered applicable to Plant Hatch Unit 2.
VIOLATION:
1 Technical Specification 3.7.6.1 requires tnat a spacial report shall be submitted by telephone within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> if more than one sater supply of 4
the fire suppression water system is inoperable.
Each water supply must have a minimum contained volume of 270,000 gallons.
Contrary to the above, on December 31, 1982, a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> telephone report l
was not submitted within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> when both water supplies to the File Suppression Water System were below the Technical Specification requirement of 270,000 gallons for each supply.
This is a repetitive occurrence (last previous occurrence on November 27, 1982).
This is a Severity Level V Violation (Supplement I).
i
RESPONSE
i Admission or denial of alleged violation: The violation occurred.
Reason for violation:
The event was caused by a Unit 1 equipment malfunction that resulted in the decrease of fire tank level for
[
Unit 2.
Operating personnel evaluated the results of this malfunction as related to Unit 1, but failed to make a proper evaluation of the event as related to Unit 2 requirements.
The failure to maintain tank level was caused by a 1A cooling tower deluge system trip, and the evaluation conducted was centered around the failure of the Unit 1 equipment.
It was not until reviews were conducted on January 3,1983 that the failure to take actions required by the Unit 2 Technical Specification was noted.
8305270508 830407 PDR ADOCK 05000321 j
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Georgia Power d U. S. Nuclear Regulatory Commission Office of Inspection and Enforcement Region II - Suite 3100 March 28, 1983 Page Two l
Corrective steps which have been taken and results achieved:
As noted l
in the Inspection Report, GPC reviews noted the failure to make the required telephone report for the December 31, 1982 event until January 3, 1983.
The findings of this review resulted in the delayed telephone report being submitted at 12:40 p.m. on January 3, 1983.
This telephone report was followed up with the required 14-day written report on January 11, 1983.
1 Corrective steps vnich will be taken to avoid further violations:
All l
SRO licensed personnel nave been instructed to complete an evaluation of i
actions to be teken for both units when an event occurs that affects shcred equipmen ;.
In
- eddition, Shift Supervisors and Operation Swervisors
- t. ave been irstructed to increase ccmunicatiuns between their positions for all abnomal or of f-nor.xd events.
These instructions have teen relaytd to eacu licensed 3R0 by an inteniecartmental memo.
D_ ate when full comoliance will be acnieved:
Full compliance was acnieved on January.sl,1963, when the recuired telephone nctification ard 14-day report follow-up weie ccmpleted.
If you nave any questiens, or require additional information, please contact this office.
i Very truly yours, h T.)bor G. F. Head WEB /mb xc:
L. T. Gucwa H. C. Nix, Jr.
Senior Resident Inspector l