ML20069Q268
| ML20069Q268 | |
| Person / Time | |
|---|---|
| Site: | Sequoyah |
| Issue date: | 06/20/1994 |
| From: | Powers K TENNESSEE VALLEY AUTHORITY |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| NUDOCS 9406270312 | |
| Download: ML20069Q268 (7) | |
Text
r Terywnsoe Va!*y Authonty. Pmt Of!ce Ekfe 2000, Sod %- Dwsy Teness* 37379 2J0 Ken Powers we Fwfoot, hvan N>r.wir rnant June 20, 1994 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C. 20555 Gentlemen:
In the Matter of
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Docket Nos. 50-327 Tennessee Valley Authority
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50-328 SEQUOYAH NUCLEAR PLANT (SQN) - INSPECTION REPORT NOS. 50-327, 328/94 REPLY TO NOTICE OF VIOLATIONS (NOVs) 50-327, 328/94-13-01 AND 94-13-02 Enclor,ure 1 contains TVA's response to Jon R. Johnson's letter to Oliver D. Kingsley dated May 23, 1994, which transmitted the subject NOVs. The first violation involves the failure to follow procedures (noncompliance with Technical Specification 6.8.1), resulting in the misconfiguration of three valves in the component cooling system. The second violation involves inadequate corrective action (a violation of 10 CFR 50, Appendix B, Criteria XVI) associated with the failure to perform preventive maintenance on electrical panels.
Commitments are listed in Enclosure 2.
If you have any questions concerning this submittal, please telephone C. H. Whittemore at (615) 843-7210.
Sincerel
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Ken Powers Enclosures cc: See page 2 I
9406270312 940620 DR ADOCK 05000327 PDR I
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i U.S. Nuclear Regulatory Commission Page 2 June 20, 1994 cc (Enclosures):
Mr. D. E. LaBarge, Project Manager U.S. Nuclear Regulatory Commission One White Flint, North 11555 Rockville Pike Rockville, Maryland 20852-2739 NRC Resident Inspector Sequoyah Nuclear Plant 2600 Igou Ferry Road Soddy-Daisy, Tennessee 37379-3624 Regional Administrator U.S. Nuclear Regulatory Conunission Region II 101 Marietta Street NW, Suite 2900 Atlanta, Georgia 30323-2711
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ENCLOSURE 1 RESPONSE TO NRC INSPECTION REPORT.
NOS. 50-327, 328/94-13 JON R. JOHNSON'S LETTER TO OLIVER D. KINGSLEY DATED MAY 23, 1994
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Violation 50-327. 328194-13-01
" Technical Specification Section 6.8.1 requires, in part, that procedures shall be established, implemented, and maintained covering the activities reconnended in Appendix A of Regulatory Guide 1.33, Revision 2, February 1978. Appendix A of Regulatory Guide 1.33 includes operations procedures to maintain required configuration control for safety-related components and systems.
" Procedure 1-SI-OPS-070-032.A. COMPONENT COOLING WATER VALVES POSITION VERIFICATION TRAIN A Revision 5, specifies the required throttle position for Component Cooling Water System (CCS) Valve 1-VLV-70-702 as j
being 20.25 turns f rom the open position.
" Procedure 1-S0-70-1, COMPONENT COOLING WATER SYSTEM "A" TRAIN, HP Revision 5, specifies the required position for CCS Valve 1-VLV-70-705 as being open.
" Attachment 6 of procedure 0-S0-70-1.06, CCS "A" TRAIN VALVE CHECKLIST 0-70-1.06, Revision 3, specifies the required position for CCS Valve HCV-0-70-532 as being open.
" Contrary to the above, the licensee failed to follow the above procedures such that, between the period of April 9 and 11,1994, CCS Valves 1-VLV-70-702,1-VLV-70-705, and HCV-0-70-532 were found out of their required positions.
"This is a Severity Level IV violation (Supplement I)."
Reason _for_the_Vlolation The reason for this violation is personnel error.
The root cause for the personnel error is indeterminate.
The personnel responsible for positioning the 1-VLV-70-702 and 1-VLV-70-705 valves had been trained, qualified, and experienced and were confident that the valves had been left in their proper position.
In addition, personnel used the concurrent verification process during the positioning of the throttle valve. Mechanical problems, e.g., sludge build-up, inoperable valve position indicators, etc., were investigated and found not to be a factor in the mispositioning of the valves.
Therefore, it can be concluded that the cause for these valves being out of position was personnel error.
The HCV-0-70-532 valve is a vent valve and is manipulated during chemical additions and venting and filling operations by the Operations group. The manipulation is always controlled by approved procedures, and the position is always required to be verified. Therefore, it can be concluded that the cause for this valve being mispositioned was personnel error.
i CorIncliYR_Slepa_luaLilaye Been Taken_and_the_Resulla Achieved In the initial walkdown of the CCS, a valve (1-VLV-70-705) in series with the throttle valve was repositioned to its correct configuration after it was discovered slightly loss than full open, i.e., not significantly out of position.
Immediate corrective action upon discovery of the mispositioned throttle valve (1-VLV-70-702) was to correctly position the valve and then to verify the position of other throttle valves in the CCS and ERCW systems (no other throttle valves were found out of position). A problem evaluation report (PER) was initiated to document the issue and
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investigate the problem of the two valves that were found to be out of configuration.
Later, a third valve (a vent valve) was also found to be out of its correct configuratica. This vent valve was correctly repositioned. Another PER was initiated to document the issue, investigate the problem, and formulate the corrective action.
A training letter describing this event and management's expectations concerning correctly positioning valves, especially throttle valves, has been issued to Operations personnel.
The appropriate personnel actions have been developed and implemented for each individual associated with this event.
CorIcclire_Slega_IhatJLill_he_.TakeJi to Avoid Future ViD.lations No additional corrective action is warranted.
Da t e_When_fu1LC omplianceEll_b e_Ac hieved TVA SQN is in full compliance with respect to the violation (failing to follow procedure) and mispositioning valves in the component cooling system. The corrective actions described above will serve to prevent recurrence.
ViolationJ0-32L_32ti/94-13-02 "10 CFR Part 50, Appendix 3, Criterion XVI, Corrective Action, requires, in part, that measures be established to assure that conditions adverse to quality such as failures, malfunctions, and nonconformances, are promptly identified and corrected.
In the case of significant conditions adverse to quality, the measures shall ensure that the cause of the condition is determined and corrective action taken to preclude repetition.
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" Contrary to the above, corrective action for Condition Adverse To Quality Report (CAQR) SQP890626, which on November 22, 1989, identified dust and dirt within relays located inside relay cabinets 1-R-70 through 1-R-79 and 2-R-70 through 2-R-79, was inadequate. The CAQR stated that dust and dirt on and in the relays could be detrimental to relay operation and was identified as a condition adverse to quality.
The root cause was identified as a lack of preventive maintenance for cleaning equipment within the auxiliary instrument room relay cabinets.
Corrective action consisted of developing an annual Preventive Maintenance Instruction to clean equipment in the relay cabinets periodically.
However, as of April 11, 1994 relays within cabinets 1-R-70 through 1-R-79 had not been cleaned. Dirt and debris were identified on and inside relays located within relay cabinets 1-R-48, 1-R-51, 1-R-55, 1-R-58, 1-R-70, 1-R-71, 1-R-72, and 1-R-73.
"This is a Severity Level IV violation (Supplement I)."
Reannn_far_the violation The reason for the violation was the lack of good housekeeping practices during the performance of work inside relay panels in that tape, screws, 1
and other debris were not removed after the completion of activities.
The NRC inspection report cited SQN with a violation of 10 CFR 50, Appendix B, Criteria XVI for inadequate corrective action.
The NRC report references the failure to complete the corrective actions associated with a 1989 corrective action document. The corrective action document was written primarily as a result of a cable-pulling lubricant that was found in several relay racks. The document also noted that the relays had dust and dirt accumulation in the racks. The corrective action to the dust and dirt problem '+as to initiate preventive maintenance (PM) instructions to periodically clean the dust and dirt from the relays.
C' scope of the PMs was limited to only 10 panels containing both open-e closed-type m
relays on each unit. However, because of a scheduling err.
the PMs were never performed. Since the PMs were written primarily for che prevention of the build-up of dust and dirt on panel faces and not for the inspection of individual relays or relay contacts, the performance of the PMs would not necessarily have identified and removed any debris on the relay contacts.
Therefore, it can be concluded that the performance of these PMs would not have prevented this event.
Corrective Steps That llave Been Taken and the Results Achieved The immediate corrective action was to remove the debris inside the relay panel and determine the extent of the problem.
An inspection for dust, dirt, and debris in and around Unit I relay panels was conducted. The inspection was subsequently followed by a cleaning and vacuuming of relay panels.
In addition, a training letter describing this event and management's expectations concerning housekeeping during work activities has been issued.
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Nrr enthe_Slepa_Tha LWil1Jte.laken_Lo_Ayoid_Eutt her_Violn11ona Modifications and Maintenance management directives will be revised to increase the sensitivity and identify the potentially adverse effect of debris in open electrical equipment.
The directives will also clearly define housekeeping monitoring efforts.
PM procedures providing instructions for performing the inspection and subsequent cleaning of relays will be developed and then scheduled with a definite periodicity. Unit 2 relays will be inspected and cleaned during the Unit 2 Cycle 6 refueling outage.
Dale.When_Eull_ Compliance _Will_he_AchiAYed SQN will be in full compliance when the relays are inspected and cleaned during the Unit 2 Cycle 6 refueling outage.
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9 ENCLOSURE 2 Commitments Einlation 50-32L_32B/94-13-02 1.
Maintenance management directives will be revised to increase the sensitivity and identify the potentially adverse effect of debris in open electrical equipment. The directives will also clearly define housekeeping monitoring efforts. This will be accomplished by August 5, 1994.
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Modifications' management directives will be revised to increase the sensitivity and identify the potentially adverse effect of debris in open electrical equipment. The directives will also clearly define housekeeping monitoring efforts. This will be accompliehed by August 5, 1994.
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Preventive maintenance procedures providing instructions for performing the inspection and subsequent cleaning of relays will be developed and then scheduled with a definite periodicity. This will be accomplished by August 5, 1994.
4.
Unit 2 relays will be inspected and cleaned during the Unit 2 Cycle 6 refueling outage.
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