ML20069L665

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Monthly Operating Rept for May 1994 for Re Ginna Nuclear Station Power Plant
ML20069L665
Person / Time
Site: Ginna 
Issue date: 05/31/1994
From: Ploof R
ROCHESTER GAS & ELECTRIC CORP.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9406200143
Download: ML20069L665 (5)


Text

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.o o-r ff ROCHES TER GA S AND ELEC TRIC CORPORA TION e 80 EA ST A VENUE, ROCHESTER, N. Y.

14649-0001 j'['

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6 2700 c.... s... -..

l GINNA STATION June 8, 1994 i

l US Nuclear Regulatory Commission Document Control Desk Washington, DC 20555

Subject:

Monthly Report for May, 1994 Operating Status Information R.

E. Ginna Nuclear Power Plant Docket No. 50-244

Dear Sir:

Pursuant to our Technical Specification 6.9.1, attached herewith is the monthly operating status report for Ginna Station for the month of May, 1994.

Very truly yours, e > ( [b

~ os h A. Wida &

Plant Manager JAW:tjn At t acilmen t s c:

Mr. Thomas T. Martin NRC (1)

/

f 9406200143 940600 Il PDR ADOCK 05000244 l

R PDR

i OPERATING DATA REPORT

+

DOCKET NO. 50-244 DATE: June 8,1994 COMPLETED BY:

Ronald D. Plo'ef TELEPHON (315) 524 4446 Ext.67 OPERATING STATUS 1, Unit N R.E._GINN A NUCL EAR _P_OWER PLAN _T Notos:

2 Reporting Penod May. t ', ? 4 i

3.

Licensed Therrnal Power (MWt):

1520 4.

Nameplate Rating (Gross MWe):

490 5.

Design Electnc Rating (Net MWe):

470 6.

Maximurn Dependable Capacity (Gro 490 7.

Maomum Dependable Capacity (Net 470 8 If Changes Occur m Capacity Rating (Items Number 3 Through 7) Sence Last Report, Give Reason:

9 Power Level to Which Restncted. If Any (Net MWet 10 Reason F or Restnctions, if Any:

.u-

.,w.

.---,----,.-_.4----

This Month Yr. to-Date Cumulative ' *

11. Hours in Reported Penod 744 O_

3623.0

_ __ 21_4871.0,

12. Number of hours Reactor Was Cntical 708.8 2509.3 171035.8
13. Reactor Reserve Shutdown Hours 0.0 0.O_

1688.0 '

14 Hours Generatur On line

_ 704.0 246,0 4

_16820(4_

l'i. Unst Reservo Shutdown Hours 0.0 0,0 8.5 '

16. Gross Thermal Energy Generated (MWH) 1019528 3506319 238462332
17. Gross Liectncal Energy Generated (MWH) 346654 1191305 78874664
18. Net Electncal Energy Gene <ated (MWH) 329590

_1131127

._74866500 19 Unit Service Factor (%)

94.6 67.6 78.3

20. Unit Availabihty Factor (%)

94.6 67.6_

_ _ _ 7 8. 3_

21. Unit Capacity Factor tusing MDC Net) (%)

94.3 66.4

, _7 5. 3_

22. Unit Capacity f actor tusmg DER Net) (%)

94 3 66.4

. _7 5. 3__

23 Unit Forced Outage Rato (%)

54 33 5.6

24. Shutdowns Scheduled Over Next 6 Months (Type, Date and Duration of Each):

<.-.%w-.-

25 If Shutdown At End of Report Penod, Estimate Date of Startup.

26 Urnts in Test Status (Pnor to Commercial Operation):

Forcast A chieved INiilAL CRITICAllTY INITIAL ELECTRICITY COMMERCIAL OPERATION

  • CUMULATIVE TOTAL COMMENCING JANUARY 1.1975
  • CUMut.ATIVE TOTAL COMMENCING NOVEMBER 8,1969

AVERAGE DAILY UNIT POWER LEVEL DOCKET NO: 50-244 UNIT: R.E Ginna Nuclear Power Plant DATE: June 8,

1994 COMPLETED BY:

Ronald Ploof TELEhlONE: (315) 524-4446 Ext. 673 MON 1'} l May, 1994 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)

(MWe-Net) 1.

480 17.

480 2.

480 18.

480 3.

411 19.

480 4.

-8,5 20.

480 S.

38.5 21.

480 6.

322.5 22, 480 7.

481 23.

480 8.

480 24.

480 9.

480 25.

480 10.

480 26.

480 11, 480 27.

480 12, 480 28, 480 13.

480 29.

479 14.

480 30, 480 15.

480 31.

479 l

16, 480 INSTRUL*rIONS On this format, list the average daily unit power level in MWe-Net for each day in reporting month.

Compute to the nearest whole megawatt.

50-244 IMX KET NO.

IWIT NA MI: R.E. GINNA NUCLEAR POWER PLANT DATE 3"""

8+

1994 1

UNIT SHUTDOWN AND POWER REDUCTIONS

( OMPLE'll{D itY a

REPORT MONTII May i Etyptiosp ( ll 5 ) 524-4 4 4 6_ ext m 673 m

_5 e

a Cause & Corrective Licensee e,

e

  • e v

oO e

[j No.

Date

{

jg

}jj Event Action to H

dE y

e di e Report #

Aj 7, u Prevent Recurrence U

f 4

Q 94-06 5/3/94 F

40 A

1 Flexable CCW cooling line to RCP developed leak as a result i

of inproper installation.

-l 1

4 4

I I

3 4

F: Forced R eason:

Metho&

Exhibit G - !nstructions i

S: Scheduled A-Equipment Failure (Explain) 1 -Ma nual for Preparmeron of Data B-Maintenance or Test 2-Manual Scram.

I nery Sheets for 1.icensee C-Refueling 3-A utomatic Scram.

E vent Report (1.ER) I ile (NifR EG-j D-Regulatory Restriction 4-Other (I uplain) 0161)

E-Operator Training & License Examination F-Adminis tra tiv e 5

G-Operational Error (Explain) nev aos em II-Other (Explain)

Exhibit I - Same Sourc e s

9

. NARRATIVE

SUMMARY

OF OPHitATING EXPERIENCE DOCKET NO: 50-244 UNIT: R.E. GillDa Nuclear Power Plaul DATE: J1tne 8,_,1994 COMPLETED BY:

Ronald Ploof TELEPl!ONE: (315) 524-44_46 Ext. 673 MONTII jiay_,_,J 9 9 4 During the month of May the average power level was 97% on May 3 to I.razzil ice buildup on intake acreens and heaters.

Returned to full power on January 21 and remained there at the end of report period.

The unit was tap.en off line to repair a leak in the CCW cooling 3ine to the "A"

RCP.

The unit was returned to full power on May 6.

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