ML20069F514

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Responds to NRC Re Violations Noted in Insp Rept 50-298/94-03.Corrective Actions:Valves Were Verified Closed & Tagged Closed.Pcn Was Also Initiated to Add PC-V-506 & PC-V-507 to Procedure 2.2.60A
ML20069F514
Person / Time
Site: Cooper Entergy icon.png
Issue date: 05/31/1994
From: Horn G
NEBRASKA PUBLIC POWER DISTRICT
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
CNSS941202, NUDOCS 9406080337
Download: ML20069F514 (3)


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Nebraska Public Power District TMW" CNSS941202 May 31,1994 U. S. Nuclear Regulatory Commission l

Attention: Document Control Desk Washington, DC 20555 j

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Subject:

Reply to a Notice of Violation, Inspection Report 50-298/94-03, Cooper Nuclear Station, NRC Docket 50-298, DPR-46

Reference:

Letter from A. B. Beach (NRC) to G. R. Horn (NPPD) dated April 29, 1994, "NRC Insoection Report 50-298/94-03 (Notice of Violation)"

Gentlemen:

The following discussion provides the Nebraska Public Power District's reply to a notice of violation issued with NRC Inspection Report 94-03 (Reference). The inspection was conducted at Cooper Nuclear Station (CNS) during the period of January 2 through February 12, 1994.

Statement of Violation 10 CFR Part 50, Appendix B, Criterion V, " Instructions, Procedures, and Drawings," states, in part, " Activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings.

Contrary to the above, new manually operated primary containment isolation valves, PC-V-506 and -507 were installed during the last refueling outage (March 1993 - July 1993), but the normal position of the manual primary containment isolation valves, an activity affecting quality, was not prescribed by any procedure.

This is a Severity Levei IV violation (Supplement I).

Reason for Violation

- Design Change (DC)90-036 installed two 3/4" instrument taps off the torus drainline during the 1993 Refueling Outage. Each tap has a manual isolation valve (PC-V-506 or PC-V-507) and is now capped until the balance of the design is installed. Since the portion of the torus drainline where the taps were installed is an extension of the Primary Containment, the valves are considered Primary Containment isolation valves.

However, no procedure changes were submitted per DC 90-036 to include the valves in a valve checklist procedure. Therefore, the normal position of the valves, an activity affecting quality, was not prescribed by any procedure.

9406080337 940531

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j Document ' Control Desk May 31,1994 Page 2 This non-conformance is documented by NCR 94-019.

This event is attributed to human error on the part of the District design engineer since his review of the design change did not identify the omission of the procedure change. This error may be partially due to the lack of specinc guidance in *e design change procedures conceming l,

the procedure change requirements for new valves, and the fact that the lines were to be capped downstrearn of these valves.

A secondary issue associated with this violation involves the lack of specinc guidance in the design change review process to review the document change section of the design change.

Specine guidance to the appropriate reviewers could possibly have prevented this situation.

Corrective Stens Taken and The Results Achieved immediately upon discovery of the non-conformance, the valves were verified closed and then tagged closed. The valves are located below the torus water line and there were no visible signs ofleakage. The design engineer was informed of the non-conformance and made aware of the need to include any new valves into the appropriate valve checklist procedure. A Procedure Change Notice (PCN) was initiated to add PC-V-506 and PC-V-507 to Procedure 2.2.60A.

Temporary Procedure Change Notice (TPCN)94-033 was also issued to implement these changes for the interim until the PCN is irapemented.

Corrective Steos Which Will Be Taken To Avoid Further Violations This violation will be discussed with personnel who prepare design changes to impress upon them the importance of updating all documents which control activities important to safety that

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are affected by a design change, the nature of the program changes to be performed, and the importance of accountability during the performance of work. Engineering procedures will be' revised to include an item in the appropriate checklist to require all new valves to be included in a system valve checklist procedure. In additica, review requirements will be evaluated and more clearly denned to further enhance our existing design change program. These revisions are expected to improve the preparation and subsequent review of future design changes such that future violations of this nature are unlikely.

l Date When Full Compliance Will Be Achieved 1

l Full compliance will be achieved by August 31,1994.

l Additional item for Discussion In addition to the above violation, the NRC inspection identified an Unresolved Item (298/9403-01) concerning the use of a single, unlocked, manual valve for a containment isolation t

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j Docyment Control Desk May 31,1994 Page 3 function. The District wishes to advise it is presently reconstituting the design basis for the Primary Containment system and will evaluate this issue within that task. Likewise, the CNS Plant Engineering Department is pursuing efforts to resolve NRC concerns involving the identification and control of manual primary containment isolation valves. The District plans to complete these efforts by August 1994 Should you have any questions regarding this matter, please contact me.

Sincerely, W

(

t. Horn Vice ' resident - Nuclear cc:

NRC Regional Administrator Region IV Arlington, Texas NRC Resident Inspector Office Cooper Nucl car Station

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