ML20066J272
| ML20066J272 | |
| Person / Time | |
|---|---|
| Site: | North Anna |
| Issue date: | 02/21/1991 |
| From: | Marshall B VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.) |
| To: | Kregloe W VIRGINIA, COMMONWEALTH OF |
| References | |
| NUDOCS 9102260042 | |
| Download: ML20066J272 (2) | |
Text
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Return Receiot Recuestdd vinor m s'o m n February 21, 1991 Mr. William L. Kregloe Virginia Water Control Board.
f Valley Regional Office 5
116 North Main. Street P.O.
Box 268-Bridgewater, VA 22812 RE:
UNUBUAL DISCHARGE - NORTH ANNA POWER STATION
Dear Mr. Kregloe:
On February 17, 1991 at 3:50 p.m. the Virginia Office of Emergency Services was notified of an unusual discharge at our '. North ? Anna Power Station. - The Water Board prep officer called G...R. Knauer of my staff later Sunday afternoon to verify the: report. This letter-confirms our notification and provides additional 'information regarding the incident.
Around 4 a.m. on Sunday, February-17, station personnel discovered that the product level in a chemical storage tank was.significantly reduced. The. level indication system had failedt allowing for siphoning of the stored water treatment chemical to a turbine building sump. This sump discharges through Outfall 004-into the discharge canal. The water treatment chemical'is a Calgon product PCL-713, which is a combination of organic and inorganic phosphates along with a dispersant for silt and other inorganic deposits. This product is used for corrosion control in the bearing cooling:
system. Approximately 300 gallons of product'were discharged, as.
determined by comparison of the residual product to the immediately l
previous level reading.
There was no apparent adverse impact on aquatic life or the natural environment as a result of this discharge. Visual inspection of the discharge canal was conducted but no-analytical data were-l'-
collected.
After evaluation of the incident, station personnel. have concluded that a future incident can be avoided by valving out the level indicator tube when it is not in use. This change in operating procedures is being implemented.
9102260042 910221]
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DR ADOCK O
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i Mr. William.L. Kregloel February 21, 1991
'I Page 2-
~ If you have any questions regarding-' this / incident, please. call-Ms'.
Gleness Knauer of my staff.atl 273-2996..
Sincerely,-
i f
B..M. Marshall, P.
Manager-Water Quality-t cc:
U.S. NRC-Docket lo.- 50-338/50-339-
-101'Marietta-St., NW
~
x Suite-2900 Atlanta,.GA-30323 U-S;"NRC2
. ATTN:i-Docket 4 Control; Desk!.
Docket No.c 50-338/50-339 Washington,aD.C.:205554: ' "
NRC. Senior Resident. Inspector
- Docket No. 50-338/50-339
- )
- North Anna' Power Station
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