ML20066J272

From kanterella
Jump to navigation Jump to search
NPDES Noncompliance Notification:On 910217.product Level in Chemical Storage Tank Significantly Reduced Due to Failure of Level Indication Sys Which Allowed Siphoning of Stored Water Treatment Chemical to Discharge
ML20066J272
Person / Time
Site: North Anna  Dominion icon.png
Issue date: 02/21/1991
From: Marshall B
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To: Kregloe W
VIRGINIA, COMMONWEALTH OF
References
NUDOCS 9102260042
Download: ML20066J272 (2)


Text

-

VMQ) (Mortlostr>>t ikIItknini

~ Giert A!iert. t kmilliti.!9XJJ j'

Certified Mail s

Return Receiot Recuestdd vinor m s'o m n February 21, 1991 Mr. William L. Kregloe Virginia Water Control Board.

f Valley Regional Office 5

116 North Main. Street P.O.

Box 268-Bridgewater, VA 22812 RE:

UNUBUAL DISCHARGE - NORTH ANNA POWER STATION

Dear Mr. Kregloe:

On February 17, 1991 at 3:50 p.m. the Virginia Office of Emergency Services was notified of an unusual discharge at our '. North ? Anna Power Station. - The Water Board prep officer called G...R. Knauer of my staff later Sunday afternoon to verify the: report. This letter-confirms our notification and provides additional 'information regarding the incident.

Around 4 a.m. on Sunday, February-17, station personnel discovered that the product level in a chemical storage tank was.significantly reduced. The. level indication system had failedt allowing for siphoning of the stored water treatment chemical to a turbine building sump. This sump discharges through Outfall 004-into the discharge canal. The water treatment chemical'is a Calgon product PCL-713, which is a combination of organic and inorganic phosphates along with a dispersant for silt and other inorganic deposits. This product is used for corrosion control in the bearing cooling:

system. Approximately 300 gallons of product'were discharged, as.

determined by comparison of the residual product to the immediately l

previous level reading.

There was no apparent adverse impact on aquatic life or the natural environment as a result of this discharge. Visual inspection of the discharge canal was conducted but no-analytical data were-l'-

collected.

After evaluation of the incident, station personnel. have concluded that a future incident can be avoided by valving out the level indicator tube when it is not in use. This change in operating procedures is being implemented.

9102260042 910221]

3 B,;

DR ADOCK O

7 b

n, -

i Mr. William.L. Kregloel February 21, 1991

'I Page 2-

~ If you have any questions regarding-' this / incident, please. call-Ms'.

Gleness Knauer of my staff.atl 273-2996..

Sincerely,-

i f

B..M. Marshall, P.

Manager-Water Quality-t cc:

U.S. NRC-Docket lo.- 50-338/50-339-

-101'Marietta-St., NW

~

x Suite-2900 Atlanta,.GA-30323 U-S;"NRC2

. ATTN:i-Docket 4 Control; Desk!.

Docket No.c 50-338/50-339 Washington,aD.C.:205554: ' "

NRC. Senior Resident. Inspector

- Docket No. 50-338/50-339

)

- North Anna' Power Station

=3 4

-i I

-j l

4 r

'I

.:j i

s

,r e

r e%--m e

-w

=,.n

.c

,enm--%

w,w w

w ;,, -.-... -. -

w e ew...wwss---e.

w 4,

1 e r a, esp w' v v9 g 4 4p v-