ML20066E451
| ML20066E451 | |
| Person / Time | |
|---|---|
| Site: | Cook |
| Issue date: | 04/02/1981 |
| From: | Gillett W INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG |
| To: | |
| Shared Package | |
| ML20066E450 | List: |
| References | |
| NUDOCS 8211150194 | |
| Download: ML20066E451 (5) | |
Text
'.
,., CPERAT*NC. DATA RI?OR-S'0'-315 DCC:GT NO.
DATI d-2-81 ri11ett CO.st?LETID Iy W T-e T' "SCNE 616-4F0 9901 c??zATING 5 ATUs Donald C. Cook 1
Not:5 g, eg. y,c,.
Ma rch 1981
. Repor:iag ?erod:
3250
- 3. LI=: sed Ther=:1 ?cwe p:W:):
1089
- 4. N=ep! :: R::in;(Crou atW ):
1054
- 3. Desi;= Ee::d=1 R::in;(Ne:51We):
1080
- 6. 51:-!=u= De; read:ble Capd:f (Gess SIW-):
104a T.
- f 221===s De;-- d '!: C p:=f:/ (Net $1We):
- 3. 'IO.:=;es Oc=ria C:pci:y R 6;s (1:e::s Nc::dar 3 Th:ot;i 7) Sise: L s Repc::. Give R::sor.s:
- f. Fewe L:ve! To Whi:h Rw= iced. If Any (Ne:.\\iwe):
- 10. E=:sens For R=::-:do==.If Asy f
This.\\f onth Y:.-<o-Oats Cer -ive 74a 2.160 5.1. 7 AR
- 11. Hov. != R:;or:i=g ? :fod 7dd 2.03d.1 41.555.I
- '. Nc
- her Cf Foe:s Re:::orwzs C."-r 0
0 463 1.i. Re:cer R:se. e sh:::iown Hou:s 744 2,024.4 40,581.5
- 14. Houn Ce==.::: On.U:=
0 0
321
- 15. U. i: R.se:se Sh tdown Ec:.s 2.411.013 6,481,716 115,708,722
- 16. Cass The==:I I e:gv Cene=:ed otWM)
- 17. Cars re=i=f Ise.h Ceme:::ed GIWH1 806,230 _
2,165,730 38,021,390 778.715 2,091,210 36,550,351
- 13. Ne: II =-;=1I:=;y Ce.e=:ed 0 Wca-100 93.7 77.2
- 19. Uni: Se.wie F::: r
%5 10 M 93.7 77.2
- 23. U:!: Aimil:iziII:y 7:::or
/ / 496.5 /
91.4 68.7 I. Uni: C:pcity 7:::=r (Usic;.'.!DC Ne:)
/
( 95. L/
90.4 64.7 2'-. Uni: Caescity F:::ce(Using CEF. Net)
NI 0.9 6.6
- 23. Uni: For:=d 0::::ge R:te
- 04. Shutdowns Scheduled Ove Nex: 5 Sloaths (, Type. D::.: d Cu-::!on of I:cht:
Refueling Outage 5-25-81 60 days I
Epd Of Re-c : ?triod. Isti== ed D:re ef 5 I
. p:
".3. If Shu: Dowr: A:
Tore.=::
Achieved
. 25. Units la Tes: 5::::.s IP.or ta C:==e-:!:1 Ope-:: font:
INIT'.AL C?.!T CALITY
~
~
INITIA L I*.ICTR:C;W
.m.3 ; =.. -. m. *.
C O... ;p r....
....a e a v
.s. e gA3 MW M 8211150194 81041o ~ ^~
N'3' ggf I *... '
gDRADOCK05000 1
o AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.
50 '315 UNIT 1
OATE a-2-81 CCMPLETED BY W. T. Gillett TELEPHONE 616-465-5901 MONTH M;rch 1o31 OAV AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWE-Net)
(MWe-Net) 1-1049 17 1051 2
1049 18 10a9 3
1049 19 1050 4
1049 20 1044 5
1049 21 1042 6
1047 22 1050 7
1032 23 1049 8
1051 24 1050 9
1052 25 104o 10 1052 26 Inen 11 In02 27 ingi 12 104g 28 insn
~
13 1051 29 1046 14 1034 30 105?
15 1047 31 1052 16 1048 INSTRUCTIONS On this famat list the average daily unit pcwer level in MWe-Net for each cay in the reporting month. Compute to the neares wnole megawatt.
l
UNITSiluTDOWNS ANI)POWElt REDUCTIONS DOCKET NO. 50-315 UNIT N AhlE D.C. Cook - Unit 1 DATE 4-9-81 March, 1981 COhlPLETEp ilY B.A. Svensson ItEl'OltT alONTil TELEPIIONE (616) 465-5901 4
=
c k
.$ E 3
-. Y5 Licensee
,E, n,,
{1, Cause & Conective No.
D tie g
5g 5
.c s E Event
[?
o8 Attiim in 6-
$E j ;f, g itepor: #
in u o
Prevent itecurrence 6
None There were no unit shutdowns or sig-nificant power reductions during the month. The unit operated at a capac-ity factor of 96.5%-(using MDC net).
I 3
4 12: lim eetl Itcason:
Melluid:
Exhible G Instructions S: Solictinleil A.E Inipment I ailuie (lixplain)
I-Manual for Preparation of Data II.hlaintenance of Test 2 Manual Scram.
Entsy Shecis fin I.icensee C Refueling l 3-Automatic Scram.
I! vent Repen t II.l!R) l7ile INutti.~G-D.Itegulatosy itestriction 4 Othes (Explain) 0161)
E Opesains Isaining& Licenw lix.iminatinn F Ailminisseative 5
G Operational Eno IExplain) lixhibit I - Same Somie (9/77)
Il Olher (Explaini i
d Docket No.:
50-315 Unit Name:
D. C. Cook Unit #1 Completed By:
D. R. Campbell Telephone:
(616) 465-59.01 Date: April 9, 1981 Page:
1 of 1 UNIT 1 MONTHLY OPERATING ACTIVITIES - MARCH, 1981 (Operating Statistics and Shutdown Experiences)
Highlights:
For the month of March,1981 the unit operated at 100% power except for a short period (average s3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />) each week, power was reduced to between 90 and 95% to test Turbine Control Valves.
Total electrical generation for March was 806,230 mw.
e 0
e 6
r DOCKET NO.
50 - 315 UNIT NAME D. C. Cook - Unit No. 1 DATE 4-10-81 COMPLETED BY B. A. Svensson TELEPHONE T616)465-5901 PAGE
[1 of 1 MAJOR SAFETY-RELATED MAINTENANCE MARCH, 1981 M-1 Gasket leaks were detected on the reciprocating charging pump from a flange in the discharge line.
Replaced the outboard flexitalic gas-ket on No. 1 cylinder of the pump.
Also replaced the gasket on the discharge line of the pump upstream of the pulsation dampener.
The pump tested satisfactorily.
M-2 The air operated cross-tie valve for the Unit 1 and Unit 2 condensate storage tanks, CRV-51, had a blown operator diaphragm.
Replaced the diaphragm and had the valve tested.
M-3 The turbine driven auxiliary feedpump trip and throttle valve was leaking by.
Disassembled valve and found the pilot valve, the stem and the main valve steam cut.
Lapped the seat, replaced the disc and stem, reassembled the valve and had it tested.
M-4 The power cable to motor operated valve, IM0-910, (suction from the refueling water storage tank to the charging pumps) indicated a ground.
The failed portion was removed and reterminated.
The valve was tested following repairs.
~
C&I-l IRV-300, residual heat removal system to CVCS controller indicated 20%
open and the setpoint dial would not turn. The setpoint potentiometer was found loose. The dial was adjusted and the potentiometer was tightened.
l C&I-2 The 50-foot wind direction recorder indication became erratic. The recorder's amplifiers contacts were cleaned and the gain of the am-plifier was decreased to reduce the oscillations. The amplifiar was calibrated and a visual check of the primary and secondary transmit-ters revealed the vanes were, in fact, changing directions rapidly.
C&I-3 SG-18, containment air temperature recorder on the CAS panel failed.
The range module of the ' recorder failed.
The range module was re-placed and the recorder calibration was performed.
l C&I-4 Loop 2, T percent power panel indication was approximately 6% low.
l The normal hot leg RTD was found drifting and not maintaining the
~
l correct value.
The spare hot leg RTD was placed into service and l
R/E module 1TY-421A was recalibrated to the spare RTD resistance l
values.
The failed RTD will be replaced during the next refueling l
- outage, i
_