ML20063J160
| ML20063J160 | |
| Person / Time | |
|---|---|
| Site: | Cook |
| Issue date: | 08/24/1982 |
| From: | Murphy C INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG |
| To: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
| Shared Package | |
| ML20063J123 | List: |
| References | |
| 82-066-03L, 82-66-3L, NUDOCS 8209020311 | |
| Download: ML20063J160 (2) | |
Text
fdRC FORM 3GG U. S. NUCLEAR REGULATORY COMMISSION
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60 61 DOCKET NUMBER 68 b3 EVENT DATE i4 IS REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h lo121lDURING A PLANNED UNIT SHUTDOWN WITH THE REACTOR IN MODE 2 THE AVERAGE REACTOR I
0 IoIa11 COOLANT TEMPERATURE DECREASED BELOW 541 FOR A PERIOD OF SEVEN (7) MINUTES.
THE I
U I o 14 i l MINIMUM TEMPERATURE OF THE TRANSIENT WAS 539 F.
REC 0VERY FROM THE TRANSIENT WAS I
i Io lsl I WITHIN THE FIFTEEN (15) MINUTES ALLOWED BY THE ACTION STATEMENT IN TECHNICAL SPEC-l
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THIS EVENT HAD NO EFFECT ON THE HEALTH AND SAFETY OF THE PUBLIC.
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3J J4 35 36 Ji 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h IiioiI DURING UNIT C00LDOWN THE STEAM DUMP VALVES ERR 0NEOUSLY CAME OPEN CAUSING A I
U IiIi11 C00LD0WN BELOW 541 F WHILE THE REACTOR WAS STILL CRITICAL.
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ii i,i l QUICKLY CLOSED THE STEAM DUMP VALVES AND RESTORED THE RCS TEMPERATURES.
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LER N0. 82-066/03L-0 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS 27 DURING UNIT _C00LD0WN, THE STEAM DUMP VALVES CAME OPEN WHEN THE STEAM DUMP CONTROL WAS PLACED IN MANUAL. THIS CAUSED A C00LD0WN BELOW 541 F WHILE THE REACTOR WAS STILL CRITICAL. THE OPERATOR QUICKLY CLOSED THE STEAM DUMP VALVES. AN INVESTIGATION REVEALED A DRIFT IN A CONTROLLER WHICH RESULTED IN AN ERR 0NE0US OUTPUT SIGNAL TO THE DUMP VALVES CAUSING THEM TO OPEN SLIGHTLY WITH NO OUTPUT FROM THE H/A STATION. THE CONTROLLER WAS RECALIBRATED WHICH CORRECTED THE PROBLEM.
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