ML20062L290
| ML20062L290 | |
| Person / Time | |
|---|---|
| Site: | Grand Gulf |
| Issue date: | 01/06/1981 |
| From: | Mcgaughy J MISSISSIPPI POWER & LIGHT CO. |
| To: | James O'Reilly NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| References | |
| REF-PT21-81-337-000 10CFR-21, 10CFR-50.55E, AECM-81-22, PT21-81-337, PT21-81-337-000, NUDOCS 8101270088 | |
| Download: ML20062L290 (3) | |
Text
sw wcn a m wapacomeomocxooma m m wn g P
wid co,ppI b u PART 21 IIERIFICATIO1 !O.
bi-3'51-600 CTPAM NVEAdsM Campans.-
m 9
DATE OF LETTFA dhOI DOGET f0. D -% ?!O O
DATE DISTRIBlRED d d4l ORIGINAL REPORT1 SUPPLEFBRAR?
3
..m.
[
DISTRIBlRION:
,c5-
.m y
N REACTOR (F.1f_
FUELCYCLE&
SAFEC4MRIE (S) -
a 9
M FMTERIALS (FD J
IE FILES m*=
EES IEFILES AD/SG AD/FFFSI AD/ROI EGIONS I,II,III,IV,V REGIONSI,II,III,IV,V PEGIGS I,II,III,IV,V V503R BR. R-IV VEEOR BR. R-IV VENDOR BR. R IV LDEB / FPA FIG 5715 f!PSS/FCFS SS-395 NRP/ DOL AEOD FIG 7602 LCEB/FPA f,4G 5715 ffSS / SG SS-881 NRR/ DOE AEOD FIG 7602 LDEB / FPA f4G 5715 NRR/DSI ASLBP FM 450 AEOD FIG 7602 NMT SAo/SP fig-7210A ASLBP E/W 450 NRR/ DOL CENTP L FILES 015 CEtERAL FILES 016
?
M 450 CENTPAL FILES ( GRON)
CBERALFILES (GR0iG l
CSER2.L FILES 016 PDR CENTRALFILES SS-395 CENTPAL FILES (WRON)
LPDR PDR PDR TERA L DR IPDR TERA i
C itFA CIID. :
PRELIMINAD.Y EVALUATION OF THE' ATTACHED REPORT INDICATES LEAD RESPONSIBILITY FOR FOLLCNJP AS SHOWN BELOW:
51 NRRE IEES 2 OTHER l
EES Pa' 8/1/80 l
'>U3e<00&&
E 91nW e..
icau m
s 6
(,
MO 2.[-,D b (~ Tj~,/)-.c *a
- _E-MISSISSIPPI POWER & LIGHT COMPANY I
!)
f Helping Build Mississippi
'I I
b _'" M b P. O.
B O X 164 0, J ACK S O N. MIS SIS SIP PI 3 9 2 05
- $$$/{,((SffoY,/r" January 6, 1981 Office of Inspection & Enforcement U. S. Nuclear Regulatory Commission Region II 101 Marietta Street, N.W.
Suite 3100 Atlanta, Georgia 30303 Attention:
Mr. J. P. O'Reilly, Director
Dear Mr. O'Reilly:
SUBJECT:
Grand Gulf Nuclear Station Units 1 and 2 Docket ::os. 5,0,-JM!.!R7..
File 0260/15525/15526 PPO-80/52, Standby Service Water Basin Fans, Status Report No. 2 AECM-81/22 On August 26, 1980, Mississippi Power & Light Company notified Mr. M. IIunt of your of fice of a Potentially Reportable Deficiency (PRD) at the Grand Gulf Nuclear Station (GG::S) construction site.
This deficiency concerned the failure of pillow block bearings in the Standby Service Water Easin Fans.
We are continuing our investicaticn of - this item for raporta-on this bility under 10CF.R50.55(e) and 10CFR21.. Our status report deficiency is attached.
We expect to complete our evaluation and report to you on this matter by April 22, 1981.
Ycurs truly, f
[
J. P. McGaughy, Jr.
y EWC:mt Attachment cc:
Mr. N. L. Stampley Mr. Victor Stello, Directo' Mr. G. B. Taylcr Mr. R. B. McGehee Division of Insp. & Enforcement South Miss. Ele.
Mr. T. B. Conner U. S. Nuclear Regulatory Comm.
Power Associat-Washington, D.C.
20555 P. O. Box 1589 11attiesburg, ME Member Middle South Utilities System
4 Attachment to AECM-81/22 Page 1 of 1 0
STATUS REPORT #2 FOR PRD-80/52 1.
Description of Deficiency Pillow block bearings on three of the eight Standby Service Water Cooling Tower Fans (QlPA1C002A-A, B-A, and C-B) for GGNS Units 1 and 2 supplied by Ceramic Cooling Tower of Fort Worth, Texas, failed completely after 300 hours0.00347 days <br />0.0833 hours <br />4.960317e-4 weeks <br />1.1415e-4 months <br /> of operation. This condition did not meet the Bechtel Design Specification 9645-M-015.1, which specified a minimum life expectancy of 100,000 hours0 days <br />0 hours <br />0 weeks <br />0 months <br /> for radial and axial shaft load, roller bearings.
II.
Approach to Resolution of the Deficiency The following actions have been planned to resolve this deficiency:
a.
Determine the cause of the bearing failures; b.
Evaluate the deficiency to determine its affect on safe oper-ations of the GGNS. This evaluation will assume that the deficiency remains uncorrected throughout the expected life-time of the plant; c.
Determine if similar deficiencies exist, or could exist, and take appropriate actions to correct them; and d.
Perform corrective actions to include actions to preclude recurrence.
The above actions are being_ tracked under Bechtel Quality Action Request, QAR F-218, which is available for inspection at the GGNS job site.
~
III.
Status of the Proposed Resolution The constructor and supplier are conducting evaluations to deter-mine the cause of the failure. The supplier has recommended re-placement of the damaged bearings with bearings having a different model number. Unit I bearings are scheduled to be replaced in January, 1981, with Unit 2 bearings to be replaced later.
Ceramic Cooling Tower has also recommended replacement of the drive shafts on the three affected fans with the drive shafts from the Unit 2 fans and that the Unit I drive shafts be returned to them for evaluation.
IV.
Reasons for Final Report Delay The investigation to determine reportability has not been completed.
V.
Projected Completion Date A final report will be available April 22, 1981.
O