ML20062J851

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Ro:On 801106,during Increase of Reactor Power from Hot Standby Condition,Main Steam Bypass Valve 3 Exhibited Erratic Operation.Caused by Defective Circuitry Board. Board Removed.Stable Pressure Control Sys re-established
ML20062J851
Person / Time
Site: Peach Bottom Constellation icon.png
Issue date: 11/06/1980
From: Ullrich W
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To: Grier B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
References
IEB-80-17, NUDOCS 8011120500
Download: ML20062J851 (2)


Text

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PHILADELPHIA ELECTRIC COMPANY Peach Bottom Atomic Power Station Delta, Pennsylvania

.j, Q "-d 17314 Emetentev.6g ps0 Mr. Boyce H.

Grier Office of Inspection sad Enforcement

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Region 1 W -j#!WCI5 United States Nuclear Regulatory Commission

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G31 Park Avenue King of Prassia, PA 19406

..r SU34BCT: _REPORTABLR OCCUKIENCE - PROMPT NQTI_PTCATION

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Ceafirming W. T.

Ulitich's conversation with Mr. Blough on November 6, 1980.

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Reference:

Docket No. 50-277 Peach Bottoa Unit 2 Technical Specification

Reference:

Nome IE Bulletin 80-17 (July 3, 1980)

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Report No. 2-80-27/IP Cecurrence Date:

November 6, 1980 7

Identification of decurr,ence_:_. --

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M During an ineresse of reactor power from a hot standby condition 6,,

cm November 6, m-1980, the No. 3 main steam bypass valve exhibited otratic operation.

Reactor power was reduced until the probles En.-

could be identified.

n-h Conditions Prior to occurrence:

THIS DOCUMENT CONTAINS

- M Unit 2 at hot standby.

g POOR QUALITY PAGES

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Apparent Cause of occurrence:

9.:

ti;:

Investigation of the posi. tion.Sontrolling circuitry associated l M. uith No. 3 bypass valve idedtifled a defective.c.ircuitry board.

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- Q T.his circuitry board.was res,oyed failing th~e bypass valve to a

W closed pe~sition.

Removing the defective component from the

}T cystem re-established a stable pressure control system frer the

. g; reactor via the usin stesa bypass valve system.

Reactor power j tras suh equently increased in preparation for returning the A

t=9 turbine generator to service.

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7.g Auslysis of Occurrence:

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.- V The Peach Sotton Unit 2 has installed nine asia steem bypass valves, h p otal capacity of this system is 25% of rated steam flow.

The

g: v rimary function of this bypass valve system is to centrol reactor

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eam pressure when the main turbine generator is not operating.

5 h val of one bypass valve from this systes decreases the main f

eas bypass capability from 25% to spyrexiastely 22%.

This A

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8011 12.0 To O-

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.kg'l f#.

.m

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reduction in bypass espability has minimum safety significanco.

-- The main-steam bypass sytes is not considered safety relatsd-and has no technical specification. associated with it.

Corrective Action:

Operability of the No. 3 bypass valve will be re-established after component repairs are completed.

Frevious Pailures:

Previous failures of this type have occurred but have not been reported since this reporting requirement was only established 4,._

on July 3, 1980, by Bulletin 80-17.

[s Very truly yours, M

t-f W. T.

Ullrich Station Superintendent T

WTU:llh

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