ML20062A939

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Monthly Operating Rept for Sept 1978
ML20062A939
Person / Time
Site: Humboldt Bay
Issue date: 10/04/1978
From: Bierbaum G
PACIFIC GAS & ELECTRIC CO.
To:
Shared Package
ML20062A938 List:
References
NUDOCS 7810180125
Download: ML20062A939 (4)


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a MONTHLY NARRATIVE REPORT OF OPERATING AND MAJOR MAINTENANCE EXPERIENCE This report describes the operating and maior maintenance experience for the month of September, 1978. This report was prepared by the Plant Staff and is submitted in accordance tith Section IX.I.1.c. of the Technical Specifications.

During the report period the reactor remained in the cold shutdown mode of operation. There were no significant events associated with the operation of the Unit. The following significant maintenance was completed during the month:

1)

No. 3 Screen Wash Pump - The pump performance decreased significantly and the pump was removed from service. The performance decrease was due to plugging of the suction bell by shells. The pump was overhauled, the pump pit cleaned, a pump suction strainer fabricated following a 10CFRSO.59 review and the pump returned to service.

2)

No. 3 Fire Pump Relief Valve - The pump was removed from service following the lifting and only partial reseating of the relief valve. The relief valve seat was cut and the sten galled. An investigation was initiated te determine if the valve performance could be improved and it was discovered that the valve had not been designed for horizontal installation (present method of installation).

The valve was overhauled and the piping modified for proper vertical installation following a 10CFR50.59 review.- This item is the subject of LER-78-003/03L-0.

3)

Radwaste Vent Monitor - The monitor failed high due to degraded electronic components. The unit was overhauled and returned to service.

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AVER AGE DAILY UNIT POWER LEVEL DOCKET NO.

f0- 8 G UNIT M&PP #n. 3 DATE 10,I4,l7 A COMPLETED BY C=.d RI ska.

TELEPHONE 707 4#1 2787 t

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MONTH 3 2 Pre >4m m1A DAY AVER AGE D AILY POhER LEVEL DAY AVER AGE DAILY POWER LEVEL (MWe Net) t MWe-Neti I

O 17 0

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2 O

19 0

3 0

20 0

4 5

21 0

0 0

22 0

6 0

0 7

23 0

24 O

0 9

0 25 10 0

26 O

O II O

27 0

28 O

I2 0

O 13 39 O

O 14 30 O

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~ LNS1RUCT10NS On this format.hst the average daily unit power levelin MWe Net for each day in the reporting month. Compute is the nearest whole megawatt.

(9 /77 )

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w OPERATING DATA REPORT DOCKET NO. KO - 113 DATE icl4f?n COMPLETED BY r,i rl,,tm.

TELEPHONE 707 9 4 21s7 OPERATING STATUS N08'S

1. Unit Name:

HBPP wa. 3

2. Reporting Period:

Se d=ls er 19 79

3. Licensed Thermal Power IMhti:

210 M

4. Nameplate Rating (Gross Mhel:

'M

5. Design Electrical Rating (Net MWel:

M

6. Madmum Dependable Capacity iGross MWel:
7. Maximum Dependable Capacity (Net MWet:
8. If Changes Occur in Capacity Ratings titems Number 3 Through 7) Since Last Report. Gise Reasons:

N/A

9. Power Lesel To which Restricted. If Any (Net MheI:

M!^

10. Reasons For Restrictions.lf Any:

M/A 1

This Month Yr to-Date Cumulatise 720 6fff 8319 c g 1I. Hours In Reporting Period

12. Number Of Hours Reactor Was Critical O

o qg,,i

13. Reactor Resene Shutdown Hours O

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14. Hours Generator On.Line
15. Unit Resene Shutdown Hours O

o o

16. Gross Thermal Energy Generated iMhH1' O

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17. Gross Electrical Energy Generated (MWHI O

O

'f 7 39 7 3 2

18. Net Electrical Energy Generated (Mh H)

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19. Unit Sersice Factor O

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20. Unit Availability Factor 0

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21. Unit Capacity Factor EUsing MDC Nett O

O Cl 9"A

22. Unit Capacity Factor (Using DER Netl o

O

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23. Unit Forced Outage Rate
24. Shutdowns Scheduled Oser Nest 6 Months (Type. Date and Duration of Eacht:

At / A

25. If Shut Down At End Of Report Period. Estimated Date of Startup:

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26. Units In Test Status (Prior to Commercial Operationi:

Forecast Achiesed INITIA L CRITICA LITY INITl A L ELECTRICITY CO\\lstERCI AL OPER ATION O

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