ML20059N386

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Forwards Special Rept SR-89-003-01 Re Results of 891008 Inservice Eddy Current Exam of Steam Generator Tubing.Visual Verification Performed to Verify Location of Plugs Installed Prior to Exam.Tube Plugs Secure & in Correct Locations
ML20059N386
Person / Time
Site: Waterford Entergy icon.png
Issue date: 10/03/1990
From: Mcgaha J
ENTERGY OPERATIONS, INC.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
W3A90-0414, W3A90-414, NUDOCS 9010120175
Download: ML20059N386 (8)


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t W3A90-0414 A4.05 QA October 3, 1990 I

U.'S.' Nuclear. Regulatory Commission ~-

1 ATTENTION:-

Document Control Desk' Washington, D.C.

20555

SUBJECT:

Waterford 3 SES Docket No. 50-382 License No.-NPF-38 ReDortina of Soecial"ReDort:

Gentlemen:

' Attached is Special Report Number SR-89-003-01'for;Waterford Steam Electric Station Unit 3.-

This Special Report' revision is

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l submitted per Technical Specifications 4.4.4.5 and 6.9.2.-

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.j very truly yours, i

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J.

. McGaha General Manager Plant Operations JRM/JEF:glp Attachment a

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Messrs.'R.D. Martin J.T. Wheelock'- INPO Records Center.

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W.M.

Stevenson i

D.L. Wigginton l'

NRC Resident Inspectors Office-i l-9010120175 501003 TE j

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-o SPECIAL REPORT.

SR-89-003-01' Stean Generator Eddy current Examination (3rd Refueling)

J INTRODUCTION In-service eddy current examination of Steam Generator (SG) tubing was conducted

'by Westinghouse Electric Corporation at Waterford Unit 3 on October 8, 1989.

This report is submitted.in accordance with Technical Specification (TS)~

4.4.4.5 which requires the complete results of this. inspection be submitted in a special report pursuant to TS. 6.9.2 within 12 months.following the inspection.

The examination included full length examination of 6;4% (600) of the tubes in SG #1..

In addition,.163 tubes in SG #1 and 162. tubes in SG #2 were examined to determine progression of tuba wear at: the diagonal strap' region near.the central cavity-(batwing region).

The tube examinations were conducted in accordance with USNRC Regulatory Guide-1.83'and ASME Section-XI using Westinghouse Procedure MRS 2.4.2 Gen-28, " Digital Multifrequency Eddy Current Inspection of Preservice and Inservice Heat Exchanger Tubing." The eddy current data was independently analyzed by level II A' data analysts.

RESULTS OF EXAMINATION STEAM GENERATOR #1 The random 6.4% examination in SG #1 resulted in 26 indications less than 20%,

7 indications equal to or greater than 20%~but'less than 40% and no indications-greater than 40% through wall..

The " batwing examination" resulted in 17 indications less than 20%, 11 indications equal to or greater than 20% but less than 40% and 1 indication greater than 40% through wall. Due to the one tube having a greater than 40%

through wall (44%) on SG #1, the tubes surrounding the preventively plugged

" Batwing region" of SG #2 were examined.

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'[In'additionto'theeddycurrentexaminationprogram,!avisualverificationwas:

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perf$rmed!.to : verify the': location of plugs-installed prior to ^this examination.

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sr All tube' plugs in SG.#1 were secure:acd in"the correct 11ocations..

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The initialT624% (600) examination.ofSG.#2 detected lthefollowing:i

ROW LINE

% THRU WALL

LOCATION -

LCOMMENTS^..

49 1,

15

- 25.

-< 20-%

' ~ 6H !

70t 38

. 20 %

TSC:

'19 :

67

<=20 %

- bW5 1

L96-.

76

<-20,%;

.- 1 C -

Q 95

77

< 20 % -

.50 1

{;

54' 78?

,< 20 %-

4CI

'[

t 1461 80::

< 20 %

.BWis 82 86-L< 20 %:-

'BW9 4.r 80-88

< 20 %~

.8C

[

.104 88

< 20 %-

7H.

1 147 91-

< 20 %

.BW9

.4 84

~92

< 20 %.-

7C t

75 105

<'20 %-

-2H T

a 75-105

'< 20 %

3H qq 75 105~

< 20 %

.4H 3

75 105

< 20 %'

SH>

-46 106

<-20-%-

6C:

Lj 77 113

< 20 %

8H 77 113

-<.20 %

6C' 1

136 120

< 20 %

BW1

-t

.30 126

'< 20 %'

TSC-t 67--

'133

< 20 %J

~TSC i

16 148

< 20 %

IC

.}

l:

22 158

.< 20 %

- 5C -

n q

L 32

.158

< 20-%'

5H k

62' 1158'

< 20 %.-

20-37 33 22 %

-TSH.

d

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s !

-V j

2 jC e

1

- R0W-LINE.

% THRU WALL LOCATION COMMENTS-125' 43' 39 %

BW8'

' PLUGGED 93 67 30 %^

7C 93

-93.

.N/A-BW9 PLUGGED DUE-TO-UNINTER-PRETABLE-PERMEABILITY

' INDICATION-AT

~BW9.-

95

.77' 25 %.

7C 104-l88-

~22 %

7H 147 95

-31:%

-BW9-

PLUGGED' 46 148 30 % '

-6H The sample of 163 tubes examined to determine' the progression ofiwear atil the-diagonal strap in' tubes surrounding the preventively-plugged region. detected -

- the following:

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R0W LINE

% THRU WALL LOCATION-COMMENTS l

33 71

< 20 %

2C 35 71

<'20'%

'4C-37 75

.< 20 %

BW9 43 75-

< 20 %_

BW9-

-l 146 80

< 20 %

-BW1-i 47 83

< 20 %

~ BW9 -

50 86

< 20 %

BW1-49 89

< 20 %

SC-l 48 90

< 20 %'

BW1 l

47 93

< 20 %

-7H 1

42 98

< 20-%-

BW9 45 99

< 20 %

BW1~

47 99

< 20 %

BW9 l

42 100

< 20 %

BW1

-1 L

42 100

< 20 %

BW9 I

48 100

< 20 %

BW9 41 103

< 20 %

BW9 1

v 7'

i h

1 3

1

_.'W hh

p R0W LINE

%-THRU WALL-'

LOCATION' COMMENTS

-35

.73

.44 %

4 iBW1

-PLUGGED-

-36' 74 20 %-

BW99 44 76

-25 %

BW9 ;-

-PLUGGED-

.43 79 27 %-

'BW5 51 87 38 %

BW9 PLUGGED 53-91 27 %

-7C 43 97 28 %

BW9 PLUGGED.

41 99 34 %

BW5.

PLUGGED, 4

38 100 27 %

BW1 PLUGGED 44' 100 20 %,

BW9 1

l 37 101 27 %

-BW9 PLUGGED

'l 36 102' 23 %-

.BW9 STEAM GENERATOR #2 The " batwing examination" resulted in-19 indications less than 20%, 8 indications j

equal to or greater than 20% but less than 40% and_no indications equal to or

-j greater than 40% through wall. Eleven. tubes outside of the batwing region which; t

contained some type of sonormality identified during previous refuelings were

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examined. There was-no expanded program in this generator.

i During' video scanning of SG #2, tuo tubes (row 33/line 73 and row 19/line 109) were discovered to be erroneously plugged on the hot 1eg side only.,These tubes were plugged during-Refuel 2 (RF2)-in place offtwo other tubes (row 33/line 103 and row'19/line 67) which were selected-to be plugged as a preven-l tive measure based on 31% and 33% through wall degradation respectively. The erroneously plugged tubes are mirror images of the tubes that had been selected for plugging.

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Further investigation revealed that the hot leg tube sheet was marked in error

-during RF2, This-taused a 180 degree offset in the. marking pattern and-resulted in plugging ine wrong tubes.

The marking equipment used during RF2' consisted of a television (TV) camera and ~ 1aser marking device.

This equipment configuration can cause the operator _to misjudge directions and mark the wrong tube.

Personnel error'has been determined to be the root cause of the improper l

tube plugging. A procedural inadequacy contributed to the event; specifically, the Westinghouse marking procedure identified a primary (TV/ laser) and alternate l

(eddy current probe) method. The~ primary method was~used during RF2; however, the eddy current probe method is the more accurate method for positive indexing of SG tubes. Use of the eddy current probe method would have precluded the l

improper marking of the SG tube sheet.

-Additionally, RF2 plug pattern verification techniques were questionable based j

on the fact that en adequate verification technique should have identified the error prior to commencing tube plugging.

Tube row 33/line 103, row 19/line 67, row 33/line 73, and row 19/line 109 have

'l been plugged on both the hot leg and cold leg sides. The Westinghouse tube l

markings procedure will be revised to designate che eddy current probe method as the primary method of tube. indexing at-Waterford 3.

The eddy current probe method was used during RF3 testing / plugging evolutions.

Current plug pattern verification techniques will be reviewed to ensure that adequate controls are utilized in order to preclude future tube marking errors. Any enhancements q

l resulting from the verification technique review will.be in place prior to RF4. This event has been discussed with the individual responsible.for the' erroneous tube marking. The SG #1 tube sheet was examined during RF3 and showed that all tubes were correctly plugged.

l Because only two tubes were erroneously plugged, SG thermal performance was I

not affected. The two tubes that were selected for pluggiag were plugged as a preventive measure, even though tube degradation was below the plugging limit 4

(40% below nominal wall thickness). Therefore, this event did not threate.. the health and safety of the general public or plant personnel.

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f Theiconditions found in SG'#2 were as follows:

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ROW.

LINE STATUS-1 l'

33 103-31%' degradation-(RF2), plugge'dP I

h on cold leg side'only. = Hot leg ='

side plugged during Refuel 3'.

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33 73 Sound tube, plugged on hot leg side only (RF2).

Cold leg side, j

-plugged during Refuel-3;

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19 67

-33% degradation (RF2),-plugged:'

on cold-leg side ~only.

Hot leg.

. side plugged during Refues 3.' M i

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q 19 109 Sound tube, plugged on. hot l leg-side only~(RF2).

Cold =1~g sidef.

e plugged'during Refuel'3.

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.j The sample of 162 tubes examined +> determine the progression of wear at th'e_

l diagonal strap in tubes surrounding the preventively plugged region detected-

.J the following:

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4 ROW LINE

% THRU WALL LOCATION

COMMENTS 1

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'30 70

< 20 %

- 4C.

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34 72

< 20 %

BW1

-l 35 73

< 20 %

7H

.)

l-37-75

< 20 %

BW1' l

1 37 75

< 20 %

BW9 l

1 41 77.

.< 20 %-

BW1 45 77

< 20 %

BW1

(;

51 81

< 20 %

BW9 i

I 47 83

< 20 %

BW1 51-85

< 20 %

BW1 d

6 x

_e L.,.1 g..

ROW

LINE '

% TIIRU WALL-LOCATION COMMENTS 50 86.

< 20.%

BW1 --

48.

c90

< 20 %'

-BW9.

49-91

< 20 %.

_BW1 S1

'91-

< 20 %

BW11 48

-92

< 20 %-

. BW1' 43 97

' < 20 %.

BW1.

i 47 97

< 20 %

BW1 1

39

'101-

< 20.%

BW1 42

'102 1<-.20 %

TSC 401 176 34~%~

BW1 PL11GGED 42 74 21 %

BW1 47 81-

! 32' L BW9_

PLUGGED 49 89

'34 %

-BW9 PLUGGED-47 93

- 26.: % -

BW1 45

'97 21 %'

BW1 I

40 100 29-%

BW9 PLUGGED' 36 102

.28 %

BV9 PLUGGED I

a Eleven tubes outside of the batwing region which contained some type of j

imperfection identified in previous <refuelings were examined. This examination detected the following:

l R0W LINE

% TIIRU WALL

' LOCATION COMMENTS 55 21

_< 20 %

1C' 105 31

< 2C %

Sll 22 44

< 20 %-

1 11 137 57

< 20 %

BW1 146 86

< 20 %

BW9 75 111.

< 20 %

.2C 2

114

< 20 %

3C

+F1.77" FROM SUPPORT 2

114

< 20 %

3C.

+8.02" FROM SUPPORT 95 61 22 %

4H l

138 114 25 %

TSil PLANT CONTACT J.E. Iloward, Procurement / Programs Engineering Manager, 504/464-3202.

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