ML20059J640

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Monthly Operating Rept for Oct 1993 for Monticello Nuclear Generating Plant
ML20059J640
Person / Time
Site: Monticello Xcel Energy icon.png
Issue date: 10/31/1993
From: Richard Anderson, Paustian H
NORTHERN STATES POWER CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9311120304
Download: ML20059J640 (5)


Text

Northem States Power Company 414 Nicollet Mall Minneapohs, Minnesota 55401 1927 Telephone (612) 330-5500 l

November 10, 1993 Monticello Technical Specifications Section 6.7.A.3 US Nuclear Regulatory Commission

[

Attn: Document Control Desk l

Vashington, DC 20555 s

MONTICELIA NUCLEAR GENERATING PLANT Docket No. 50-263 License No. DPR-22 Monthly Operating Report.

October. 1993 Attached is the Monthly Operating Report for October, 1993-for the Monticello Nuclear Generating Plant.

ifh P ger 0 Anderson Director i

Licensing and Management Issues c:

Director, Office of Resource Management Regional Administrator-III, NRC NRR Project Manager, NRC NRC Resident Inspector State of Minnesota - Kris Sanda Attachment I'

/.-

y 9311120304 931031 27

')

I PDR ~ADDCK 05000263 9h R

PDR

r OPERATING DATA REPORT q

3.-

1 DOCKET NO.

50-263' DATE 11-2-93 COMPLETED BY' H. H. Paustian TELEPHONE 612/295-5151 OPERATING STATUS

] Notes ~

]

l1. Unit Name :

Monticello

]

]

2. Reporting period:

OCTOBER

]

]

3. Licensed Thernal Power (MWt):

1670

]

]

4. Nameplate Rating (Gross MWe):

569

)

-]

5. Design Electrical Rating-(Net.MWe):

545.4~

]

.]

6. Maximum Dependable Capacity (Gross MWe): __564

)

-]-

7. Maximum Dependable Capacity (Net MWe):

536- ]

]

'8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last-1 Report, Give Reasota aw

9. Power Level To Which Restricted, If Any (Net MWe):

N/A

10. Reasons For Restrictions, If Any: __N/A THIS MONTH YR.-TO-DATE CUMULATIVE
11. Hours In Reporting Period 745 7296 195817
12. Number Of Hours Reactor Was Critical 736.0 5927.0 157911.7
13. Reactor Reserve Shutdown Hours 0.0 0.0

-940.7

14. Hours Generator On-Line 722.6 5860.5 155136.7
15. Unit Reserve Shutdown Hours 0.0 0.0 0.0
16. Gross Thernal Energy Generated (MWH) 1185000 9428445 238821858
17. Gross Electrical Energy Generated (MNH) 403161 3193610 80724410 1
18. Net Electrical Energy Generated (MWH) 388580 3062058.

77217945 l'

19. Unit Service Factor 97.0%

80.3%.

179.2%~

20. Unit Availability Factor' 97.0%

80.3%

79.2%

21. Unit Capacity Factor (Using MDC Net) 97.3%-

78.3%

73.6%'

22. Unit Capacity Factor (Using DER Net) 95.6%

77.0%

72.3%

~

23. Unit Forced Outage Rate 3.0%

1.8%

3.7%

24. Shutdowns Scheduled Over Next 12 Months (Type, Date, and Duration of Each)
None
25. If Shut Down At End Of Report Period, Estimated Date Of Startup.:N/A
26. Units In Test Status (Prior to Commercial Operation): N/A-Forecast Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION

4-s

' AVERAGE DAILY UNIT POWER LEVEL' DOCKET NO.

50-263-1 UNIT Monticello_._

DATE 11-2-93 COMPLETED BY H. H. Paustian-TELEPHONE 612/295-5151 MONTH OF OCTOBER DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER' LEVEL (MWe-Net)

(MWe-Net) 1 548.

17 160.

2 549.

18 93.

3

550, 19 544.

4 548.

20 545.

5 549.

21 549.

6 548.

22 548.

7 550.

23 550.

8

548, 24 549.

9 551.

25 549.

10 549.

26 548.

11 553.

27 550.

12 545.

28 548.

13 550.

29 549._

14

549, 30 550._

15 549.

31 550.

16 551.

INSTRUCTIONS On this format, list the average daily unit power level in MWe-Net for:each.

day in the reporting month.

Compute.to the nearest whole megawatt.

. NARRATIVE

SUMMARY

OF OPERATING EXPERIENCE DOCKET NO.

50-263 l-DATE 11 2 COMPLETED BY H. H. Paustian TELEPHONE 612/295-5151 MONTH OCT 10-1-93 to Power operation.

10-17-93 10-17-93 Power reduced to 35% to replace Recirc. MG set brushes.

Idle to loop cooled to >50 degrees colder than operating loop and 10-18-93 shutdown was required to allow idle loop startup.

10-18-93 to Power operation.

10-31-93 i

F

?

'l Note: Power operation defined as essentially 100% of rated power except for weekend load drops for specified surveillance testing.

v UNIT SHlHDOVNS AND POVER REDUCTIONS DOCKET NO.

50-263 UNIT NAME ~Monticello DATE 7 1-04-93 COMPETED BY ~B. H. Paustian REPORT MotRH _0ctober_

TELEPHONE [612/295-5151 -

No.

Date Duration Reason Method LER System Comp.

Cause & Corrective Ty(pe (hours)

(2) of No Me Me Action to 1)

Shutdown (4)

(5)

Prevent Recurrence (3) 8 10-17-93 F

22.4 B

1 N/A AD MG During a power reduction to change recire. MG set brushes, excessive idle loop cooldown forced a shutdown in order ?p, restart idle loop.

1 2

3 4

F: Forced Reason:

Method:

Draft IEEE Standard S: Scheduled A-Equipment Failure (Explain) 1-Manual 805-1984(P805-D5)

B-Haintenance or Test 2-Manual Scram C-Refueling 3-Automatic Scram 5

D-Regulator Restriction 4-Other (Explain)

IEEE Standard 803A-1983 E-Operator Training & License Examination F-Administrative G-Operational Error (Explain)

H-Other (Explain)