ML20059J146
| ML20059J146 | |
| Person / Time | |
|---|---|
| Site: | Crane |
| Issue date: | 08/31/1990 |
| From: | Heysek W, Hukill H GENERAL PUBLIC UTILITIES CORP. |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| C311-90-2124, NUDOCS 9009190194 | |
| Download: ML20059J146 (6) | |
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GPU Nuclear Corporation,
g f, Post Office Box 480 '
,. Route 441 South 1
"g' 17057 0191 Middletown, Pennsylvania 717 944 7621-
. TELEX 8442386..
Writer's Direct Dial Number:
Septerrber 14[1990
,C311-90-2124
[
.U. S. Nuclear. Regulatory Commission'
- 1
-Attna Document Control Desk Washington,.D.C.- 20555-t
,j.
Dear Sir I
'Three Mile Island Nuclear-. Station, Unit I (THIN)-
Operating License No. DPR-50 Docket No. 50-289 Monthly Operating Report; August 1990
(
Enclosed are two copies of the August, 1990 Monthly Operating Report for Three Mile Island Nuclear Station, Unit l.
t Sincerel'y, t
Vice President:& Director,?THI-1' l
-1 4
MDH/WGH:
cca T. T. Martin, USNRC N
s F. Young,-USNRC Attachments j
0^' 000 i
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9009190194 900831 PDR ADOCK 05000289 R
PDC g
GPU Nuclear Corporation is a subsidiary of General Pubkc'Utihties Corporation
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a OPERATIONS
SUMMARY
August 1990-I i
The unit entered the month operating at =96.5% power (limited by.high OTSG 1evel) producing 814 MWe gross electrical generation.
-A ATc.of -4.5'F was' input.to compensate for high OTSO level on the "B" side. The unit continued to operate.
at =96.5% power throughout the month.
MAJQR SAFETY RELATED MAINTENANCE l
During - August, the following major safety related maintenance! activity was-performed:
Screen Wash Ventilation Strainer - SW-S-2A Screen Wash Ventilation Strainer (SW-S-2A) - was. rebu lt i using L a new shaf t, j
bearings and seals.
A new drive gear unit was also installed,on the strainer
~I before the assembly was reinstalled in the housing. Post maintenance testing was i
completad satisfactorily and the unit returned to service.
Waste Evaoorator Condensate Storace Tank - WDL-T-11B A leak which developed on the recirculating piping inlet flange of the Waste Evaporator Condensate Storage Tank was repaired by replacing the existing 2"-150#
slip-on weld flange with a weld neck flange of the same size and pressure rating.
I Af ter NDE inspection found the weld antisf actory,' the-flange connection was made.
_j up and the recirculating piping returned to service.-
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OPERATING DATA' REPORT 4
' DOCKET'NO.
50-289 DATE 8-31-90 9
COMPLETED BY W.G. Heysek TELEPHONE 717-948-8191 I
i
' OPERATTNG STATUS
- 1. UNIT NAME:
1 NOTES-I THREE MILE ISLAND' UNIT 1 i
^
- 2. REPORTING PERIOD:
'l~
AUGUST-
,1990.1 1
'3.. LICENSED THERMAL POWER (MWT):.
' 2568. I l'
l4.'-NAMEPLATE RATING (GROSS MWE):
871. I 1
l
' 5. DESIGN EL ECTRICAL RATING (NET MWE):
i l
819.
l--
'6.' MAXIMUM DCPENDABLE CAPACITY-(GROSS MWE):'
.I
-l 856.- I 7.LMAXIMUM DEPENDABLE CAPACITY l(NET NWE):
l-808'. I i:
I I
O.
IF CHANGES OCCUR IN (ITEMS 3-7) SINCE.LAST REPORT, GIVE REASONS:
- )
- 9. POWER LEVEL TO WHICH RESTRICTED, IF ANY (NET MWE)
-4
- 10. REAaONS FOR RESTRICTIONS, IF ANY:
i
- 11. HOURS IN REPORTING PERIOD THIS MONTH: YR-TO-DATE-'CUMMULATIVE 1744.
5831.-
140232;
- 12. NUMBER OF HOURS REACTOR WAS' CRITICAL 744.0 4236.6, E66235;27
- 13. REACTOR RESERVE SHUTDOWN-HOURS
- 14. HOURS GENERATOR ON-LINE 0.0
'242 8' 2245.6?
j 744.O'
'4194.6 65190.7 l
' 15. UNIT RESERVE SHUTDOWN HOURS
- 16. GROSS THERMAL ENERGY GENERATED (MWH)
. 0.0 CG Co
.O.0-
'1846495.
9998559.
159570454.
,i
- 17. GROSS ELECTRICAL ENERGY GENERATED-(MWH) 604484..
3345090.
_53651759.
-i
'10. NET ELECTRICAL ENERGY GENERATED (MWH)
UNIT SERVICE FACTOR 569981.--
,3129757.
-50316246.
,19.
- 20. UNIT AVAILABILITY FACTOR 100.O' 71.9 46.5 100.0 71.9 46.5 i
- 21. UNIT CAPACITY FACTOR (USING MDC NET) 94.8 66.4-45.7
- 22. UNIT CAPACITY FACTOR (USING-DER NET),
'93.5 65.5-
' 43.8-1
- 23. UNIT-FORCED OUTAGE RATE O.0-5.4 48.2 I
24.
SHUTDOWNS SCHEDULED OVER'NEXT 6 MONTHS i
(TYPE, DATE, AND DURATION!OF EACH.
25.
IF SHUT DOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP :
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......u,..,...-..,4,.,...,..
,,,.,,...,.,,,.,,,,,..,,,,,,,,.3;
,,..,,,..m,
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AVERAGE ~ DAILY. UNIT POWER LEVEL--
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. DOCKET NO.
50-299" UNIT. 31-90 TMI-1 DATE COMPLETED BY. W.G. Heysek :
1 TELEPHONE' 717-948-8191-ii
. MONTH:t AUGUST
' DAY AVERAGE DA7'"' POWER LEVEL DAY AVERAGE: DAILY: POWER' LEVEL (MWE- 'T)
'(MWE-NET) 1.
775.
17-
-761.:
+
2 774.
18
' 759.
3 770.
19 760'.
4-767.
20 776.
5 766.
- 21..
776.
,6 762.
22
- 773.
7 766. 772.
L.l 8
769.
- 24 768.'
4 9
772.
-25
-.762.
O 10 770.
26.
760.-
11 s764.
27 755.12-765.
28 755.
13 762.
29
-760.
= 14 767.
30 767.
- i 15 764.
31'
- 768.
q
=
16 764.
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f" DOCKET Wo. 289-UNIT SHUTDOWHS AND POWER REDUCTICIIS IIIIIT EERBS TMI-1 DATE 8/31/90 REPORT 300er1T ADUUST 1990 COBrLETED BY.
W. G.'HEYSEK TERPECOBE (717)-948-8191 f'
plethod of Licensee System Component Coune & Corrective l
2 Action to 80 0 -
Date Type Duration Reeson Shutting Event Code Code (Hours)
-Down Report #
Prevent Recurrence 3
6 Reactor 5
5 6 g
j
- NONE -
b 2
3 4
1 Reason Method Exhibit G - Instructions F Forced for Properation of Date S Sciwasted A-Eqipment Felture (Explain) 1-sternset
~ Entry Sheets for Licensee 9-Maintenance or Test 2-seenuel Scram
.C-Refueling 3-Autoestic Scrom.
Event Report (LER) File (IRNEG-0161).
D-Regulatory Restriction.
4-other (Explain)
E-Operator Training & Licensing Examination F-Administrative 5 Exhibit 1 Same Source G-Operational Error (Explain) 5
- : -~
....:..-. -. - - =
REFUELING INFORMATION REQUEST
=1.
Name of Facility:
Three Nile = Island. Nuclear Station, Unit 1
- 2. Scheduled date for next refueling shutdowns.
October 4,11991"(9R).
- 3. scheduled date for-restart following current refueling: NA
- 4. Nill refueling or resumption of operation thereafter require a technical specification change or other license' amendment?. No. -
If answer is yesi in general,-what wil'l these be?
I If answer is no,. has the reland fuel. design and core configuration a
been reviewed by'your Plant 4 % y; Review Committee to determine j
whether any unreviewed safety.epek lons'are associated with the core--
reload (Ref.'10 CFR sec4jtn 50.59)f
.No' 1
3:
If no such review has taken place, when:is it scheduled? =6/1/91.
j
- 5. Scheduled date(s) for submitting proposed. licensing action _and supporting information: None. planned.
- 6. Important licensing considerations associated with refueling,'.e.g. new or-different fuel design or supplier, unreviewed design'or performance i
analysis methods, significant changes in fuel design,jnew operating; q
procedures:
-None.
-i
- 7. The number of fuel assemblies (a) in tho' core,Iand (b) in the spent fuel storage pools (a) 177 (b) 441
- 8. The present licensed spent fuel pool storage-capacity and the size of any increase in licensed storage capacity that has been requested or is-planned, in number of fuel assemblies:,
The present licensed capacity is 752.
Planning.to increase licensed' capacity through fuel pool: reracking is.in progress.
- 9. The projected date of the last refueling that can be discharged to th6 spent fuel pool assuming the present licensed capacity:
1991.is the last refueling discharge which allows full core off-load. capacity (177 fuel assemblies).
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