ML20059B375

From kanterella
Jump to navigation Jump to search
Special Rept:On 931014,inservice Insp of Tubes in Steam Generator Completed.Two Tubes Removed from Svc Due to Tube Degradation in Excess of TS Limit of 40 Percent Through Wall
ML20059B375
Person / Time
Site: Beaver Valley
Issue date: 10/25/1993
From: Freeland L
DUQUESNE LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
ND3MNO:3494, NUDOCS 9310280158
Download: ML20059B375 (4)


Text

.- .. - -- _-. , _. - . . - . . . _ . . - .. _ _,

,. r k '

e ~!Ap5 .

M T& phone H12) 3934000 Nuclear Group .

P O Bon . -

r.niwnmai. er isonum October 25,1993 ND3MNO:3494 i Beaver Valley Power Station, Unit No.2 .

Docket No. 50-412, License No. NPF-73  :

Special Reoort i

United States Nuclear Regulatory Commission Document Control Desk Washington, DC 20555  :

Gentlemen: ,

In accordance with Appendix A, Beaver Valley Technical Specifications 4.4.5.5.a, "Stean' Generators," the following Special Report is submitted. This report is required to document the results of the Inservice Inspection of the steam generator tubes, performed during the Fourth Refueling Outage.

On October 14, 1993, the inservice inspection of the tubing in steam generators 2RCS-  ;

SG21A (S/G A), 2RCS-SG21B (S/G B), and 2RCS-SG21C (S/G C) was completed. The number of tubes inspected is documented below.

One hundred percent (100%) of all inservice tubes in the three steam generators _ were inspected during the outage. Two tubes were removed from_ service due to tube degradation in excess of the Technical Specification limit of 40 percent through wall. Two additional tubes were removed from service due to denting.

Six Babcock & Wilcox (B&W) rolled plugs on the cold leg side of S/G 21C were replaced with Babcock & Wilcox Inconel 690 plugs, completing the replacemeut of all Inconel 600 B&W plugs at Unit 2.

A review of the inspection data coupled with related industry experience resulted in the precautionary plugging of thirty-four (34) tubes in 2RCS-SG21A, twenty-three (23) tubes in 2RCS-SG21B, and twenty-nine (29) tubes in 2RCS-SG21C. The tubes were plugged based on .

the indications received at the following locations: U-Bend, Support Plate, Free Span, and Top ,

of Tubesheet. Additionally, eight (8) tubes in 2RCS-SG21B were plugged following stabilization due to loose part indications received during steam generator secondary side foreign object inspections.

N ih 9310280158 931025 PDR 's p S ADOCK 05000412 PDR gpip #

'. i October 25,1993 ND3MNO:3494 l l

Page 2 l

The following table documents the number of tubes plugged (>40% through wall) this _

outage in each steam generator, the number of tubes plugged following stabilization, the  ;

I number of tubes plugged as a precautionary measure due to the indications received at the locations specified above, the number of tubes previously plugged, and the total number of l tubes plugged:

S/G S/G S/G 21A 21B 21C Tubes plugged this outage 0 2 0  ;

(for ir 'ications > 40 percent)

Nurn , s.' tubes stabilized 0 8 0 Number of tubes plugged as 34 23 29 precautionary Tubes previously plugged 11 7 15 n

Total tubes plugged 45 40 44

(% of tubes) (1.33 %)- (1.18%) (1.30%)

I g

- L Cd' '

L. R. Freeland General Manager Nuclear Operations i

JGT/ke Attachment

.., ew.., ~ , , , . + -

r -

-y,-, , ,-

-smn,.

. o October 25,1993 ND3MNO:3494 "Page 3 i

cc: Mr. T. T. Martin, Regional Administrator United States Nuclear Regulatory Commission Region 1 475 Allendale Road King of Prussia, PA 19406 Mr. G. E. Edison, BVPS Licensing Project Manager .

United States Nuclear Regulatory Commission Washington, DC 20555 Larry Rossbach, Nuclear Regulatory Commission. [

BVPS Senior Resident Inspector i J. A. Holtz, Ohio Edison 76 S. Main Street Akron, OH 44308 Larry Beck Centerior Energy 6200 Oak Tree Blvd.

Independence, OH 44101-4661 INPO Records Center 700 Galleria Parkway Atlanta, GA 30339-5957 Mr. Robert Barkanic Department of Environmental Resources P.O. Box 2063 16th Floor, Fulton Building Harrisburg, PA 17120 Director, Safety Evaluation & Control .,

Virginia Electric & Power Co.

P.O. Box 26666 One James River Plaza Richmond, VA 23261 W. Hartley Virginia Power Company 5000 Dominion Blvd.

2SW Glenn Allen, VA 23060 )

l

October 25,1993 ND3MNO:3494 Page 4 l

..i' J. M. Riddle Halliburton NUS

-t Poster Plaza 7 661 Anderson Drive Pittsburgh, PA 15220 Bill Wegner, Consultant 23 Woodlawn Terrace Fredricksburg, VA 22405 0

'T 2

1 b.

w -,.* *-. -

enm -

--ar---e v - - - -, w = * - ,- -t v w r --- -