ML20058P665
ML20058P665 | |
Person / Time | |
---|---|
Site: | Summer ![]() |
Issue date: | 07/31/1990 |
From: | Haltiwanger J SOUTH CAROLINA ELECTRIC & GAS CO. |
To: | |
Shared Package | |
ML20058P661 | List: |
References | |
NUDOCS 9008170260 | |
Download: ML20058P665 (8) | |
Text
Document Control Desk July Monthly Operating Report Page 1 ATTACHMENT I AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.: 50/395 UNIT: V. C. SUMMER I DATE: 08/01/90 COMPLETED BY: J. W.'HALTlWANGER TELEPHONE: (803) 345-4297 JULY 1990 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) (MWe-Net)
- 1. 881 17. 879
- 2. 881 18. 080
- 3. 880 19, 880 4, 881 20. 881
- 5. 880 21. 881
- 6. 785 22, 881
- 7. -35 23. 879
- 8. 171 24, 879
- 9. 684 25, 879 10, 880 26. 878
- 11. 879 27, 878
- 12. 880 28. 878
- 13. _ 880 29. 879
- 14. 881 30. 879 15, 880 31. 878
- 16. 879 l
'9008170260 400815 PDR ADOCK 05000393 R PDC
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Document Control Desk July Monthly Operating Report Page 2 ATTACHMENT 11 OPERATING DATA REPORT DOCKET NO.: 50/395 UNIT: V. C. SUMMER I DATE: 8/1/90 COMPLETED 8Y: J. W. HALTlWANGER TELEPHONE: (803) 345-4297 OPERATING STATUS
- 1. Reporting Period: July 1990 Gross Hours in Reporting Period: 744 2.CurrentlyAuthorizedPowerLevel(MWt): 2775 Max. Depend. Capacity (MWe-Net): _.886 DesignElectricalRating(MWe-Net):- 900 3.PowerLeveltoWhichRestricted(ItAny)(MWe-Net): N/A
- 4. Reasons for Restrictions: N/A THIS MONTH YR TO DATE CUMULATIVE
- 5. Number of Hours Reactor Critica 744.0 3673.3 43686.1
- 6. Reactor Reserve Shutdown Hours 0.0 0.0 0.0
- 7. Hours Generator on Line 716.7 _3589.4 42749d
- 8. Unit Reserve Shutdown Hours {
0.0 0.0 0.0 '
9.'GrossThermalEnergyGenerated(MWH) 1928248 9657093 112027406
- 10. Gross Electrical Energy (MWH) .635880 3193010 _37054719
- 11. Het Electrical Energy Generated (MWH) 608524 3039486 35139402
- 12. Reactor Service Factor 100.0 72.2 75.7-
- 13. Reactor Availability Factor 100.0 72.2 75.7
- 14. Unit Service Factor 96.3 70.6 74.1
- 15. Unit Availability Factor 96.3 70.6 74.1 16.UnitCapacityFactor(UsingMDC) 92.4 67.5 68.8
- 17. Unit Capacity Factor (Design MWe) 90.9 66.4 67.7
- 18. Unit Forced Outage Rate 0.0 0.0 8.3 19.ShutdownsSchaduledOverNext6 Months (Type.Date&DurationofEach):
N/A
- 20. If Shut Down at End of Report Period. Estimated Date of Startup:
N/A !
(
- 21. Units in Test Status (Prior to Commercial Operation): N/A /
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Document Control Desk !
March Monthly Operating Report ;
Page 2 "
A'iTACHMENT II ,
OPERATING DATA REPORT
{
DOCKET NO.: 50/395 UNIT: V. C. SUMMER I DATE: 4/1/90 COMPLETED BY: J. W. HALTlWANGER .
TELEPHONE: (803) 345 4297
( OPERATING STATUS
- 1. Reporting Period: March 1990 Gross Hours in Reporting Period: 744 ,
- 2. Currently Authorized Power Level (MWt): 2775 i Max. Depend. Capacity (MWe. Net): i
__ B85 Design Electrical Rating (MWe-Net): 900
- 3. Power Level to Which Restricted (If Any)(MWe-Net): N/A
- 4. Reasons'for Restrictions: !!/A THIS MONTH YR TO DATE CUMULATIVE
- 5. Number of Hours Reactor Critica 554.0 1970.1 41982.9
- 6. Reactor Reserve Shutdown Hours 0.0 0.0 0.0 '
- 7. Hours Generator on Line 551.0 -1967.4 41127.0
- 8. Unit Reserve Shutdown Hours 0.0 0.0 0.0
- 9. Gross Thermal Energy Generated (MWH) 1508020 5426744 107797057 10.GrossElectricalEnergy(MWH) 500300 1798980 35660682
- 11. Het Electrical Energy Generated (MWH) 476372 1722395 33822311
- 12. Reactor Service Factor 74.5 91.1 76.7 i
- 13. Reactor Availability Factor 74.5 91.2 76.7
- 14. Unit Service Factor 74 91.1 75.1
- 15. Unit Availability Factor 74. 1 90.1 75.1
- 16. Unit Capacity Factor (Using MDC) 72.3 90.1 69.8
- 17. Unit Capacity Factor (Design MWe) _ 71.1 88.6 68.6
- 18. Unit Forced Outage Rate 0.0 0.0 8.6 ,
- 19. Shutdowns Scheduled Ov6r Next 6 Months (Type, Date & Duration of Each):
REFUELING OUTAGE. 03/23/90. 65 DAYS
- 20. If Shut Down at End of Report Period, Estimated Date of Startup:
05/27/90
- 21. Units in Test Status (Prior to Commercial Operation): N/A i
i M._
Document Control Desk April Monthly Operating Report Page 2 ATTACHMENT II OPERATING DATA REPORT DOCKET NO.: 50/395 UNIT: V. C. SUMMER I DATE: 5/1/90 COMPLETED BY: J. W. HALTIWANGER TELEPHONE: (803) 345-4297 OPERATING STATUS
- 1. Reporting Period: April _191Q Gross Hours in Reporting Period: 744 2.CurrentlyAuthorizedPowerLevel(MWt): 2775 Max. Depend. Capacity (MWe-Net): _ . . 885 Design Electrical Rating (MWe. Net): 900
- 3. Power Level to Which Restricted (If Any)(MWe. Net): N/A
- 4. Reasons for Restrictions: M THIS MONTH YR TO DATE CUMULATIVE
- 5. Number of Hours Reactor Critica 0.0 1970.1 41982.9
- 6. Reactor Reserve Shutdown Hours 0.0 0.0 0.0
- 7. Hours Generator on Line 0.0 1967.4 41127.0
- 8. Unit Reserve Shutdown Hours 0.0 0.0 0.0 ;
- 9. Gross Thermal Energy Generated (MWH) 0 5426744 197797057
- 10. Gross Electrical Energy (MWH) 0 1798980 35660689 !
- 11. Net Electrical Energy Generated (MWH) -5176 1717219 33817135 =
- 12. Reactor Service Factor 0.0 68.4 75.7 '
- 13. Reactor Availability Factor _ 0.0 68.4 75.7
- 14. Unit Service Factor 0.0 68J 74.1
- 15. Unit Availability Factor 0.0 68.3 74.1
- 16. Unit Capacity Factor (Using MDC) 0.0 67.4 68.9
- 17. Unit Capacity Factor (Design MWe) 0.0 66.3
- 18. Unit Forced Outage Rate 67.7k 0.0 0.0 8.6
- 19. Shutdowns Scheduled Over Next 6 Months (Type, Date & Duration of Each):
REFUELING OUTAGE. 03/23/90. 65 DAYS
- 20. If Shut Down at End of Report Period. Estimated Date of Startup:
05/27/90
- 21. Units in Test Status (Prior to Commercial Operation): N/A l
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l Document Control Desk May Monthly Operating Report Page 2 ATTACHMENT 11 OPERATING DATA REPORT DOCKET NO.: 50/395 !
UNIT: V. C. SUMMER I DATE: 6/1/90 !
COMPLETED BY: J. W. HALTlWANGER TELEPHONE: (803) 345 4297 OPERATING STATUS ,
- 1. Reporting Period: May 1990 Gross Hours in Reporting Period: 744
- 2. Currently Authorized Power Level (MWt): 2775 Max. Depend. Capacity (MWe. Net): 885 Design Electrical Rating (MWe. Net): 900 :
- 3. Power Level to Which Restricted (If Any)(MWe. Net): N/A
- 4. Reasons for Restrictions: WA THIS MONTH YR TO DATE CUMULATIVE
- 5. Number of Hours Reactor Critica 239.2 2209.3 42222
- 6. Reactor Reserve Shutdown Hours 0.0 . 0.0 0.0
- 7. Hours Generator on Line 185.3 12152.7 41312.3 j 8. Unit Reserve Shutdown Hours 0.0 00 0.0-l 9.GrossThermalEnergyGenerated(MWH) _305992 5732736 108103049
- 10. Gross Electrical Energy (MWH) 95440 1894420 35756129 l 11.HetElectricalEnergyGenerated(MWH) 77568 1794787 33894703
- 12. Reactor Service Factor 32.2 61.1 75.1
- 13. Reactor Availability Factor 32.2 --61.2 75.1
- 14. Unit Service factor 24.9 59.4 73.5
- 15. Unit Availability factor 24.9 59.4 73.5
- 16. Unit Capacity Factor (Using MDC) 11.8 56._0 68.1
- 17. Unit Capacity factor (Design MWe) 11.6 55.0 67.0
- 18. Unit Forced Outage Rate 0.0 0.0 8.5 19.ShutdownsScheduledOverNext6 Months (Type,Date;&DurationofEach):
N/A
- 20. If Shut Down at End of Report Period. Estimated Date of Startup:
N/A
- 21. Units in Test Status (Prior to Commercial Operation): N/A
Document Control Desk June Monthly Operating Report Page 2 ATTACHMENT 11 OPERATING DATA REPORT DOCKET NO.: 50/395 UNIT: V. C. SUMMER I DATE: 7/1/90 COMPLETED BY: J. W. HALT!WANGER TELEPHONE: (803)345-4297 OPERATING STATUS
- 1. Reporting Period: . June 1990 Gross Hours in Reporting Period: 744
- 2. Currently Authorized Power Level (MWt): 2775 Max. Depend. Capacity (MWe. Net): . 885 Design Electrical Rating (MWe. Net): 900 3.PowerLeveltoWhichRestricted(IfAny)(MWe. Net): N/A
- 4. Reasons for Restrictions: N/A THIS MONTH YR TO DATE CUMULATIVE
- 5. Number of Hours Reactor Critica 720.0 2229.3 42942.1
- 6. Reactor Reserve Shutdown Hours 0.0 0._0 0.0
- 7. Hours Generator on Line __720.0 2872.7 42032.3
- 8. Unit Reserve Shutdown Hours 0.0 0.0 0.0
- 9. Gross Thermal Energy Generated (MWH) 1996109 7728845 110099158 10.GrossElectricalEnergy(MWH) _b62710 2557130 36418839
- 11. Het Electrical Energy Generated (MWH) _636175 2430962 34530873
- 12. Reactor Service factor 100.0 67.4 75.4
- 13. Reactor Availability factor 100.0 67.4 75.4
- 14. Unit Service Factor 100.0 66.1 73.8
- 15. Unit Availability factor 100.0 66.1 73.8
- 16. Unit Capacity Factor (Using MDC) 99.8 63.2 68.5
- 17. Unit Capacity Factor (Design Mde) 98.2 62.2 67.4
- 18. Unit forced Outage Rate 0.0 0.0 8.4
- 19. Shutdowns Scheduled Over Next 6 Months (Type. Date & Duration of Each):
N/A
- 20. If Shut Down at End of Report Period. Estimated Date of Startup:
N/A
- 21. Units in Test Status (Prior to Commercial Operation): N/A
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t Document Control Desk t July Monthly Operating Report i Page 3 ATTACHMENT III t, NIT SHUTDOWNS AND POWER REDUCTIONS f
DOCKET NO.: 50/395 UNIT: V. C. SUMMER 1 DATE: 08/01/90.
COMPLETED BY: J. W. HALT!WANGER .
TELEPHONE: (803) 345-4297 ,
JULY 1990 Method of TYPE Shutting F or S Duration No. Date Reason Down the Corrective Actions /
forced or (Hours) Reactor or Coments Scheduled Reducing Power i
?
2 7/6/90 S 27.3 8 1 Repair Altere; Coupling
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Document Control Desk l July Monthly Operating Report )
Page 4 ;
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ATTACHMENT IV i NARRATIVE
SUMMARY
OF OPERATING EXPERIENCE j DOCKET NO.: 50/395 UNIT: V. C. SUMMER I !
DATE: 08/01/90 l COMPLETED BY: J.-W. HALTIWANGER TELEPHONE: (803)345-4297 i JULY 1990 9
V. C. Summer Nuclear Station operated at approximately 100% power through July 5, 1990.
On July 6 at 2010 hours0.0233 days <br />0.558 hours <br />0.00332 weeks <br />7.64805e-4 months <br />, power reduction commenced to correct a misalignment of the alterex coupling. The generator breaker was opened at 2250 hourt. The reactor was maintained critical in Mode 2 until 0045 hours5.208333e-4 days <br />0.0125 hours <br />7.440476e-5 weeks <br />1.71225e-5 months <br /> on July 8 when Mode 1 was entered. The generator breaker was closed at 0208 on July 8 and power escalation began. Following a twelve hour hold for water chemistry at 30 percent power the plant reached full power at 1800 hours0.0208 days <br />0.5 hours <br />0.00298 weeks <br />6.849e-4 months <br /> on July 9. '
V. C. Summer Nuclear Station operated at approximately 100% power for the remainder of July 1990, i
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