ML20058K704

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Suppl to Ler:On 741230,RCIC Steamline Isolation Valve Failed to Close During Surveillance Test
ML20058K704
Person / Time
Site: Monticello Xcel Energy icon.png
Issue date: 03/26/1975
From: Clarity M, Mayer L
NORTHERN STATES POWER CO.
To: Anthony Giambusso
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
References
LER-LER-750326, NUDOCS 9102130516
Download: ML20058K704 (2)


Text

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(PLEASE PRINT ALL REOUMED SIPORMOT *J '

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(CENSE E LCg NS[

EVENT l

NAME LCENSE NUMBE A TYPE TYPE l

blM!N ! Ml ' ! P ! 1j l 0 l 0!-l0 l0 l 0 ! 0 l 0 !-I 0l0 l l4 l1 l1 l1 l1 l l0l1l 7 89 14 16 25 26 30 31 32 h I[ uke DOCK E T NUMBE R EVtNT DaTE RE PDAT DATE CATE GORv T

D 1 CON'T l P I 0 l d

W l Ol 5l 0l-l0 !2 l6 l3 l l 1 l 2 ! 31 O! 7l 4l l 0l 31286 l7 l 5 ;

7 8 57 58 59 60 61 68 69 74 75 80 CVENT DESCHiPTION

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HE I uuring surveillance test, acIc outboare steam line isolation valve failee to close. l 7 89 80

$l The redundant isolation valve was operable.

Similar event occured August 26, 1974

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7 8D 80

@l (A0 4-25) l 7 89 80

$l l

7 39 B0 bl l

7 89 80 gg SYSYEM CAUSL COMPUNENT COMPONENT CDDE CODE COMPONEN1 CCDC SUPPULA MANUFACTUHER VOLATON O

ISlDl d lV ! A lL l V! OlPJ lA l l L 12 l010 l QI 7 89 10 11 12 17 43 44 47 46 CAUSE DESCRIPTION DE l Valve was inspected during recent refueling outage and the valve's limit and torque l 7 89 80

[switcheswereadjusted.

In addition. it was found that the main gear train grease j 0

7 89 RO 1O l and limit switch grease had deteriorated.

The gear trains were thoroughly cleaned l

7 89 80 i aCa.rt <

u.:Twoo os 51ATUS

% POWFA OTHEA STATUE D;SCO d c

  • 0:SCDvfCv DE SCAePT ON h

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13 44 4b 46 B0 FonM or ACTfVriv CONTENT ALLEAS D OF AELE ASE AMOUNT CF ACTrvrf y LOCATON OF AELEASE h

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7 8 9

10 11 44 45 80 PERSONNEL EXPOSURES NUM BE R TvPf D E SCAiP' ON 13 l 0 l 010l

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7 89 11 12 13 BO PERSONNEL INJURIES NUMBEA DE SCRIPT ON 8 10101 01 1

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7 89 11 12 60 OFFSITE CONSEQUENCES hI NA l

7 89 80 LOSS OR DA4 AGE TO FACILITY TYPE DE SCRIPT ON

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1 7 E9 10 80 O2130516 750326 PUBLICITY ADOCK 05000263 l

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l NA CF 7 09 go ADDITIONAL FACTORS

]l Cause Description (Cont'd) and repacked.

Tha valve. ras demonstrated to l

7 89 80 j

function properly prior to return to power operation following the outage.

7 89 80 M H Clarity 612-295-5151 NAME:

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GPO $0h*$$T L

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e~ t g NORTHERN 5TATES POWER COMPANY MIN N E A PO L.S S. MI N N E S OTA 55401 2.\\ g.fu

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March 26,1975 S F" 5

-o Mr. A. Giambusso, Dprector6 9

~A Division of Reactor Licensing Y'?f)s s

U S Iuclear Regulatory Cocnission v.

Washington, D. C.

20555 Supplement to Licensee Event Report to the NRC RCIC Steamline Isolation Valve Failed to Close

Dear Mr. Giambusso:

1975 is An update to our previous Licensee Event Report dated January 9, reproduced on the back of this letter.

Yours very truly, DC M

poA L 0 Mayer, PE Manager of Nuclear Support Services LOM/yb cc:

J G Keppler G Charnoff Minne ota Pollution Control Agency h

Attn:

E A Prytina y

-s dJ14

-over-

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